Cessna T210M Safety Record
Complete NTSB accident and incident history. 189 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Aug 07, 2005 | Kissimmee, FL | N732WN | Incident | substantial | A loss of engine power due to the pilot's inaccurate fuel consumption calculations and subsequent fuel exhaustion. |
| Jul 14, 2005 | TwentyninePalms, CA | N210NS | Incident | substantial |
the pilot's failure to verify the current local wind condition that resulted in his selection of the wrong runway and an inadvertent downwind landing,…the pilot's failure to verify the current local wind condition that resulted in his selection of the wrong runway and an inadvertent downwind landing, a runway overrun and a ground collision with objects. A factor in the accident was the short runway and its dirt surface, which reduced brake effectiveness. |
| Jan 14, 2005 | Mesa, AZ | N761YH | Incident | substantial | the pilot's failure to use the emergency gear extension procedure to manually extend the landing gear to the down and locked position. |
| Jul 04, 2004 | Mallard Creek, ID | N761TD | Incident | substantial | Improper touchdown during landing. A factor contributing to the accident was soft ground conditions. |
| May 30, 2004 | Santa Rosa, CA | N121JR | Incident | substantial |
Maintenance personnel's improper installation and servicing of a retaining ring, which resulted in the failure of the landing gear door actuator and f…Maintenance personnel's improper installation and servicing of a retaining ring, which resulted in the failure of the landing gear door actuator and failure of the landing gear extension system during landing. |
| Aug 10, 2003 | Hialeah, FL | N86PH | Incident | substantial |
Spinning of the crankshaft No. 2 main bearing for undetermined reasons resulting in damage to the aft cheek of the No. 2 main bearing journal, fatigue…Spinning of the crankshaft No. 2 main bearing for undetermined reasons resulting in damage to the aft cheek of the No. 2 main bearing journal, fatigue failure of the crankshaft cheek, failure of the engine in cruise flight, and damage to the airplane during the subsequent forced landing on unsuitable terrain.. |
| Jul 05, 2003 | Essex, MT | N761QN | Incident | substantial | The unexpected transit of a deer across the runway which impacted the aircraft during the pilot's aborted landing. |
| Jul 02, 2003 | Aspen, CO | N761XE | Incident | substantial |
the failure of the landing gear actuator switch. Factors relating to the accident were the false landing gear indication, the precautionary landing, …the failure of the landing gear actuator switch. Factors relating to the accident were the false landing gear indication, the precautionary landing, and the improper maintenance adjustment performed on the landing gear switch prior to the accident flight. |
| Nov 25, 2002 | Lakeland, FL | N6026N | Incident | substantial | The collapse of the main landing gear for undetermined reasons. |
| Dec 25, 2001 | SANTA ROSA, CA | N1309M | Incident | substantial |
The pilot's inadequate preflight and in-flight planning/decision resulting in miscalculation of fuel consumption, fuel exhaustion and loss of engine p…The pilot's inadequate preflight and in-flight planning/decision resulting in miscalculation of fuel consumption, fuel exhaustion and loss of engine power. Factors were rough terrain in a vineyard, power lines in the landing area, and night time. |
| Oct 30, 2001 | Salem, IL | N761UV | Incident | substantial | The ruptured hydraulic hose. |
| May 27, 2001 | Portland, OR | N761DL | Incident | substantial | A burst hydraulic line and consequent total loss of hydraulic fluid from the landing gear, which disabled landing gear operation. |
| Apr 06, 2001 | Abilene, TX | N555HG | Incident | substantial |
the loss of engine power while on final approach due to fuel starvation as a result of the pilot's improper use of the fuel selector. A contributing …the loss of engine power while on final approach due to fuel starvation as a result of the pilot's improper use of the fuel selector. A contributing factor was the elevated runway edge. |
| Feb 03, 2001 | Kelseyville, CA | N761SE | Incident | substantial |
The failure of the pilot to comply with emergency procedures contained in the Pilot's Operating Handbook, which resulted in an excessively rich mixtur…The failure of the pilot to comply with emergency procedures contained in the Pilot's Operating Handbook, which resulted in an excessively rich mixture and loss of engine power. |
| May 25, 2000 | BOISE, ID | N761VZ | Incident | substantial |
The deterioration and subsequent leakage of a hydraulic line which resulted in the total loss of hydraulic fluid and the inability of the pilot to ext…The deterioration and subsequent leakage of a hydraulic line which resulted in the total loss of hydraulic fluid and the inability of the pilot to extend the landing gear into the locked position. |
| May 21, 2000 | LARAMIE, WY | N66DF | Incident | substantial |
The pilot-in-command's failure to confirm, the landing gear was down and locked. Factors were the check pilot's failure to confirm the landing gear w…The pilot-in-command's failure to confirm, the landing gear was down and locked. Factors were the check pilot's failure to confirm the landing gear was down and locked, and the sun glare. |
| Feb 16, 2000 | ELFRIDA, AZ | N761KC | Incident | substantial |
The company mechanic's failure to correctly install one or more of the crankshaft counterweight pin retaining plate snap rings, specifically ensuring …The company mechanic's failure to correctly install one or more of the crankshaft counterweight pin retaining plate snap rings, specifically ensuring that the snap rings were fully seated in their grooves. This led to the complete separation of the No. 2 leading counterweight and the partial separation of the No. 3 trailing weight from the crankshaft and a resulting internal catastrophic engine failure. A factor in the accident was the lack of definitive procedural guidance in any of the engine manufacturer's reference material, available at the time, on the correct installation of these components. |
| Jul 16, 1999 | CEDAR CITY, UT | N6029N | Incident | substantial |
The pilot's failure to follow alternate landing gear extension procedures. Factors were the main landing gear failure to extend and a loss of electri…The pilot's failure to follow alternate landing gear extension procedures. Factors were the main landing gear failure to extend and a loss of electrical power. |
| Sep 02, 1998 | MCALLEN, TX | XARIM | Incident | substantial | The pilot's inadequate compensation for the crosswind resulting in a loss of control. A factor was the crosswind. |
| May 20, 1998 | SANTA BARBARA, CA | N6056B | Incident | destroyed | The pilot's mismangement of the fuel by the improper position of the fuel tank selector. |
| Aug 29, 1997 | SAN MARTIN, CA | N761HQ | Incident | substantial |
Installation of improper connecting hardware by maintenance personnel, and, the inadequate inspection of the installed hardware by inspection personne…Installation of improper connecting hardware by maintenance personnel, and, the inadequate inspection of the installed hardware by inspection personnel resulting in separation of the engine throttle linkage. |
| Jul 02, 1997 | KERRVILLE, TX | N761FM | Incident | substantial |
The disintegration of the #1 cylinder piston resulting from a detonation/pre-ignition condition due to an unknown reason. A factor was the lack of sui…The disintegration of the #1 cylinder piston resulting from a detonation/pre-ignition condition due to an unknown reason. A factor was the lack of suitable terrain for the forced landing. |
| Oct 10, 1996 | MENTOR, KY | N6163N | Incident | substantial |
the pilot's improper planning/decision, which resulted in fuel exhaustion and loss of engine power. Factors relating to the accident were: the inaccu…the pilot's improper planning/decision, which resulted in fuel exhaustion and loss of engine power. Factors relating to the accident were: the inaccurate fuel quantity gage, and the light condition at dusk. |
| Oct 04, 1995 | APOPKA, FL | N6508B | Incident | substantial | THE PILOT'S FAILURE TO PERFORM FUEL CONSUMPTION CALCULATIONS FOR THE FLIGHT WHICH RESULTED IN A LOSS OF ENGINE POWER DUE TO FUEL EXHAUSTION. |
| Sep 28, 1995 | DODGE CITY, KS | N7660E | Incident | substantial | the pilot's improper use of the auxiliary fuel boost pump during descent which led to fuel flooding and loss of combustion. |