Cessna T210M Safety Record
Complete NTSB accident and incident history. 189 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Nov 02, 2014 | Jacksonville, OR | N1593M | Minor | substantial | A loss of engine power during cruise flight due to the failure of the No. 6 connecting rod, which resulted from oil starvation. |
| Jul 19, 2012 | Wells, NV | N6181N | Minor | substantial |
A loss of engine power during the final landing approach for reasons that could not be determined because postaccident examination did not reveal any …A loss of engine power during the final landing approach for reasons that could not be determined because postaccident examination did not reveal any malfunctions or failures that would have precluded normal operation. |
| Jan 28, 2012 | Clearwater, FL | N761HW | Minor | substantial |
The total loss of engine power due to fuel starvation for reasons that could not be determined because postaccident testing of the engine did not reve…The total loss of engine power due to fuel starvation for reasons that could not be determined because postaccident testing of the engine did not reveal any malfunctions or failures that would preclude normal operation. Contributing to the accident was the pilot’s improper in-flight fuel management following the loss of engine power. |
| Feb 24, 2011 | Independence, MO | N6149B | Minor | substantial |
Latent dimensional discrepancies related to the engine crankcase main bearing saddle bores, which precipitated the fatigue failure of the crankshaft a…Latent dimensional discrepancies related to the engine crankcase main bearing saddle bores, which precipitated the fatigue failure of the crankshaft and a complete loss of engine power. Contributing to the accident was the engine manufacturer's failure to properly identify and address the crankcase discrepancies when the engine was rebuilt. |
| Aug 13, 2010 | Put-in-Bay, OH | N14AW | Minor | substantial | A total loss of engine power while on final approach for undetermined reasons. |
| Sep 22, 2006 | Delta, UT | N732PC | Minor | substantial | A loss of engine power for an undetermined reason during cruise flight. |
| Feb 28, 2004 | Grape Creek, TX | N50MC | Minor | substantial |
The pilot's improper in-flight planning, which resulted in a loss of engine power due to fuel exhaustion. A factor was the lack of suitable terrain a…The pilot's improper in-flight planning, which resulted in a loss of engine power due to fuel exhaustion. A factor was the lack of suitable terrain available for the forced landing. |
| Jul 16, 2002 | Grass Valley, CA | N761HP | Minor | substantial |
The failure of the right main landing gear wheel, which resulted in the pilot's inability to maintain directional control during landing rollout. A f…The failure of the right main landing gear wheel, which resulted in the pilot's inability to maintain directional control during landing rollout. A factor in the accident was the failure of maintenance personnel to inspect the wheel in accordance with maintenance manual instructions. |
| Jul 28, 2001 | Spanish Fork, UT | N6798B | Minor | substantial |
the pilot's inadequate compensation for the wind conditions which resulted in a loss of control during landing. A contributing factor was the gusty c…the pilot's inadequate compensation for the wind conditions which resulted in a loss of control during landing. A contributing factor was the gusty crosswind. |
| Jul 15, 2001 | Marble Canyon, AZ | N732RC | Minor | substantial |
The pilot's failure to use all the available runway and his failure to follow the prescribed short field takeoff procedure resulting in a loss of cont…The pilot's failure to use all the available runway and his failure to follow the prescribed short field takeoff procedure resulting in a loss of control during the takeoff roll. Factors were the short, rough, and rising runway, and the soft dirt surrounding the runway. |
| Jun 16, 1998 | LA PINE, OR | N22CT | Minor | substantial | Fuel starvation for undetermined reasons. |
| Dec 21, 1996 | LEXINGTON, KY | N732UH | Minor | substantial |
failure of #5 exhaust valve and/or #5 exhaust valve guide, which resulted in a progressive engine failure (debris puncturing the #5 piston crown, exha…failure of #5 exhaust valve and/or #5 exhaust valve guide, which resulted in a progressive engine failure (debris puncturing the #5 piston crown, exhaust gasses entering the crankcase, loss of oil through the breather system, oil exhaustion, and subsequent damage to the engine bearings and connecting rods). Darkness and obstructions (vehicles) in the emergency landing area were related factors. |
| Dec 14, 1996 | CHARLOTTESVILLE, VA | N1929M | Minor | substantial |
The pilot's miscalculation of fuel consumption and his inadequate in-flight decision making, which resulted in fuel exhaustion and the loss of engine …The pilot's miscalculation of fuel consumption and his inadequate in-flight decision making, which resulted in fuel exhaustion and the loss of engine power. |
| Apr 26, 1996 | EL PASO, TX | N724YY | Minor | destroyed |
failure of the #2 cylinder connecting rod bolt due to oil starvation as a result of the shifting of the main bearing. A factor was the unsuitable terr…failure of the #2 cylinder connecting rod bolt due to oil starvation as a result of the shifting of the main bearing. A factor was the unsuitable terrain for the forced landing. |
| Jan 18, 1996 | LAS VEGAS, NM | N761KK | Minor | substantial | failure of the throttle cable. A factor relating to the accident was: the lack of suitable terrain for a forced landing. |
| Aug 17, 1990 | SODA SPRINGS, CA | N732VS | Minor | substantial |
ENGINE FAILURE DUE TO INADEQUATE VAPOR RECOVERY SYSTEM (INADEQUATE AIRCRAFT MAINTENANCE/SERVICE) AND INCORRECT FUEL GRADE. A FACTOR IN THE ACCIDENT WA…ENGINE FAILURE DUE TO INADEQUATE VAPOR RECOVERY SYSTEM (INADEQUATE AIRCRAFT MAINTENANCE/SERVICE) AND INCORRECT FUEL GRADE. A FACTOR IN THE ACCIDENT WAS UNSUITABLE TERRAIN. |
| Jul 07, 1990 | WHARTON, TX | N351WB | Minor | substantial | THE LOSS OF POWER DUE TO AN OUT-OF-RIG CONDITION IN THE AUTOMATIC AUXILIARY BOOST PUMP MECHANISM. |
| Oct 28, 1989 | PEACHTREE CITY, GA | N8444M | Minor | substantial |
THE IMPROPER CALIBRATION OF THE FUEL QUANTITY GAUGES BY MAINTENANCE PERSONNEL, WHICH RESULTED IN ERRONEOUS FUEL QUANTITY INDICATIONS AND LED TO FUEL S…THE IMPROPER CALIBRATION OF THE FUEL QUANTITY GAUGES BY MAINTENANCE PERSONNEL, WHICH RESULTED IN ERRONEOUS FUEL QUANTITY INDICATIONS AND LED TO FUEL STARVATION. CONTRIBUTING TO THE ACCIDENT WERE THE UNSUITABLE TERRAIN CONDITIONS THAT EXISTED AT THE FORCED-LANDING SITE. |
| Nov 08, 1988 | SHEPERDSVILLE, KY | N732WC | Minor | destroyed | Investigation pending |
| May 30, 1988 | LONG BEACH, CA | N6178N | Minor | substantial | Investigation pending |
| Jun 30, 1987 | TRACY, CA | N761JM | Minor | substantial | Investigation pending |
| Aug 22, 1986 | DILLON, MT | N6952M | Minor | substantial | Investigation pending |
| Apr 02, 1986 | HIGHLAND, MI | N732KR | Minor | substantial | Investigation pending |
| Dec 04, 1985 | HIGHLAND, MI | N1982M | Minor | substantial | Investigation pending |
| May 06, 1985 | MCKINNEY, TX | N732YR | Minor | substantial | Investigation pending |