Enstrom 280 Safety Record
Complete NTSB accident and incident history. 86 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Dec 28, 2025 | Hammonton, NJ | N280MG | Fatal (2) | substantial | Investigation pending |
| Mar 15, 2025 | Waterford, CA | N402TA | Serious (1) | destroyed | The pilot’s failure to maintain clearance from water while operating at a low altitude. |
| Jul 27, 2024 | Russellville, KY | N280D | Incident | substantial |
The flight instructor’s failure to maintain sufficient rotor rpm while maneuvering the helicopter low to the ground, which resulted in a loss of contr…The flight instructor’s failure to maintain sufficient rotor rpm while maneuvering the helicopter low to the ground, which resulted in a loss of control. |
| Feb 15, 2024 | Lewistown, MT | N899JS | Incident | substantial |
The pilot’s failure to maintain clearance from terrain. Contributing to the accident was the pilot’s encounter with low light conditions and snow-cove…The pilot’s failure to maintain clearance from terrain. Contributing to the accident was the pilot’s encounter with low light conditions and snow-covered terrain. |
| Dec 01, 2023 | Madrid, SP | F-HPUX | Incident | substantial | Investigation pending |
| Aug 25, 2021 | Llanfachreth, OF | G-OJBB | Incident | substantial | Investigation pending |
| Aug 21, 2021 | Port Orange, FL | N9285 | Incident | substantial | The failure of the tail rotor drive shaft at the coupling due to torsionally applied shear stress. |
| Jul 30, 2021 | Colchester, VT | N36DK | Serious (1) | destroyed |
An in-flight fire originating in the engine compartment near the turbocharger from a source that could not be determined, which resulted in a loss of …An in-flight fire originating in the engine compartment near the turbocharger from a source that could not be determined, which resulted in a loss of engine power and led to an autorotation and a hard landing. |
| Jul 04, 2020 | Des Moines, IA | N282SH | Minor | destroyed |
The partial loss of rotor and engine speed during approach for landing, which resulted in an autorotation and impact with terrain. The reason for the …The partial loss of rotor and engine speed during approach for landing, which resulted in an autorotation and impact with terrain. The reason for the partial loss of rotor and engine speed could not be determined based on the available evidence. Contributing to the accident was the pilot’s improper execution of the autorotation. |
| Jun 24, 2020 | Hayden, ID | N280MM | Fatal (1) | destroyed | The total loss of power while maneuvering at low altitude due to the detonation of two engine cylinders and damaged spark plugs. |
| Oct 25, 2019 | Jordan Valley, OR | N280F | Fatal (1) | substantial |
A partial loss of engine power due to a worn engine air induction hose, and a subsequent uncontrolled descent into terrain. Contributing to the accide…A partial loss of engine power due to a worn engine air induction hose, and a subsequent uncontrolled descent into terrain. Contributing to the accident was the failure of maintenance personnel to adequately inspect the hose, and the pilot’s decision to fly the helicopter at a speed and altitude that provided limited time to enter and establish an autorotation following the loss of power. |
| Jun 27, 2016 | Zeeland, MI | N518EG | Incident | minor | The exhaust band clamp failure, which resulted in an engine fire due to hot exhaust gases entering the engine compartment. |
| Jan 25, 2016 | Phoenix, AZ | N133AB | Minor | substantial |
A total loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any anomalies that…A total loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any anomalies that would have precluded normal operation. |
| Jan 22, 2016 | Buttwil, SZ | HB-XLS | Incident | substantial | Investigation pending |
| Dec 10, 2015 | Salinas Victoria, MX | XB-GRG | Incident | substantial | Investigation pending |
| Jan 26, 2015 | Erie, CO | N86235 | Fatal (2) | destroyed |
An in-flight failure of the helicopter's #2 main rotor spindle due to undetected fatigue cracking, which resulted in an in-flight breakup. Contributin…An in-flight failure of the helicopter's #2 main rotor spindle due to undetected fatigue cracking, which resulted in an in-flight breakup. Contributing to failure were the nonconforming thread root radius of the spindle and the manufacturer's failure to include a bending moment within the spindle threads when performing the fatigue analysis during initial design of the spindle. |
| Dec 08, 2014 | Fort Lupton, CO | N409LH | Minor | substantial | The loss of engine power during cruise flight for reasons that could not be determined based on the available information. |
| Apr 05, 2014 | Kirchham, Austria, AU | G-OJMF | Fatal (1) | destroyed | <br /><br /> |
| Oct 12, 2013 | Wolica Kozia, PL | SP-GMB | Fatal (2) | substantial | Investigation pending |
| Apr 03, 2012 | Corpus Christi, TX | N3042D | Minor | substantial | The failure of the bolt that retained the clutch drive rod end, which resulted in a loss of main rotor drive and a subsequent hard landing. |
| Sep 03, 2011 | Heber City, UT | N280AD | Serious (3) | substantial |
The pilot’s failure to ensure that there was sufficient fuel onboard to conduct the flight, which resulted in a loss of engine power due to fuel exhau…The pilot’s failure to ensure that there was sufficient fuel onboard to conduct the flight, which resulted in a loss of engine power due to fuel exhaustion. Contributing to the severity of the passengers’ injuries was the operator’s failure to provide adequate restraints for the passengers. |
| Mar 04, 2010 | Goshen, IN | N327TB | Serious (1) | substantial |
The inadequate preflight inspection by both pilots, resulting in a loss of engine power due to fuel exhaustion. Contributing to the accident was the d…The inadequate preflight inspection by both pilots, resulting in a loss of engine power due to fuel exhaustion. Contributing to the accident was the disconnected fuel tank sending unit. |
| Apr 20, 2009 | Dacono, CO | N409LH | Incident | substantial | A partial loss of engine power for undetermined reasons. |
| Mar 19, 2009 | Wendover, UT | N280AD | Incident | substantial |
A loss of engine power due to fuel exhaustion, which resulted from an inadequate preflight inspection by both pilots and their failure to ensure that …A loss of engine power due to fuel exhaustion, which resulted from an inadequate preflight inspection by both pilots and their failure to ensure that adequate fuel was on board for the flight. Contributing to the accident was the flight instructor's inadequate supervision of the flight. |
| Aug 06, 2008 | Aurora, CO | N285SH | Incident | substantial |
The pilot's improper planning and decision making resulting in the loss of engine power due to fuel exhaustion. Contributing to the accident was the p…The pilot's improper planning and decision making resulting in the loss of engine power due to fuel exhaustion. Contributing to the accident was the pilot's premature application of collective resulting in a hard landing and substantial damage. |