Cessna T210N Safety Record
Complete NTSB accident and incident history. 245 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jan 27, 2023 | Murrieta, CA | N4758C | Serious (1) | substantial |
A loss of engine power during the turn from base to final for undetermined reasons. Contributing to the accident was the pilot’s decision to not maint…A loss of engine power during the turn from base to final for undetermined reasons. Contributing to the accident was the pilot’s decision to not maintain traffic pattern altitude, which resulted in the off-airport landing. |
| Nov 19, 2015 | La Verne, CA | N91HC | Serious (1) | substantial | The total loss of engine power for reasons that could not be determined based on the available information. |
| Aug 05, 2011 | Amarillo, TX | N829MB | Serious (2) | substantial |
A loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any anomalies that would…A loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any anomalies that would have precluded normal operation. |
| Dec 31, 2006 | Albany, GA | N5093A | Serious (2) | substantial | The loss of engine power during cruise flight due to a fractured crankshaft, resulting in an off-airport forced landing in a muddy field. |
| May 29, 2006 | Santa Fe, NM | N7353C | Serious (1) | substantial |
the loss of engine power due to fuel exhaustion. Contributing factors were the pilot's inadequate preflight planning and failure to refuel the airpla…the loss of engine power due to fuel exhaustion. Contributing factors were the pilot's inadequate preflight planning and failure to refuel the airplane. |
| Apr 20, 2006 | Arkansas City, KS | N7617N | Serious (2) | destroyed | the pilot's failure to maintain clearance from the guide wire resulting in the airplane striking the wire and subsequently impacting the terrain. |
| Mar 22, 2005 | Carefree, AZ | N6897N | Serious (2) | substantial | the pilot's improper use of the fuel boost pump contrary to the procedures specified in the pilot owner handbook and other documents. |
| Sep 09, 2003 | Pine River, MN | N5360U | Serious (1) | substantial |
An inadequate pre-flight inspection by the pilot due to his failure to visually confirm fuel quantity prior to flight, and the resulting fuel exhausti…An inadequate pre-flight inspection by the pilot due to his failure to visually confirm fuel quantity prior to flight, and the resulting fuel exhaustion. Contributing factors were the pilot's improper use of the fuel management computer installed in the aircraft, and the tree located in the middle of the emergency landing field. |
| May 06, 2002 | Flagstaff, AZ | N888GB | Serious (1) | substantial | a loss of engine power for undetermined reasons. |
| Nov 24, 2000 | CHIHUAHUA, MX | N1963U | Serious (2) | substantial | Investigation pending |
| Nov 11, 2000 | Kankakee, IL | N9528Y | Serious (1) | substantial |
The unsuitable terrain encountered by the pilot during the emergency landing. Factors to the accident were the loss of engine power due to the failur…The unsuitable terrain encountered by the pilot during the emergency landing. Factors to the accident were the loss of engine power due to the failure of the crankshaft, the pilot misjudging the descent glide path, and the presence of the highway embankment during the landing roll. |
| Oct 29, 2000 | SANTA TERESA, NM | N5170Y | Serious (1) | substantial |
the pilot's failure to follow procedures/directives and lower the landing gear for landing. Contributing factors were the damaged propellers making i…the pilot's failure to follow procedures/directives and lower the landing gear for landing. Contributing factors were the damaged propellers making it impossible to perform a go-around, the inadvertent stall to the runway, and the pilot being in a state of fatigue. |
| Jun 12, 1999 | SENECA, SC | N6407N | Serious (1) | substantial |
The PIC's improper fuel management resulting in loss of engine power during approach to landing due to fuel starvation and the subsequent collision wi…The PIC's improper fuel management resulting in loss of engine power during approach to landing due to fuel starvation and the subsequent collision with trees and a residence during an emergency landing. Contributing to the accident was the PIC's failure to follow the airplane's inflight engine failure and before landing checklists. |
| May 29, 1999 | KALAMAZOO, MI | N9612Y | Serious | substantial |
the excessive airspeed, the proper touchdown point not obtained and the aborted landing not performed by the pilot. The fence and automobile were cont…the excessive airspeed, the proper touchdown point not obtained and the aborted landing not performed by the pilot. The fence and automobile were contributing factors. |
| Nov 30, 1996 | SCOTTSDALE, AZ | N4788C | Serious (5) | destroyed |
detonation/pre-ignition for unknown reason(s), which resulted in failure of the number two piston, loss of engine power, and a subsequent forced landi…detonation/pre-ignition for unknown reason(s), which resulted in failure of the number two piston, loss of engine power, and a subsequent forced landing on rough/uneven desert terrain. |
| Jan 12, 1996 | LOUISVILLE, KY | N5218A | Serious (1) | destroyed |
the pilot's misjudgment of the fuel supply, which resulted in a loss of engine power due to fuel exhaustion during final approach to the destination a…the pilot's misjudgment of the fuel supply, which resulted in a loss of engine power due to fuel exhaustion during final approach to the destination airport. Factors relating to the accident were: terrain conditions and vehicles in the emergency landing area. |
| Jun 11, 1995 | FALL RIVER MILL, CA | N5436Y | Serious (1) | destroyed | Fatigue failure of the No. 2 lower connecting rod bolt as a result of improper torque during the last engine overhaul. |
| Jun 16, 1989 | HERLONG, CA | N4857C | Serious (1) | substantial |
FUEL STARVATION, AFTER THE PILOT DIVERTED HIS ATTENTION TO AN ELECTRICAL PROBLEM, AND HIS FAILURE TO REPOSITION THE FUEL SELECTOR SWITCH, EITHER BEFOR…FUEL STARVATION, AFTER THE PILOT DIVERTED HIS ATTENTION TO AN ELECTRICAL PROBLEM, AND HIS FAILURE TO REPOSITION THE FUEL SELECTOR SWITCH, EITHER BEFORE THE ENGINE LOST POWER OR DURING EMERGENCY PROCEDURES. FACTORS RELATED TO THE ACCIDENT WERE: THE TRIPPED ALTERNATOR CIRCUIT BREAKER, AND HIGH OBSTRUCTIONS IN THE EMERGENCY LANDING AREA. |
| Feb 20, 1987 | WEST FARGO, ND | N9499Y | Serious (1) | substantial | Investigation pending |
| Nov 11, 1986 | BUCKEYE, AZ | N1625U | Serious (2) | substantial | Investigation pending |
| Mar 21, 1986 | PHOENIX, AZ | N5256A | Serious (1) | substantial | Investigation pending |
| Nov 11, 1985 | PADUCAH, KY | N9473Y | Serious (1) | substantial | Investigation pending |
| Nov 04, 1984 | SODDY DAISEY, TN | N64276 | Serious (1) | substantial | Investigation pending |
| Sep 26, 1984 | SAN AUGUSTINE, TX | N6399Y | Serious (2) | destroyed | Investigation pending |
| Aug 17, 1984 | CONE, AZ | N6462N | Serious (5) | substantial | Investigation pending |