Cessna 421B Safety Record
Complete NTSB accident and incident history. 104 events recorded from 1982 to 2022.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jun 22, 2017 | Carlsbad, CA | N380AL | Incident | substantial | The right main landing gear collapse for undetermined reasons. |
| Sep 29, 2012 | Selma, AL | N1537T | Incident | substantial |
The pilot’s improper fuel management, which resulted in a total loss of engine power on the right engine and a partial loss of engine power on the lef…The pilot’s improper fuel management, which resulted in a total loss of engine power on the right engine and a partial loss of engine power on the left engine due to fuel starvation. |
| Dec 09, 2011 | Pampa, TX | N421CE | Incident | substantial | The pilot's inadequate aircraft control during landing, which resulted in a hard landing. |
| May 02, 2011 | Truckee, CA | N270CS | Incident | — | Fatigue failure of the right flap extend cable during the landing approach. |
| Jun 04, 2010 | Anderson, IN | N421KB | Incident | substantial | The pilot’s failure to establish proper rotation and liftoff speed during the takeoff roll. |
| Mar 18, 2010 | Artesia, NM | N3382Q | Incident | substantial | A loss of engine power due to fuel starvation as a result of the pilot's improper fuel management. |
| Oct 03, 2009 | San Simeon, CA | N31KT | Incident | substantial | The pilot's failure to follow the manufacturer’s checklist and set the parking brake. |
| Aug 08, 2007 | Oceanside, CA | N968J | Incident | substantial |
The collapse of the right main landing gear during the landing roll for undetermined reason, which resulted in a loss of directional control and colli…The collapse of the right main landing gear during the landing roll for undetermined reason, which resulted in a loss of directional control and collision with a fence. |
| Jul 07, 2005 | Medina, OH | N318RF | Incident | substantial | An overload failure of the left main landing gear attachment assembly. |
| Apr 04, 2005 | Lake Havasu Cit, AZ | N637SC | Incident | substantial | the fracture of the landing gear shaft roll pin that resulted in a main gear collapse during the taxi. |
| Jul 02, 2004 | Portland, ME | N421KS | Incident | substantial | Failure of the right main landing gear down-lock mechanism resulting in the collapse of the right main landing gear. |
| Jun 16, 2004 | Bend, OR | N332CC | Incident | substantial |
On ground encounter with terrain during the takeoff roll as a result of the left side brake not operating. Inadequate maintenance inspection, overloa…On ground encounter with terrain during the takeoff roll as a result of the left side brake not operating. Inadequate maintenance inspection, overload of the nose landing gear and soft terrain were factors. |
| Sep 20, 2003 | Driggs, ID | N41053 | Incident | substantial | The collapse of the nose landing gear while taxiing due to the failure of the nose wheel bearing. A factor was the lack of lubrication. |
| Sep 28, 2002 | Mineral Wells, TX | N7926R | Incident | substantial | The pilot's failure to maintain a proper descent rate which resulted hard landing and a subsequent failure of the main landing gear. |
| Aug 17, 2001 | New Braunfels, TX | N5286Z | Incident | substantial | the pilot's inadequate flare of the airplane resulting in a hard landing. A contributing factor was the crosswind. |
| Dec 14, 2000 | PENSACOLA, FL | N781SL | Incident | substantial |
The failure of the left main landing gear scissors washer during taxi for takeoff, and collapse of the left main landing gear. A factor in the acciden…The failure of the left main landing gear scissors washer during taxi for takeoff, and collapse of the left main landing gear. A factor in the accident was the failure of unknown maintenance personnel to comply with a manufacturers service letter concerning the scissors washers. |
| Oct 05, 1999 | MONTAGUE, CA | N69GP | Incident | substantial |
The collapse of the left main landing gear during the landing rollout for undetermined reasons, which resulted in the pilot's loss of directional cont…The collapse of the left main landing gear during the landing rollout for undetermined reasons, which resulted in the pilot's loss of directional control. |
| Jan 15, 1999 | YOUNGSTOWN, OH | N882BB | Incident | substantial | The pilot's failure to maintain aircraft control. A factor was the icy runway. |
| Mar 18, 1998 | SHOW LOW, AZ | N70PD | Incident | substantial | The pilot's failure to attain the proper alignment on the runway due to the obscuration by snow of the runway and on the airplane's windows. |
| Nov 19, 1996 | OLYMPIA, WA | N8005Q | Incident | substantial |
inoperative deicing equipment, due to multiple wing boot holes and malfunctioning control/shuttle valves; subsequent build-up of airframe (wing) ice; …inoperative deicing equipment, due to multiple wing boot holes and malfunctioning control/shuttle valves; subsequent build-up of airframe (wing) ice; and failure of the pilot to maintain adequate airspeed during the flare for landing. Factors relating to the accident included: the adverse weather (icing) conditions, and inadequate maintenance concerning the deicing equipment. |
| Jul 02, 1996 | STILLWATER, OK | N450SU | Incident | substantial |
the failure of the pilots of the Cessna 421B, N450SU, and the Cessna 152, N94532, to maintain visual lookout. Factors were: the inadequate radio commu…the failure of the pilots of the Cessna 421B, N450SU, and the Cessna 152, N94532, to maintain visual lookout. Factors were: the inadequate radio communications maintained by both pilots, and the failure of the student pilot of the Cessna 152 to take evasive action. |
| Sep 07, 1995 | ALBUQUERQUE, NM | N5368J | Incident | substantial | THE PILOT'S INADEQUATE COMPENSATION FOR THE CROSSWIND CONDITION. A FACTOR WAS THE CROSSWIND. |
| Oct 03, 1994 | STUART, FL | N701AM | Incident | substantial |
THE IMPROPER RIGGING OF THE LANDING GEAR SAFETY SQUAT SWITCH BY OTHER MAINTENANCE PERSONNEL. CONTRIBUTING TO THE ACCIDENT WAS THE CONTAMINATION OF THE…THE IMPROPER RIGGING OF THE LANDING GEAR SAFETY SQUAT SWITCH BY OTHER MAINTENANCE PERSONNEL. CONTRIBUTING TO THE ACCIDENT WAS THE CONTAMINATION OF THE GEAR SQUAT SWITCH WITH CORROSION AND WATER. |
| Feb 28, 1994 | LAGRANGE, GA | N421HA | Incident | minor |
THE PILOT'S INTENTIONAL SWERVE OFF THE TAXIWAY TO AVOID A GROUND COLLISION. A FACTOR IN THE INCIDENT WAS AN UNDETERMINED MALFUNCTION OF THE AIRPLANE'S…THE PILOT'S INTENTIONAL SWERVE OFF THE TAXIWAY TO AVOID A GROUND COLLISION. A FACTOR IN THE INCIDENT WAS AN UNDETERMINED MALFUNCTION OF THE AIRPLANE'S NORMAL BRAKE SYSTEM. |
| Jun 10, 1993 | ATTALLA, AL | N699DT | Incident | destroyed | THE FAILURE OF THE LEFT ENGINE TURBOCHARGER DUE TO ROTOR SHAFT SEIZURE, WHICH RESULTED IN A LOSS OF ENGINE POWER. |