Cessna 421B Safety Record

Complete NTSB accident and incident history. 104 events recorded from 1982 to 2022.

104

All Events

52

Incidents

10

Minor

11

Serious

31

Fatal (96 fatalities)

Date Location Reg# Severity Damage Probable Cause
Jun 22, 2017 Carlsbad, CA N380AL Incident substantial The right main landing gear collapse for undetermined reasons.
Sep 29, 2012 Selma, AL N1537T Incident substantial
The pilot’s improper fuel management, which resulted in a total loss of engine power on the right engine and a partial loss of engine power on the lef…

The pilot’s improper fuel management, which resulted in a total loss of engine power on the right engine and a partial loss of engine power on the left engine due to fuel starvation.

Dec 09, 2011 Pampa, TX N421CE Incident substantial The pilot's inadequate aircraft control during landing, which resulted in a hard landing.
May 02, 2011 Truckee, CA N270CS Incident Fatigue failure of the right flap extend cable during the landing approach.
Jun 04, 2010 Anderson, IN N421KB Incident substantial The pilot’s failure to establish proper rotation and liftoff speed during the takeoff roll.
Mar 18, 2010 Artesia, NM N3382Q Incident substantial A loss of engine power due to fuel starvation as a result of the pilot's improper fuel management.
Oct 03, 2009 San Simeon, CA N31KT Incident substantial The pilot's failure to follow the manufacturer’s checklist and set the parking brake.
Aug 08, 2007 Oceanside, CA N968J Incident substantial
The collapse of the right main landing gear during the landing roll for undetermined reason, which resulted in a loss of directional control and colli…

The collapse of the right main landing gear during the landing roll for undetermined reason, which resulted in a loss of directional control and collision with a fence.

Jul 07, 2005 Medina, OH N318RF Incident substantial An overload failure of the left main landing gear attachment assembly.
Apr 04, 2005 Lake Havasu Cit, AZ N637SC Incident substantial the fracture of the landing gear shaft roll pin that resulted in a main gear collapse during the taxi.
Jul 02, 2004 Portland, ME N421KS Incident substantial Failure of the right main landing gear down-lock mechanism resulting in the collapse of the right main landing gear.
Jun 16, 2004 Bend, OR N332CC Incident substantial
On ground encounter with terrain during the takeoff roll as a result of the left side brake not operating. Inadequate maintenance inspection, overloa…

On ground encounter with terrain during the takeoff roll as a result of the left side brake not operating. Inadequate maintenance inspection, overload of the nose landing gear and soft terrain were factors.

Sep 20, 2003 Driggs, ID N41053 Incident substantial The collapse of the nose landing gear while taxiing due to the failure of the nose wheel bearing. A factor was the lack of lubrication.
Sep 28, 2002 Mineral Wells, TX N7926R Incident substantial The pilot's failure to maintain a proper descent rate which resulted hard landing and a subsequent failure of the main landing gear.
Aug 17, 2001 New Braunfels, TX N5286Z Incident substantial the pilot's inadequate flare of the airplane resulting in a hard landing. A contributing factor was the crosswind.
Dec 14, 2000 PENSACOLA, FL N781SL Incident substantial
The failure of the left main landing gear scissors washer during taxi for takeoff, and collapse of the left main landing gear. A factor in the acciden…

The failure of the left main landing gear scissors washer during taxi for takeoff, and collapse of the left main landing gear. A factor in the accident was the failure of unknown maintenance personnel to comply with a manufacturers service letter concerning the scissors washers.

Oct 05, 1999 MONTAGUE, CA N69GP Incident substantial
The collapse of the left main landing gear during the landing rollout for undetermined reasons, which resulted in the pilot's loss of directional cont…

The collapse of the left main landing gear during the landing rollout for undetermined reasons, which resulted in the pilot's loss of directional control.

Jan 15, 1999 YOUNGSTOWN, OH N882BB Incident substantial The pilot's failure to maintain aircraft control. A factor was the icy runway.
Mar 18, 1998 SHOW LOW, AZ N70PD Incident substantial The pilot's failure to attain the proper alignment on the runway due to the obscuration by snow of the runway and on the airplane's windows.
Nov 19, 1996 OLYMPIA, WA N8005Q Incident substantial
inoperative deicing equipment, due to multiple wing boot holes and malfunctioning control/shuttle valves; subsequent build-up of airframe (wing) ice; …

inoperative deicing equipment, due to multiple wing boot holes and malfunctioning control/shuttle valves; subsequent build-up of airframe (wing) ice; and failure of the pilot to maintain adequate airspeed during the flare for landing. Factors relating to the accident included: the adverse weather (icing) conditions, and inadequate maintenance concerning the deicing equipment.

Jul 02, 1996 STILLWATER, OK N450SU Incident substantial
the failure of the pilots of the Cessna 421B, N450SU, and the Cessna 152, N94532, to maintain visual lookout. Factors were: the inadequate radio commu…

the failure of the pilots of the Cessna 421B, N450SU, and the Cessna 152, N94532, to maintain visual lookout. Factors were: the inadequate radio communications maintained by both pilots, and the failure of the student pilot of the Cessna 152 to take evasive action.

Sep 07, 1995 ALBUQUERQUE, NM N5368J Incident substantial THE PILOT'S INADEQUATE COMPENSATION FOR THE CROSSWIND CONDITION. A FACTOR WAS THE CROSSWIND.
Oct 03, 1994 STUART, FL N701AM Incident substantial
THE IMPROPER RIGGING OF THE LANDING GEAR SAFETY SQUAT SWITCH BY OTHER MAINTENANCE PERSONNEL. CONTRIBUTING TO THE ACCIDENT WAS THE CONTAMINATION OF THE…

THE IMPROPER RIGGING OF THE LANDING GEAR SAFETY SQUAT SWITCH BY OTHER MAINTENANCE PERSONNEL. CONTRIBUTING TO THE ACCIDENT WAS THE CONTAMINATION OF THE GEAR SQUAT SWITCH WITH CORROSION AND WATER.

Feb 28, 1994 LAGRANGE, GA N421HA Incident minor
THE PILOT'S INTENTIONAL SWERVE OFF THE TAXIWAY TO AVOID A GROUND COLLISION. A FACTOR IN THE INCIDENT WAS AN UNDETERMINED MALFUNCTION OF THE AIRPLANE'S…

THE PILOT'S INTENTIONAL SWERVE OFF THE TAXIWAY TO AVOID A GROUND COLLISION. A FACTOR IN THE INCIDENT WAS AN UNDETERMINED MALFUNCTION OF THE AIRPLANE'S NORMAL BRAKE SYSTEM.

Jun 10, 1993 ATTALLA, AL N699DT Incident destroyed THE FAILURE OF THE LEFT ENGINE TURBOCHARGER DUE TO ROTOR SHAFT SEIZURE, WHICH RESULTED IN A LOSS OF ENGINE POWER.
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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