Cessna 402C Safety Record
Complete NTSB accident and incident history. 106 events recorded from 1982 to 2021.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jun 30, 2000 | NAPLES, FL | N7037E | Incident | substantial | an inflight collision with a bird during descent that resulted in substantial damage to the airplane's vertical stabilizer spar. |
| May 22, 2000 | CORDOVA, AK | N402ET | Incident | substantial | An in-flight collision with a bird. |
| Mar 16, 2000 | SAN ANTONIO, TX | N11NX | Incident | substantial |
The pilot's inadequate handling of the aircraft during the landing flare/touchdown resulting in a hard landing that collapsed the left main landing ge…The pilot's inadequate handling of the aircraft during the landing flare/touchdown resulting in a hard landing that collapsed the left main landing gear. |
| Jun 08, 1999 | FORT LAUDERDALE, FL | N440AB | Incident | substantial |
The pilot's decision takeoff with condensation on the cockpit windows which restricted visibility, his improper use of aileron control, improper compe…The pilot's decision takeoff with condensation on the cockpit windows which restricted visibility, his improper use of aileron control, improper compensation for winds during takeoff, and his failure to maintain directional control during takeoff, resulting in the aircraft running off the left side of the runway, colliding with a taxiway sign and ditch, and collapsing the landing gear. |
| Sep 19, 1997 | NANTUCKET, MA | N6879Y | Incident | substantial |
the pilot's delayed decision to perform a go-around (missed approach). Related factors were: darkness, low ceiling, fog, and disorientation of the fl…the pilot's delayed decision to perform a go-around (missed approach). Related factors were: darkness, low ceiling, fog, and disorientation of the flight crew, while making the approach in conditions of limited visibility. |
| Sep 15, 1997 | KIVALINA, AK | N2649Z | Incident | substantial | An overstress fracture of the nose landing gear attachment. A factor associated with the accident was the rough landing area. |
| Sep 08, 1997 | BUCKLAND, AK | N2649Z | Incident | substantial | The failure of the pilot of the Cessna 402C, N2649Z, to maintain adequate clearance while taxiing alongside the stationary Cessna 208B, N1123R. |
| Jan 25, 1997 | PROVINCETOWN, MA | N121PB | Incident | minor |
the pilot's inadequate inflight planning/decision, and his misjudgment of speed and distance. Related factors were: fog, tailwind, and soft terrain o…the pilot's inadequate inflight planning/decision, and his misjudgment of speed and distance. Related factors were: fog, tailwind, and soft terrain on the overrun area at the end of the runway. |
| Apr 11, 1996 | ST JOHNS, AZ | N172VB | Incident | substantial |
the pilot's inadequate compensation for the wind conditions, his use of an overly excessive approach speed, and his misjudged distance/altitude relati…the pilot's inadequate compensation for the wind conditions, his use of an overly excessive approach speed, and his misjudged distance/altitude relationship to the runway. The wind was a factor. |
| Jun 27, 1995 | CONGO TOWN, CF | N60LC | Incident | substantial | Investigation pending |
| Nov 01, 1994 | FORT LAUDERDALE, FL | N5715C | Incident | substantial |
The failure of the left main landing gear upper barrel and trunion assembly due to overstress separations, resulting in the collapse of the left main …The failure of the left main landing gear upper barrel and trunion assembly due to overstress separations, resulting in the collapse of the left main landing gear on landing rollout. |
| Sep 26, 1994 | FT. LAUDERDALE, FL | N63PB | Incident | minor |
The first officer's failure to maintain directional control on landing roll out due to improper use of brakes, resulting in the airplane veering off t…The first officer's failure to maintain directional control on landing roll out due to improper use of brakes, resulting in the airplane veering off the runway, and subsequent on-ground collision with a runway light and sign. Contributing to the incident was the failure of the return spring in the right master brake cylinder, and the failure of the first officer to relinquish the flight controls when requested by the pilot-in- command. |
| Jul 24, 1994 | ST. PETERSBURG, FL | N318AB | Incident | minor | COLLAPSE OF THE RIGHT MAIN LANDING GEAR DURING THE LANDING ROLL FOR UNDETERMINED REASONS. |
| Feb 12, 1994 | GRAND CANYON, AZ | N26514 | Incident | substantial |
THE FAILURE OF THE OTHER AIRCRAFT'S LEFT BRAKE SYSTEM DUE TO A WORN MASTER CYLINDER, AND THE FAILURE OF THE OTHER PILOT TO TAXI AT A SPEED AND SPACING…THE FAILURE OF THE OTHER AIRCRAFT'S LEFT BRAKE SYSTEM DUE TO A WORN MASTER CYLINDER, AND THE FAILURE OF THE OTHER PILOT TO TAXI AT A SPEED AND SPACING INTERVAL WHICH WOULD ALLOW FOR SUCCESSFUL REMEDIAL ACTION. |
| Feb 07, 1994 | BILLINGS, MT | N2718Y | Incident | substantial | THE NOSE GEAR ACTUATOR FROZE. A FACTOR TO THE ACCIDENT WAS TEMPERATURE EXTREMES. |
| Feb 20, 1993 | NOME, AK | N4182G | Incident | destroyed | THE PILOT IN COMMAND NOT REMOVING THE ICE FROM THE PLANE'S AIRFOIL SURFACES BEFORE TAKEOFF. THE WEATHER CONDITION WAS A FACTOR. |
| Mar 18, 1992 | MIAMI, FL | N69SC | Incident | minor | THE TOTAL FAILURE OF THE MAIN LANDING GEAR UPLOCK AND SEQUENCING VALVE FOR UNDETERMINED REASONS. |
| Mar 01, 1992 | FORT LAUDERDALE, FL | N6786C | Incident | minor | IMPROPER OVERHAUL BY COMPANY MAINTENANCE PERSONNEL AND INACCURATE GEAR DOWN AND LOCKED INDICATION IN THE COCKPIT. |
| Aug 09, 1991 | GRAND CANYON, AZ | N161TA | Incident | substantial | THE FAILURE OF THE AIRPORT OPERATOR TO DEVELOP ANIMAL CONTROL PROCEDURES FOR THE AIRPORT PROPERTY. |
| Dec 31, 1990 | MARATHON, FL | N155PB | Incident | minor |
FATIGUE FAILURE OF A NOSE LANDING GEAR DRAG BRACE ASSEMBLY WHICH CAUSED THE NOSE LANDING GEAR TO COLLAPSE DURING THE LANDING ROLL. CONTRIBUTING TO THE…FATIGUE FAILURE OF A NOSE LANDING GEAR DRAG BRACE ASSEMBLY WHICH CAUSED THE NOSE LANDING GEAR TO COLLAPSE DURING THE LANDING ROLL. CONTRIBUTING TO THE ACCIDENT WAS AN INADEQUATE INSPECTION OF THE AIRPLANE APPROXIMATELY 7 HOURS EARLIER BY COMPANY MAINTENANCE PERSONNEL. |
| Aug 12, 1989 | FORT LAUDERDALE, FL | N5851C | Incident | substantial |
THE FAILURE OF THE PILOT TO POSITION THE AUXILIARY PUMP TO LOW FOR TAKEOFF, COMPUNDED BY IMPROPER PROCUDERES USED DURING THE RESULTANT IN-FLIGHT EMERG…THE FAILURE OF THE PILOT TO POSITION THE AUXILIARY PUMP TO LOW FOR TAKEOFF, COMPUNDED BY IMPROPER PROCUDERES USED DURING THE RESULTANT IN-FLIGHT EMERGENCY. |
| Aug 25, 1988 | PRESCOTT, AZ | N5715C | Incident | substantial | Investigation pending |
| May 16, 1988 | MANGROVE CAY, BF | C6503 | Incident | substantial | Investigation pending |
| Feb 02, 1988 | PROVINCETOWN, MA | N29PB | Incident | substantial | Investigation pending |
| Jan 18, 1988 | PRESCOTT, AZ | N6842Q | Incident | substantial | Investigation pending |