Cessna 210L Safety Record
Complete NTSB accident and incident history. 136 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jul 11, 2017 | Wilkes-Barre/Scranton, PA | N732FJ | Incident | substantial | Failure of the left landing gear door actuator, which resulted in a loss of all hydraulic pressure and subsequent gear collapse on landing. |
| Mar 19, 2016 | Myrtle Beach, SC | N59196 | Incident | substantial |
A complete loss of electrical power, which resulted from the separation of an alternator wire due to corrosion. Contributing to the accident was the f…A complete loss of electrical power, which resulted from the separation of an alternator wire due to corrosion. Contributing to the accident was the failure of the emergency landing gear extension system due to a lack of hydraulic fluid, which resulted in insufficient pressure to extend the landing gear. |
| Aug 13, 2011 | Seattle, WA | N732FY | Incident | substantial | A loss of electrical power while on final approach due to a depleted battery, which resulted in an intentional gear-up emergency landing. |
| Jun 09, 2010 | Tampa, FL | N2263S | Incident | substantial |
The total loss of engine power due to inadequate torgue on the crankcase bolts. Contributing to the accident was the inadequate inspection performed 1…The total loss of engine power due to inadequate torgue on the crankcase bolts. Contributing to the accident was the inadequate inspection performed 19.5 hours prior to the accident. |
| Feb 18, 2010 | Aurora, OR | N777FW | Incident | substantial |
The failure of the landing gear to properly function for undetermined reasons, resulting in the right main landing gear collapsing during landing. Co…The failure of the landing gear to properly function for undetermined reasons, resulting in the right main landing gear collapsing during landing. Contributing to the accident was the pilot's failure to follow the emergency gear extension procedure. |
| Feb 27, 2008 | Tampa, FL | N5489V | Incident | substantial | The malfunction of the right main landing gear down-and-locked switch. |
| Nov 16, 2007 | Santa Barbara, CA | N987M | Incident | substantial |
The left main landing gear's down limit switch plunger being bent and stuck in the closed position, which resulted in the collapse of the landing gear…The left main landing gear's down limit switch plunger being bent and stuck in the closed position, which resulted in the collapse of the landing gear during the landing roll. The reason for the down limit switch plunger being bent could not be determined. |
| Aug 25, 2007 | Cottage Grove, OR | N75032 | Incident | substantial | The loss of engine power for an undetermined reason. A contributing factor was the lack of suitable terrain for the forced landing. |
| Oct 26, 2005 | BAKER, LA | N59051 | Incident | substantial | The pilot's failure to maintain clearance during takeoff roll. |
| May 25, 2005 | Harvey, LA | N5120Q | Incident | substantial | The loss of engine power for undetermined reasons. A contributing factor was the lack of suitable terrain for the forced landing. |
| May 15, 2005 | Houston, TX | N1766X | Incident | substantial | The pilot's failure to maintain directional control during landing roll. A contributing factor was reported partial loss of brake control. |
| Mar 08, 2005 | Oxnard, CA | N2044S | Incident | substantial |
A pinhole leak in the fuel pressure line during the takeoff roll that was ignited by an electrical arc associated with wires adjacent to the fuel line…A pinhole leak in the fuel pressure line during the takeoff roll that was ignited by an electrical arc associated with wires adjacent to the fuel line. A contributing factor in the accident was the failure of maintenance personnel to comply with a manufacturer's service bulletin that addressed potential damage to the fuel line. |
| Jan 14, 2004 | Fort Meade, FL | N453MC | Incident | substantial |
The failure of the pilot to abort the takeoff after encountering fog during the preflight and engine run-up, and also his failure to maintain proper a…The failure of the pilot to abort the takeoff after encountering fog during the preflight and engine run-up, and also his failure to maintain proper alignment with the runway during the takeoff roll due to a fogged windshield resulting in the collision with a fence. |
| Oct 07, 2003 | Tallahassee, FL | N59063 | Incident | substantial | Loss of engine power due to crankshaft counterweight failure. |
| Feb 04, 2003 | Morrilton, AR | N22432 | Incident | substantial | The failure of the main landing gear to extend and lock, as a result of a hydraulic fluid leak caused by a chaffed and ruptured flex line. |
| Aug 30, 2002 | Georgetown, SC | N32W | Incident | substantial | The failure of the landing gear to lock in the down position. |
| Aug 10, 2002 | Lacon, IL | N3UF | Incident | substantial |
The pilot's improper in-flight decision to perform an intentional gear-up precautionary landing instead of continuing to the next available airport. …The pilot's improper in-flight decision to perform an intentional gear-up precautionary landing instead of continuing to the next available airport. A factor to the accident was the corn crop. |
| Jul 30, 2002 | Cascade, ID | N732EK | Incident | substantial |
The pilot's failure to maintain the proper rate of descent on short final resulting in a touchdown short of the runway threshold. Contributing factor…The pilot's failure to maintain the proper rate of descent on short final resulting in a touchdown short of the runway threshold. Contributing factors were the variable winds and swampy terrain at the touchdown site. |
| Feb 27, 2002 | Atlanta, GA | N115CW | Incident | substantial |
The pilot's failure to obtain the proper touchdown point and excessive airspeed on landing resulting in the airplane going off the end of the runway, …The pilot's failure to obtain the proper touchdown point and excessive airspeed on landing resulting in the airplane going off the end of the runway, on-ground collision with an embankment, and subsequent nose over. |
| Jan 09, 2002 | Great Falls, MT | N1713X | Incident | substantial |
The pilot's intentional continuation of a visual flight rules (VFR) flight into instrument meteorological conditions (IMC), and his failure to mainta…The pilot's intentional continuation of a visual flight rules (VFR) flight into instrument meteorological conditions (IMC), and his failure to maintain clearance from the terrain. Factors include low ceilings, snow, mountainous/hilly terrain, and trees. |
| Aug 13, 2001 | Bluefield, WV | N732JT | Incident | minor |
Improper maintenance which resulted in the installation of an unserviceable piston assembly, and the subsequent catastrophic engine failure. Factors …Improper maintenance which resulted in the installation of an unserviceable piston assembly, and the subsequent catastrophic engine failure. Factors in this accident were the improper inspection by the piston supplier and the softening of the piston. |
| Dec 04, 1999 | COLUMBUS, OH | N1773X | Incident | substantial |
The pilot's failure to verify landing gear extension. Factors were the unreliable retraction/extension assembly, and the flying club's continued oper…The pilot's failure to verify landing gear extension. Factors were the unreliable retraction/extension assembly, and the flying club's continued operation of the airplane with known deficiencies in the equipment. |
| Oct 01, 1999 | FAYETTEVILLE, AR | N2157S | Incident | substantial |
The cause of the right main gear collapse was undetermined. A factor was the failure of the gear 'down & locked' switch resulting in a false 'down & …The cause of the right main gear collapse was undetermined. A factor was the failure of the gear 'down & locked' switch resulting in a false 'down & locked' indication in the cockpit. |
| Jun 11, 1999 | GT. HARBOUR CAY, BF | N1765X | Incident | destroyed | Investigation pending |
| Sep 26, 1998 | ORLANDO, FL | N300EW | Incident | substantial |
A 6-8 inch crack on the right main landing gear strut, which allowed the hydraulic fluid to escape from the system, along with a power pack sequencing…A 6-8 inch crack on the right main landing gear strut, which allowed the hydraulic fluid to escape from the system, along with a power pack sequencing valve failure which allowed the main landing gear to fold on landing. A factor in the accident was the pilots execution of a night landing without her prescribed eye glasses. |