Cessna 210L Safety Record
Complete NTSB accident and incident history. 136 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jul 29, 2025 | Turks and Caicos Islands, OF | N1110S | Incident | substantial | Investigation pending |
| Apr 03, 2025 | Raceland, LA | N1574P | Fatal (2) | destroyed | Investigation pending |
| Jun 16, 2023 | Groote Eylandt, AS | VH-FTM | Serious (3) | substantial | Investigation pending |
| Dec 21, 2020 | Midway, GA | N2246S | Fatal (1) | substantial |
The pilot's intentional visual flight rules flight into instrument meteorological conditions, which resulted in controlled flight into terrain. Contri…The pilot's intentional visual flight rules flight into instrument meteorological conditions, which resulted in controlled flight into terrain. Contributing to the accident was the pressure to complete the flight to work in an emergency room. |
| Jul 11, 2017 | Wilkes-Barre/Scranton, PA | N732FJ | Incident | substantial | Failure of the left landing gear door actuator, which resulted in a loss of all hydraulic pressure and subsequent gear collapse on landing. |
| Mar 19, 2016 | Myrtle Beach, SC | N59196 | Incident | substantial |
A complete loss of electrical power, which resulted from the separation of an alternator wire due to corrosion. Contributing to the accident was the f…A complete loss of electrical power, which resulted from the separation of an alternator wire due to corrosion. Contributing to the accident was the failure of the emergency landing gear extension system due to a lack of hydraulic fluid, which resulted in insufficient pressure to extend the landing gear. |
| Apr 11, 2015 | Assuncao do Piaui, BR | PR-APG | Fatal (1) | destroyed | Investigation pending |
| Jul 03, 2014 | Las Vegas, NM | N1175Q | Serious (1) | substantial |
The pilot's loss of airplane control during an aborted landing. Contributing to the accident was the pilot's inadequate preflight planning, which resu…The pilot's loss of airplane control during an aborted landing. Contributing to the accident was the pilot's inadequate preflight planning, which resulted in his attempt to land on a runway closed by a notice to airmen and the loss of engine power due to fuel exhaustion. |
| Feb 15, 2014 | Clay, AL | N732EJ | Fatal (2) | destroyed |
The pilot's failure to maintain control of the airplane while being vectored to intercept the localizer during night instrument meteorological conditi…The pilot's failure to maintain control of the airplane while being vectored to intercept the localizer during night instrument meteorological conditions (IMC). Contributing to the accident was the operator's inadequate dispatch procedures, which did not prevent the pilot from flying beyond his duty day, flying at night for which he was not current, or flying in IMC for which he was not qualified by the company. |
| Nov 28, 2013 | Montrose, PA | N777BK | Minor | substantial | The pilot’s failure to check the fuel tanks for contaminants after fueling, which resulted in a total loss of engine power due to water contamination. |
| Apr 26, 2013 | Belem, BR | PR-LJI | Fatal (2) | substantial | Investigation pending |
| Nov 09, 2012 | La Grange, TX | N732BL | Minor | substantial |
The total loss of engine power due to the loss of oil to the engine. Contributing to the accident was maintenance personnel’s improper installation of…The total loss of engine power due to the loss of oil to the engine. Contributing to the accident was maintenance personnel’s improper installation of the engine oil filter adaptor, which resulted in the loss of oil to the engine. |
| Aug 13, 2011 | Seattle, WA | N732FY | Incident | substantial | A loss of electrical power while on final approach due to a depleted battery, which resulted in an intentional gear-up emergency landing. |
| Jun 09, 2010 | Tampa, FL | N2263S | Incident | substantial |
The total loss of engine power due to inadequate torgue on the crankcase bolts. Contributing to the accident was the inadequate inspection performed 1…The total loss of engine power due to inadequate torgue on the crankcase bolts. Contributing to the accident was the inadequate inspection performed 19.5 hours prior to the accident. |
| Feb 18, 2010 | Aurora, OR | N777FW | Incident | substantial |
The failure of the landing gear to properly function for undetermined reasons, resulting in the right main landing gear collapsing during landing. Co…The failure of the landing gear to properly function for undetermined reasons, resulting in the right main landing gear collapsing during landing. Contributing to the accident was the pilot's failure to follow the emergency gear extension procedure. |
| May 15, 2008 | Abingdon Downs, AS | VH-IDM | Fatal (1) | substantial | Investigation pending |
| Feb 27, 2008 | Tampa, FL | N5489V | Incident | substantial | The malfunction of the right main landing gear down-and-locked switch. |
| Nov 16, 2007 | Santa Barbara, CA | N987M | Incident | substantial |
The left main landing gear's down limit switch plunger being bent and stuck in the closed position, which resulted in the collapse of the landing gear…The left main landing gear's down limit switch plunger being bent and stuck in the closed position, which resulted in the collapse of the landing gear during the landing roll. The reason for the down limit switch plunger being bent could not be determined. |
| Aug 25, 2007 | Cottage Grove, OR | N75032 | Incident | substantial | The loss of engine power for an undetermined reason. A contributing factor was the lack of suitable terrain for the forced landing. |
| Oct 26, 2005 | BAKER, LA | N59051 | Incident | substantial | The pilot's failure to maintain clearance during takeoff roll. |
| May 25, 2005 | Harvey, LA | N5120Q | Incident | substantial | The loss of engine power for undetermined reasons. A contributing factor was the lack of suitable terrain for the forced landing. |
| May 15, 2005 | Houston, TX | N1766X | Incident | substantial | The pilot's failure to maintain directional control during landing roll. A contributing factor was reported partial loss of brake control. |
| Mar 08, 2005 | Oxnard, CA | N2044S | Incident | substantial |
A pinhole leak in the fuel pressure line during the takeoff roll that was ignited by an electrical arc associated with wires adjacent to the fuel line…A pinhole leak in the fuel pressure line during the takeoff roll that was ignited by an electrical arc associated with wires adjacent to the fuel line. A contributing factor in the accident was the failure of maintenance personnel to comply with a manufacturer's service bulletin that addressed potential damage to the fuel line. |
| Jan 14, 2004 | Fort Meade, FL | N453MC | Incident | substantial |
The failure of the pilot to abort the takeoff after encountering fog during the preflight and engine run-up, and also his failure to maintain proper a…The failure of the pilot to abort the takeoff after encountering fog during the preflight and engine run-up, and also his failure to maintain proper alignment with the runway during the takeoff roll due to a fogged windshield resulting in the collision with a fence. |
| Oct 13, 2003 | Hickory, NC | N732AG | Minor | substantial | The pilot's failure to maintain airspeed which resulted in a stall. |