Cessna 210 Safety Record
Complete NTSB accident and incident history. 819 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| May 17, 2016 | Wantage, NJ | N6450N | Fatal (1) | substantial |
A collision with terrain for reasons that could not be determined as the investigation did not reveal any postaccident anomalies with the airplane or …A collision with terrain for reasons that could not be determined as the investigation did not reveal any postaccident anomalies with the airplane or pilot. |
| Mar 19, 2016 | Myrtle Beach, SC | N59196 | Incident | substantial |
A complete loss of electrical power, which resulted from the separation of an alternator wire due to corrosion. Contributing to the accident was the f…A complete loss of electrical power, which resulted from the separation of an alternator wire due to corrosion. Contributing to the accident was the failure of the emergency landing gear extension system due to a lack of hydraulic fluid, which resulted in insufficient pressure to extend the landing gear. |
| Feb 02, 2016 | Park Valley, UT | N8340Z | Minor | substantial |
The pilot's decision to drag the left main landing gear on a snow covered dry lake bed, which resulted in a loss of directional control and a nose ove…The pilot's decision to drag the left main landing gear on a snow covered dry lake bed, which resulted in a loss of directional control and a nose over during an aborted landing. |
| Jan 26, 2016 | Lodi, CA | N7316E | Incident | substantial | The pilot's failure to attain a proper touchdown point, which led to a runway excursion. |
| Jan 18, 2016 | Venice, FL | N761EP | Incident | substantial | The pilot's failure to properly configure the landing gear, which resulted in a landing with the landing gear in the retracted position. |
| Nov 19, 2015 | Coalinga, CA | N9824G | Incident | substantial |
A partial loss of engine power during takeoff for reasons that could not be determined, because postaccident examination revealed no mechanical malfun…A partial loss of engine power during takeoff for reasons that could not be determined, because postaccident examination revealed no mechanical malfunctions or failures that would have precluded normal operation. |
| Jul 19, 2015 | Rio Verde, BR | PR-ITO | Fatal (1) | destroyed | Investigation pending |
| Jul 12, 2015 | Juneau, AK | N3607Y | Incident | substantial |
A loss of hydraulic fluid due to a fractured left main landing gear hydraulic actuator as a result of a fatigue crack, which led to the landing gear c…A loss of hydraulic fluid due to a fractured left main landing gear hydraulic actuator as a result of a fatigue crack, which led to the landing gear collapsing upon touchdown. |
| Jul 12, 2015 | Stafford Twp, NJ | N315EC | Minor | substantial |
The total loss of engine power due to the failure of the crankshaft, which resulted from a mechanic's failure to properly torque the engine cylinder t…The total loss of engine power due to the failure of the crankshaft, which resulted from a mechanic's failure to properly torque the engine cylinder through bolts. |
| May 21, 2015 | Pleasanton, CA | N1842F | Fatal (1) | destroyed |
The pilot’s continued visual flight into instrument flight rules conditions, which resulted in his failure to maintain sufficient clearance from risin…The pilot’s continued visual flight into instrument flight rules conditions, which resulted in his failure to maintain sufficient clearance from rising terrain. |
| Apr 11, 2015 | Assuncao do Piaui, BR | PR-APG | Fatal (1) | destroyed | Investigation pending |
| Jan 14, 2015 | Dodge City, KS | N3320S | Serious (1) | substantial | The loss of engine power on approach due to fuel exhaustion, which resulted from the pilot's improper preflight fuel planning and inspection. |
| Jan 08, 2015 | Sullivan, MO | N9565X | Incident | substantial |
The loss of hydraulic fluid and subsequent pressure due to cracks in the right main landing gear (MLG) actuator, which resulted in the collapse of the…The loss of hydraulic fluid and subsequent pressure due to cracks in the right main landing gear (MLG) actuator, which resulted in the collapse of the MLG during landing. |
| Dec 04, 2014 | Sussex, NJ | N8296Z | Minor | substantial |
Maintenance personnel’s inadequate inspection of the No. 2 cylinder valve area during the most recent annual inspection, which resulted in the in-flig…Maintenance personnel’s inadequate inspection of the No. 2 cylinder valve area during the most recent annual inspection, which resulted in the in-flight failure of the intake valve springs due to rust on the spring surfaces and subsequent fatigue cracking. |
| Dec 02, 2014 | Edinburg, TX | N9452T | Incident | substantial |
The loss of engine power due to fuel exhaustion, which resulted from the non-certificated pilot's inadequate preflight planning and inflight decision …The loss of engine power due to fuel exhaustion, which resulted from the non-certificated pilot's inadequate preflight planning and inflight decision making. |
| Nov 08, 2014 | Bullhead City, AZ | N9578X | Incident | substantial | The failure of the landing gear actuator housing during landing for reasons that could not be determined based on the available evidence. |
| Oct 24, 2014 | Kalamazoo, MI | N8219M | Incident | substantial |
The pilot's failure to ensure that the landing gear was fully extended in the down and locked position prior to touchdown, which resulted in the left …The pilot's failure to ensure that the landing gear was fully extended in the down and locked position prior to touchdown, which resulted in the left main landing gear collapse, runway excursion, and impact with a runway exit sign. |
| Jul 03, 2014 | Las Vegas, NM | N1175Q | Serious (1) | substantial |
The pilot's loss of airplane control during an aborted landing. Contributing to the accident was the pilot's inadequate preflight planning, which resu…The pilot's loss of airplane control during an aborted landing. Contributing to the accident was the pilot's inadequate preflight planning, which resulted in his attempt to land on a runway closed by a notice to airmen and the loss of engine power due to fuel exhaustion. |
| Jun 22, 2014 | Port Angeles, WA | N9457X | Incident | substantial | The pilot's failure to maintain directional control during landing, which resulted in a ground-loop. |
| May 28, 2014 | Moab, UT | N9589T | Incident | substantial | The pilot's inadequate landing flare, which resulted in a hard landing. |
| May 13, 2014 | Sinop, BR | PT-WHT | Incident | substantial | <br /><br /> |
| Apr 18, 2014 | Searcy, AR | N9421X | Minor | substantial | The pilot's inadequate preflight inspection of the airplane, which resulted in oil starvation and a subsequent engine failure. |
| Mar 17, 2014 | Marathon, FL | N210JZ | Incident | substantial |
The pilot's failure to ensure that the airplane's landing gear was down and locked prior to touchdown. Contributing to the accident was the possibilit…The pilot's failure to ensure that the airplane's landing gear was down and locked prior to touchdown. Contributing to the accident was the possibility of intermittent landing gear operation due to a faulty hydraulic power pack contactor. |
| Feb 15, 2014 | Clay, AL | N732EJ | Fatal (2) | destroyed |
The pilot's failure to maintain control of the airplane while being vectored to intercept the localizer during night instrument meteorological conditi…The pilot's failure to maintain control of the airplane while being vectored to intercept the localizer during night instrument meteorological conditions (IMC). Contributing to the accident was the operator's inadequate dispatch procedures, which did not prevent the pilot from flying beyond his duty day, flying at night for which he was not current, or flying in IMC for which he was not qualified by the company. |
| Feb 09, 2014 | Palmas, BR | PT-OMX | Fatal (3) | substantial | <br /><br /> |