Cessna 210 Safety Record
Complete NTSB accident and incident history. 819 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Oct 11, 1989 | OGDEN, UT | N7409E | Incident | substantial | AN ENGINE STOPPAGE FOR UNDETERMINED REASONS. |
| Oct 07, 1989 | JACKSONVILLE, FL | N5252E | Incident | substantial | INADEQUATE PREFLIGHT BY THE PILOT, AND FUEL STARVATION, DUE TO HIS IMPROPER POSITIONING OF THE FUEL SELECTOR. |
| Sep 07, 1989 | BETHANY, OK | N732XW | Incident | substantial |
A LOOSE FUEL LINE CONNECTION, DUE TO INADEQUATE MAINTENANCE, WHICH RESULTED IN FUEL STARVATION. FACTORS RELATED TO THE ACCIDENT WERE: DARKNESS AND T…A LOOSE FUEL LINE CONNECTION, DUE TO INADEQUATE MAINTENANCE, WHICH RESULTED IN FUEL STARVATION. FACTORS RELATED TO THE ACCIDENT WERE: DARKNESS AND THE OBSTRUCTIONS (HAY BALE & APPROACH LIGHT POLE) IN THE EMERGENCY LANDING AREA. |
| Aug 31, 1989 | WESTERLY, RI | N873PJ | Incident | destroyed | THE PILOT-IN-COMMAND'S FAILURE TO PROPERLY ENSURE A SUFFICIENT QUANTITY OF FUEL FOR THE INTENDED FLIGHT. |
| Jul 27, 1989 | THERMAL, CA | N76RR | Incident | substantial | A TWISTED NOSE GEAR UPLOCK DUE TO AN ELONGATED BOLT HOLE WHICH PREVENTED THE NOSE GEAR FROM EXTENDING. |
| Jun 26, 1989 | KAISER, MO | N9440T | Incident | substantial | FAILURE OF THE PILOT TO EXTEND THE LANDING GEAR. A FACTOR IN THE ACCIDENT WAS THE PILOT'S FAILURE TO USE THE CHECKLIST. |
| Jun 19, 1989 | OCEAN CITY, MD | N9520X | Incident | substantial |
FAILURE OF THE PILOT TO GO AROUND AFTER LANDING LONG & RECOVERING FROM A BOUNCED LANDING. CONTRIBUTING FACTORS WERE: THE PILOT'S EXCESSIVE AIRSPEED ON…FAILURE OF THE PILOT TO GO AROUND AFTER LANDING LONG & RECOVERING FROM A BOUNCED LANDING. CONTRIBUTING FACTORS WERE: THE PILOT'S EXCESSIVE AIRSPEED ON THE APCH, HIS IMPROPER FLARE FOR THE LANDING, HIS FAILURE TO ATTAIN THE PROPER TOUCHDOWN POINT, AND THE AIRPORT FACILITY (LOCALIZER TRANSMITTER) BEYOND THE END OF THE RUNWAY. |
| Jun 09, 1989 | HALLS CROSSING, UT | N9515Y | Incident | substantial | INADEQUATE AIRCRAFT HANDLING BY THE PILOT, RESULTING IN A RUNWAY OVERRUN. |
| Jan 14, 1989 | CARSON CITY, NV | N7342E | Incident | substantial |
SEPARATION OF THE THROTTLE CABLE DUE TO WEAR AS POWER WAS APPLIED FOR A LANDING GO-AROUND. CONTRIBUTING TO THE ACCIDENT WAS ROUGH TERRAIN AT THE TOUCH…SEPARATION OF THE THROTTLE CABLE DUE TO WEAR AS POWER WAS APPLIED FOR A LANDING GO-AROUND. CONTRIBUTING TO THE ACCIDENT WAS ROUGH TERRAIN AT THE TOUCHDOWN POINT OF THE FORCED LANDING. |
| Jan 07, 1989 | Greenwood, MS | N590GC | Incident | substantial | FAILURE OF THE PILOT TO MAINTAIN DIRECTIONAL CONTROL, WHICH RESULTED IN AN INADVERTENT GROUND SWERVE. |
| Dec 24, 1988 | ROSWELL, NM | N59217 | Incident | minor | Investigation pending |
| Dec 17, 1988 | BANNOCK BURN, IL | N5225K | Incident | substantial | FUEL STARVATION CAUSED BY ICE BLOCKED FUEL LINES. |
| Dec 17, 1988 | TWIN FALLS, ID | N3815Y | Incident | substantial | Investigation pending |
| Nov 12, 1988 | STUART, FL | N2267S | Incident | minor | Investigation pending |
| Nov 07, 1988 | ANACORTES, WA | N9495M | Incident | substantial | Investigation pending |
| Nov 04, 1988 | MONTE VISTA, CO | N6240B | Incident | substantial | Investigation pending |
| Oct 19, 1988 | MALTA, MT | N3811Y | Incident | substantial | Investigation pending |
| Oct 11, 1988 | ORLANDO, FL | N9064M | Incident | minor | Investigation pending |
| Sep 30, 1988 | KIRKWOOD, NY | N7457E | Incident | substantial | Investigation pending |
| Sep 23, 1988 | JUNEAU, AK | N249CC | Incident | substantial | Investigation pending |
| Jul 10, 1988 | INDIANAPOLIS, IN | N210WP | Incident | substantial | Investigation pending |
| Jul 06, 1988 | BAKER, NV | N6524X | Incident | substantial | Investigation pending |
| Jun 20, 1988 | TRES PINOS, CA | N732KS | Incident | substantial | Investigation pending |
| Jun 05, 1988 | RENO, NV | N70SA | Incident | substantial | Investigation pending |
| May 29, 1988 | NEW ROADS, LA | N3799Y | Incident | destroyed | Investigation pending |