Cessna 182H Safety Record
Complete NTSB accident and incident history. 76 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Oct 04, 2025 | Smithfield, RI | N1998X | Incident | substantial |
Maintenance personnel’s improper rigging of the elevator trim system, which resulted in a hard landing. Contributing was the maintenance personnel and…Maintenance personnel’s improper rigging of the elevator trim system, which resulted in a hard landing. Contributing was the maintenance personnel and pilot’s failure to perform adequate post maintenance/preflight inspections. |
| May 10, 2024 | Three Forks, MT | N2388X | Incident | substantial |
The pilot’s inadequate preflight inspection, which resulted in an attempted departure with the flight control lock device installed, and subsequent no…The pilot’s inadequate preflight inspection, which resulted in an attempted departure with the flight control lock device installed, and subsequent nose landing gear collapse. |
| Jul 04, 2022 | Petaluma, CA | N8414S | Incident | substantial | The pilot’s failure to maintain airplane control during a go-around in gusting wind conditions. |
| Apr 11, 2021 | Blakely Island, WA | N2030X | Incident | substantial | A total loss of engine power during climb for reasons that could not be determined which resulted in a forced water landing. |
| Nov 12, 2017 | Tucson, AZ | N8515S | Incident | substantial | The pilot’s failure to use taxiways shown on the airport diagrams and his subsequent failure to avoid a ditch. |
| Dec 27, 2013 | Littleton, NC | N1833X | Incident | substantial | The pilot's failure to maintain directional control during takeoff. |
| Jul 09, 2013 | Hesperia, CA | N2062X | Incident | substantial | The loss of engine power during cruise flight due to the detachment of the mixture control cable from its mounting clamp. |
| Jun 16, 2012 | Meadow Creek, MT | N2424X | Incident | substantial | The pilot's misjudged approach and improper landing flare, which resulted in a hard landing. |
| Jun 20, 2011 | Soldotna, AK | N331AA | Incident | substantial | The pilot's failure to maintain pitch control resulting in an aerodynamic stall. |
| Apr 14, 2011 | Park Falls, WI | N8364S | Incident | substantial | The student pilot's failure to maintain aircraft control during an aborted landing. |
| May 05, 2008 | Prescott, AZ | N6320B | Incident | substantial | A loss of engine power from fuel starvation due to the pilot's mismanagement of the fuel system and failure to select a tank containing fuel. |
| Aug 14, 2007 | Page, AZ | N3464S | Incident | substantial | the pilot's failure to maintain clearance with obstructions while taxiing behind parked airplanes. |
| Mar 14, 2007 | Phoenix, AZ | N1903X | Incident | substantial | The pilot's inadequate preflight inspection, resulting in fuel exhaustion and the loss of power. A factor was the sign. |
| Jul 08, 2006 | Birmingham, AL | N3479S | Incident | substantial | The pilot's failure to maintain airspeed during final approach resulting in a stall/mush and a hard landing. |
| Sep 09, 2004 | Nashua, NH | N8463S | Incident | substantial | An in flight collision with birds while landing. A factor was the night conditions. |
| Jun 08, 2004 | La Belle, FL | N8304S | Incident | substantial | The inadvertent deployment of the main parachute resulting in damage to the right horizontal stabilizer and elevator. |
| Oct 05, 2003 | Knoxville, TN | N1919X | Incident | substantial |
The pilot's inadequate preflight inspection by his failure to secure the left fuel tank cap which resulted in fuel exhaustion, and the loss of engine …The pilot's inadequate preflight inspection by his failure to secure the left fuel tank cap which resulted in fuel exhaustion, and the loss of engine power. |
| Jul 29, 2003 | New Era, MI | N460JH | Incident | substantial | The pilot's misjudged flare which led to a hard landing and subsequent collapse of the landing gear. |
| Mar 08, 2002 | West Plains, MO | N64AE | Incident | substantial |
The engine failure due to the fatigue fracture of the crankshaft which resulted from the installation of improper pistons during an STC'd engine conve…The engine failure due to the fatigue fracture of the crankshaft which resulted from the installation of improper pistons during an STC'd engine conversion by other maintenance personnel. Additional factors included the unsuitable terrain encountered by the pilot during the forced landing. |
| Feb 17, 2001 | Weaver, AL | N8556S | Incident | substantial |
Damage to the No. 4 cylinder intake valve push rod tube at an undetermined time which resulted in the push rod rubbing on the push rod tube and failin…Damage to the No. 4 cylinder intake valve push rod tube at an undetermined time which resulted in the push rod rubbing on the push rod tube and failing due to wear, resulting in loss of engine power and damage to the airplane during a forced landing in a field. |
| Jul 06, 1997 | PEDRICTOWN, NJ | N1858X | Incident | substantial | The pilot's improper flare. |
| Jan 06, 1997 | BURBANK, CA | N1870X | Incident | substantial |
the pilot's improper planning/decision concerning landing and taxiing in high wind conditions. Factors relating to the accident were: the unfavorable…the pilot's improper planning/decision concerning landing and taxiing in high wind conditions. Factors relating to the accident were: the unfavorable wind conditions, and the lack of crosswind limit information in the Cessna 182H Pilot's Operating Handbook regarding landing or taxiing operations. |
| Nov 28, 1995 | KOYUK, AK | N1997X | Incident | destroyed |
The pilot's delayed application of carburetor heat. Factors in the accident were carburetor icing conditions and lack of suitable terrain for a force…The pilot's delayed application of carburetor heat. Factors in the accident were carburetor icing conditions and lack of suitable terrain for a forced landing. |
| Nov 23, 1995 | EAGLE LAKE, TX | N8493S | Incident | destroyed | a loss of engine power for undetermined reasons. Factors were the lack of suitable terrain for the forced landing and the dark night. |
| Jun 03, 1994 | TELLURIDE, CO | N1838X | Incident | substantial | WAS THE PILOT'S IMPROPER RECOVERY FROM A BOUNCED LANDING. FACTORS WERE GUSTY WINDS AND RUNWAY DOWNSLOPE. |