Cessna 182 Safety Record

Complete NTSB accident and incident history. 2779 events recorded from 1982 to 2026.

2779

All Events

1535

Incidents

459

Minor

249

Serious

529

Fatal (1000 fatalities)

Date Location Reg# Severity Damage Probable Cause
Dec 17, 1994 BOWLING GREEN, MO N6090B Minor substantial
INADEQUATE DESIGN OF THE RESERVE PARACHUTE CABLE HOUSING, WHICH RESULTED IN AN INADVERTENT DEPLOYMENT OF THE PARACHUTE, AND SUBSEQUENT COLLISION WITH,…

INADEQUATE DESIGN OF THE RESERVE PARACHUTE CABLE HOUSING, WHICH RESULTED IN AN INADVERTENT DEPLOYMENT OF THE PARACHUTE, AND SUBSEQUENT COLLISION WITH, AND JAMMING OF, THE AIRCRAFT'S HORIZONTAL STABILIZER, NECESSITATING A FORCED LANDING.

Nov 27, 1994 GREER, SC N6556M Minor substantial
THE PILOT'S FAILURE TO FOLLOW INSTRUMENT APPROACH PROCEDURES AND HIS PREMATURE DESCENT BELOW THE PUBLISHED DECISION HEIGHT. A FACTOR WAS PILOT FATIGUE…

THE PILOT'S FAILURE TO FOLLOW INSTRUMENT APPROACH PROCEDURES AND HIS PREMATURE DESCENT BELOW THE PUBLISHED DECISION HEIGHT. A FACTOR WAS PILOT FATIGUE.

Nov 16, 1994 HASKELL, OK N5931J Minor substantial
THE TOTAL LOSS OF ENGINE POWER DUE TO CONTAMINATED FUEL. FACTORS WERE THE IMPROPER MAINTENANCE PROCEDURES RESULTING IN FUEL CONTAMINATION, THE PILOT'S…

THE TOTAL LOSS OF ENGINE POWER DUE TO CONTAMINATED FUEL. FACTORS WERE THE IMPROPER MAINTENANCE PROCEDURES RESULTING IN FUEL CONTAMINATION, THE PILOT'S INADEQUATE PREFLIGHT INSPECTION, AND THE LACK OF SUITABLE TERRAIN AVAILABLE FOR THE FORCED LANDING.

Oct 15, 1994 WORTHINGTON, PA N70751 Minor substantial The failure of the aileron control cable which resulted in the inflight loss of control and collision with trees.
Sep 23, 1994 MONTE VISTA, CO N3540U Minor substantial THE PILOT'S FAILURE TO MAINTAIN DIRECTIONAL. FACTORS WERE THE CROSS WIND CONDITIONS, AND THE PILOT'S POOR EVALUATION OF THE WEATHER.
Sep 04, 1994 TWENTYNINE PALM, CA N8431T Minor substantial the cause of the loss of engine power could not be determined. The dirt berm was a factor in this accident.
Sep 02, 1994 ARDMORE, OK N3413R Minor substantial THE PARTIAL LOSS OF POWER DUE TO A CYLINDER HEAD SEPARATION. FACTORS WERE THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING AND THE LOW CEILING.
Aug 09, 1994 TEXARKANA, TX N1478S Minor substantial
FUEL CONTAMINATION AND THE IMPROPER ADJUSTMENTS MADE TO THE CARBURETOR BY UNIDENTIFIED MAINTENANCE PERSONNEL. A FACTOR WAS THE LACK OF SUITABLE TERRAI…

FUEL CONTAMINATION AND THE IMPROPER ADJUSTMENTS MADE TO THE CARBURETOR BY UNIDENTIFIED MAINTENANCE PERSONNEL. A FACTOR WAS THE LACK OF SUITABLE TERRAIN TO WHICH A FORCED LANDING COULD BE EXECUTED.

Jul 14, 1994 GREENVILLE, SC N21380 Minor substantial THE PILOT'S IMPROPER POSITIONING OF THE FUEL SELECTOR VALVE WHICH RESULTED IN FUEL STARVATION.
Jul 02, 1994 GARDEN CITY, KS N901JM Minor substantial fuel exhaustion for reason or reasons undetermined. A factor was the rough/uneven terrain.
Jun 19, 1994 INDIAN VALLEY, ID N735QB Minor substantial CONNECTING ROD BOLT FATIGUE AND NO SUITABLE TERRAIN FOR THE FORCED LANDING.
May 21, 1994 BRYAN, TX N6372A Minor substantial
THE PILOT'S FAILURE TO REFUEL RESULTING IN A TOTAL LOSS OF ENGINE POWER DUE TO FUEL EXHAUSTION. A FACTOR WAS THE LACK OF SUITABLE TERRAIN FOR THE FORC…

THE PILOT'S FAILURE TO REFUEL RESULTING IN A TOTAL LOSS OF ENGINE POWER DUE TO FUEL EXHAUSTION. A FACTOR WAS THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING.

May 07, 1994 CRYSTAL RIVER, FL N7355S Minor substantial FAILURE OF THE PILOT-IN-COMMAND TO MAINTAIN DIRECTIONAL CONTROL DURING THE LANDING ROLL.
May 01, 1994 PHOENIX, AZ N1454S Minor substantial the pilot's failure to ensure that the magneto switch was in the off position prior to rotating the propeller by hand.
Apr 23, 1994 ATHENS, AL N2945F Minor substantial THE MECHANIC'S FAILURE TO PROPERLY INSTALL AN ACCESS PLUG WHICH RESULTED IN THE LOSS OF ENGINE OIL PRESSURE.
Nov 10, 1993 SALT LAKE CITY, UT N9652X Minor destroyed
THE PILOT IN COMMAND'S MAINTAINING INADEQUATE ALTITUDE WHILE CROSSING OVER THE GROUND TRACK OF THE LANDING BOEING 757. A FACTOR CONTRIBUTING TO THE A…

THE PILOT IN COMMAND'S MAINTAINING INADEQUATE ALTITUDE WHILE CROSSING OVER THE GROUND TRACK OF THE LANDING BOEING 757. A FACTOR CONTRIBUTING TO THE ACCIDENT WAS WAKE TURBULENCE.

Oct 24, 1993 BYRON, WI N5390B Minor destroyed
the pilot's inaccurate fuel consumption calculations which resulted in his not refueling during the flight. A factor related to the accident was the …

the pilot's inaccurate fuel consumption calculations which resulted in his not refueling during the flight. A factor related to the accident was the pilot's failure to maintain proper airspeed during the forced landing.

Oct 01, 1993 BATAVIA, OH N3332U Minor substantial THE PILOT'S IMPROPER FLARE.
Jul 30, 1993 PAGOSA SPRINGS, CO CGLIL Minor destroyed
THE DECISION BY THE PILOT IN COMMAND TO FLY AT AN ALTITUDE INSUFFICIENT FOR THE SURROUNDING TERRAIN. FACTORS WERE: THE PILOT'S ATTENTION BEING MOMENT…

THE DECISION BY THE PILOT IN COMMAND TO FLY AT AN ALTITUDE INSUFFICIENT FOR THE SURROUNDING TERRAIN. FACTORS WERE: THE PILOT'S ATTENTION BEING MOMENTARILY DIVERTED AND THE AIRPLANE'S CLIMB PERFORMANCE BEING EXCEEDED.

Jun 18, 1993 HOLBROOK, NY N735CA Minor destroyed THE ENGINE FAILURE AS THE RESULT OF A FRACTURED CRANKSHAFT DUE TO METAL FATIGUE.
Jun 13, 1993 WOODSTOCK, CT N6158B Minor substantial A COMPLETE LOSS OF ENGINE POWER FOR UNDETERMINED REASONS.
Apr 12, 1993 TORRANCE, CA N460JA Minor destroyed
FAILURE OF THE PILOT TO ATTAIN SUFFICIENT LIFT OFF AIRSPEED. FACTORS IN THIS ACCIDENT WERE THE PILOT'S OVERCONFIDENCE IN HIS PILOTING SKILLS, AND THE…

FAILURE OF THE PILOT TO ATTAIN SUFFICIENT LIFT OFF AIRSPEED. FACTORS IN THIS ACCIDENT WERE THE PILOT'S OVERCONFIDENCE IN HIS PILOTING SKILLS, AND THE INADVERTENT STALL OF THE AIRPLANE.

Apr 08, 1993 HAMILTON, MT N71654 Minor substantial THE PILOT'S IMPROPER USE OF CARBURETOR HEAT. A FACTOR WHICH CONTRIBUTED TO THE ACCIDENT WAS THE CARBURETOR ICING CONDITIONS.
Mar 15, 1993 LAKE HAVASU, AZ N466KT Minor substantial
THE IMPROPER WELDING OF THE INBOARD BOSS BY AN UNKNOWN PERSON RESULTING IN A FATIGUE FAILURE ON THE INBOARD BOSS. A FACTOR RELATED TO THE ACCIDENT WA…

THE IMPROPER WELDING OF THE INBOARD BOSS BY AN UNKNOWN PERSON RESULTING IN A FATIGUE FAILURE ON THE INBOARD BOSS. A FACTOR RELATED TO THE ACCIDENT WAS THE VEHICLE THAT WAS STRUCK DURING THE FORCED LANDING.

Feb 22, 1993 RALEIGH, MS N1581M Minor substantial THE FATIGUE FAILURE OF THE NO. 1 EXHAUST VALVE FOR UNDETERMINED REASONS, AND THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING.
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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