Cessna 172 Safety Record
Complete NTSB accident and incident history. 6810 events recorded from 1974 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jan 29, 2018 | Babylon, NY | N294ME | Incident | substantial |
The partial loss of engine power after a simulated engine failure for reasons that could not be determined because a postaccident examination and an e…The partial loss of engine power after a simulated engine failure for reasons that could not be determined because a postaccident examination and an engine test run did not reveal any anomalies that would have precluded normal operation. |
| Jan 26, 2018 | Silver City, NM | N1046F | Incident | substantial | The student pilot’s improper landing flare in gusting crosswind conditions, which resulted in a hard, bounced landing. |
| Jan 24, 2018 | McKinney, TX | N9520Z | Incident | substantial | The student pilot’s improper approach and landing flare, which resulted in a porpoised landing. |
| Jan 21, 2018 | Martinsburg, WV | N9415B | Incident | substantial | A hydraulic leak in the right main landing gear actuator, which resulted in the main landing gear not extending. |
| Dec 21, 2017 | Monroe, MI | N4491R | Incident | substantial |
The student pilot’s improper yaw control during the landing flare and the flight instructor’s failure to take remedial action, which resulted in a har…The student pilot’s improper yaw control during the landing flare and the flight instructor’s failure to take remedial action, which resulted in a hard landing. |
| Dec 09, 2017 | Algona, IA | N8856B | Incident | substantial | The No. 1 cylinder head separating at the cylinder head-to-barrel interface and the subsequent total loss of engine power. |
| Dec 08, 2017 | Everett, WA | N4801D | Incident | substantial | The pilot’s decision to abort the takeoff following a touch-and-go landing with too little runway remaining, which resulted in a runway overrun. |
| Dec 07, 2017 | Auburn, WA | N2351U | Incident | substantial | The pilot's loss of airplane control for reasons that could not be determined based on the available information. |
| Dec 02, 2017 | Park Rapids, MN | N524ND | Incident | substantial | The student pilot’s improper landing flare, which resulted in the propeller striking the ground. |
| Dec 02, 2017 | Huntingdon, TN | N9730F | Incident | substantial |
A total loss of engine power for reasons that could not be determined because a postaccident engine examination and testing revealed no preimpact mech…A total loss of engine power for reasons that could not be determined because a postaccident engine examination and testing revealed no preimpact mechanical malfunctions or failures that would have precluded normal operation. |
| Dec 01, 2017 | Miami, FL | N537HF | Incident | substantial | The pilot's decision to continue the landing after a loss of visual cues during a night landing. |
| Nov 30, 2017 | Bowie, MD | N474SP | Incident | substantial |
The pilot’s failure to maintain situational awareness during the approach to land. Contributing to the accident was the pilot’s distraction by the ins…The pilot’s failure to maintain situational awareness during the approach to land. Contributing to the accident was the pilot’s distraction by the instrument panel during the approach. |
| Nov 26, 2017 | Daytona Beach, FL | N452ER | Incident | substantial | The pilot’s improper landing flare, which resulted in a hard, bounced landing. |
| Nov 22, 2017 | Maple Lake, MN | N734VH | Incident | substantial | The pilot’s failure to maintain directional control while landing, which resulted in a runway excursion. |
| Nov 20, 2017 | San Diego, CA | N172SX | Incident | substantial | An in-flight collision with a bird. |
| Nov 16, 2017 | Opa Locka, FL | N6102R | Incident | substantial |
A failure of the airplane 's electrical system, which led to the failure of the landing gear system, for reasons that could not be determined because …A failure of the airplane 's electrical system, which led to the failure of the landing gear system, for reasons that could not be determined because postaccident examination and testing revealed no mechanical anomalies that would have precluded normal operation. Contributing to the accident were the inoperative landing gear unsafe warning horn and the low voltage warning light. |
| Nov 16, 2017 | Pompano, FL | N75919 | Incident | substantial | The pilot’s improper landing flare, which resulted in a porpoise. |
| Nov 09, 2017 | Trenton, NJ | N2138W | Incident | substantial | The pilot’s improper landing flare, which resulted in a bounced landing. |
| Nov 07, 2017 | Bonners Ferry, ID | N55234 | Incident | substantial | The pilot’s failure to see and avoid power lines while maneuvering at a low altitude. |
| Nov 02, 2017 | Redding, CA | N2103T | Incident | substantial |
The fatigue separation of the crankshaft due to a fatigue fracture, which resulted in a total loss of engine power and a subsequent off-airport landin…The fatigue separation of the crankshaft due to a fatigue fracture, which resulted in a total loss of engine power and a subsequent off-airport landing and impact with a fence. |
| Oct 17, 2017 | Old Bridge, NJ | N6384D | Incident | substantial | The student pilot’s failure to maintain directional control during the landing roll. |
| Oct 15, 2017 | Auburn, WA | N5159U | Incident | substantial |
The failure of the right main landing gear for reasons that could not be determined because postaccident examination did not reveal any anomalies that…The failure of the right main landing gear for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation. |
| Oct 08, 2017 | Black River Falls, WI | N9664Q | Incident | substantial | The pilot’s failure to maintain directional control during landing in gusting crosswind conditions. |
| Oct 02, 2017 | Tonopah, NV | N5311H | Incident | substantial |
The pilot's failure to enrich the mixture during the descent, as required by the Pilot's Operating Handbook (POH), and his subsequent failure to follo…The pilot's failure to enrich the mixture during the descent, as required by the Pilot's Operating Handbook (POH), and his subsequent failure to follow the POH emergency procedures, which resulted in an excessively lean fuel/air mixture and subsequent loss of rpm. Contributing to the accident was the pilot's improper decision to land on unsuitable terrain despite the availability of two nearby airports. |
| Sep 25, 2017 | Tamuning, USA | N5448K | Incident | substantial | The pilot's inadequate preflight inspection, which resulted in oil exhaustion and a subsequent total loss of engine power during cruise flight. |