Cessna 150G Safety Record
Complete NTSB accident and incident history. 244 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Sep 20, 2025 | Seagoville, TX | N2500Q | Incident | substantial | The pilot’s inadequate fuel planning which resulted in a total loss of engine power due to fuel exhaustion. |
| Jun 17, 2025 | Heber City, UT | N6349S | Incident | substantial | The student pilot’s improper recovery from a bounced landing, which resulted in a nose over. |
| Dec 20, 2022 | Pocahantas, IA | 2930J | Incident | substantial |
The pilot’s landing flare which resulted in a bounced landing and the nose landing gear collapsing. Contributing to the accident was the airplane's en…The pilot’s landing flare which resulted in a bounced landing and the nose landing gear collapsing. Contributing to the accident was the airplane's encounter with adverse weather conditions which led to structural icing that affected flight characteristics and obscured the pilot's vision. Also contributing to the accident were the self-induced and external pressures that influenced the pilot’s decision to initiate and continue the flight. |
| Jul 15, 2022 | Tuscaloosa, AL | N3301J | Incident | substantial |
The student pilot’s inadvertent use of the fuel mixture knob instead of the carburetor heat knob, which resulted in fuel starvation and a subsequent l…The student pilot’s inadvertent use of the fuel mixture knob instead of the carburetor heat knob, which resulted in fuel starvation and a subsequent loss of engine power. |
| Feb 17, 2021 | Indian Head, MD | N8428J | Incident | substantial |
The pilot’s failure to detect water in the fuel during the preflight inspection, which resulted in a total loss of engine power. Contributing was the …The pilot’s failure to detect water in the fuel during the preflight inspection, which resulted in a total loss of engine power. Contributing was the flight instructor’s mismanagement of the precautionary landing approach. |
| Aug 13, 2016 | Shirley, NY | N3666J | Incident | substantial |
Maintenance personnel’s inadequate maintenance and inspection of the airplane, which resulted in the left elevator attachment bolt backing out of the …Maintenance personnel’s inadequate maintenance and inspection of the airplane, which resulted in the left elevator attachment bolt backing out of the nutplate, and partial inflight separation and damage of the elevator. |
| Mar 02, 2016 | Simmesport, LA | N3339J | Incident | substantial |
The installation of an improper bearing and thrust washer during engine overhaul, which resulted in failure of the connecting rods and a subsequent to…The installation of an improper bearing and thrust washer during engine overhaul, which resulted in failure of the connecting rods and a subsequent total loss of engine power. |
| Jul 20, 2015 | Mekoryuk, AK | N3392J | Incident | substantial | The pilot's improper decision to land on an unsuitable landing surface which resulted in a nose over. |
| Aug 21, 2014 | Pittstown, NJ | N2466J | Incident | substantial |
A total loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any a…A total loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation. |
| Sep 06, 2013 | Denver, CO | N4791X | Incident | substantial |
The pilot's failure to maintain directional control during landing which resulted in an impact with the runway surface. A contributing factor was the …The pilot's failure to maintain directional control during landing which resulted in an impact with the runway surface. A contributing factor was the certified flight instructor delayed response to the pilot's improper landing. |
| Jun 10, 2013 | Franklin, OH | N3718J | Incident | substantial | The pilot's improper fuel planning which resulted in a loss of engine power due to fuel exhaustion. |
| Jun 03, 2012 | Ketchikan, AK | N3235J | Incident | substantial | The pilot’s decision to take off with a quartering tailwind, which resulted in a loss of control. |
| Jul 06, 2011 | Mesa, AZ | N2878S | Incident | substantial | The pilot's failure to maintain directional control during the go around. |
| Jun 21, 2010 | Jasper, TN | N8321J | Incident | substantial | The pilot under instruction's failure to maintain directional control during landing, and his failure to relinquish the flight controls when directed. |
| Apr 04, 2010 | Winter Haven, FL | N4655X | Incident | substantial | The student pilot's inadequate recovery from a bounced landing in gusting winds. |
| Feb 01, 2010 | St. Augustine, FL | N3995J | Incident | substantial |
A loss of engine power due to fuel exhaustion caused by the failure of the right wing fuel tank sending unit gasket, which resulted in a forced landin…A loss of engine power due to fuel exhaustion caused by the failure of the right wing fuel tank sending unit gasket, which resulted in a forced landing. |
| Jan 01, 2010 | Doylestown, PA | N4026J | Incident | substantial | A partial loss of engine power due to carburetor icing. |
| Apr 24, 2009 | Kingston, NY | N2792S | Incident | substantial | The pilot's failure to maintain clearance from trees during approach. |
| Jun 10, 2008 | Brenham, TX | N4691R | Incident | substantial |
The sudden windshift (crosswind gust), rendering directional control impossible. Contributing factors in this accident were the high speed during the …The sudden windshift (crosswind gust), rendering directional control impossible. Contributing factors in this accident were the high speed during the aborted takeoff and trees. |
| Feb 16, 2008 | Viroqua, WI | N10RH | Incident | substantial | The pilot not maintaining directional control during the landing and the ground loop the pilot encountered. A factor was the crosswind. |
| Jan 10, 2008 | Sarasota, FL | N2490J | Incident | substantial | The pilot's improper preflight and in-flight planning which resulted in a loss of engine power due to fuel exhaustion. |
| Aug 25, 2007 | Kenai, AK | N2981S | Incident | substantial | The pilot's excessive flap setting during takeoff. |
| Dec 06, 2006 | Eureka, CA | N3394J | Incident | substantial |
a loss of engine power due to carburetor icing and the pilot's inadequate preflight planning and decision to operate the airplane in carburetor icing …a loss of engine power due to carburetor icing and the pilot's inadequate preflight planning and decision to operate the airplane in carburetor icing conditions with an inoperative carburetor heat system. |
| Jun 27, 2006 | Indianapolis, IN | N3366J | Incident | substantial |
The pilot intentionally leaving the airplane unoccupied during the engine start and the failure of the tail tie-down, which ultimately resulted in the…The pilot intentionally leaving the airplane unoccupied during the engine start and the failure of the tail tie-down, which ultimately resulted in the unoccupied airplane becoming airborne. |
| May 06, 2006 | Coleman, TX | N3815J | Incident | substantial |
The pilot's failure to refuel the airplane, which resulted in fuel exhaustion. A contributing factor was the lack of suitable terrain available for t…The pilot's failure to refuel the airplane, which resulted in fuel exhaustion. A contributing factor was the lack of suitable terrain available for the forced landing. |