Cessna 150G Safety Record
Complete NTSB accident and incident history. 244 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Sep 20, 2025 | Seagoville, TX | N2500Q | Incident | substantial | The pilot’s inadequate fuel planning which resulted in a total loss of engine power due to fuel exhaustion. |
| Jun 17, 2025 | Heber City, UT | N6349S | Incident | substantial | The student pilot’s improper recovery from a bounced landing, which resulted in a nose over. |
| Sep 14, 2023 | Cross Keys, NJ | N2880S | Serious (1) | substantial | The pilot’s failure to maintain adequate airspeed during the banner pickup, which resulted in a low altitude aerodynamic stall/spin. |
| Feb 27, 2023 | Hillsville, VA | N2991J | Fatal (1) | substantial | The pilot’s continued visual flight rules flight into instrument meteorological conditions, resulting in controlled flight into terrain. |
| Dec 20, 2022 | Pocahantas, IA | 2930J | Incident | substantial |
The pilot’s landing flare which resulted in a bounced landing and the nose landing gear collapsing. Contributing to the accident was the airplane's en…The pilot’s landing flare which resulted in a bounced landing and the nose landing gear collapsing. Contributing to the accident was the airplane's encounter with adverse weather conditions which led to structural icing that affected flight characteristics and obscured the pilot's vision. Also contributing to the accident were the self-induced and external pressures that influenced the pilot’s decision to initiate and continue the flight. |
| Nov 11, 2022 | Star Valley, AZ | N3131J | Serious (1) | substantial | The failure of the No. 1 cylinder exhaust or intake valve which resulted in the partial loss of engine power and subsequent impact with terrain. |
| Jul 15, 2022 | Tuscaloosa, AL | N3301J | Incident | substantial |
The student pilot’s inadvertent use of the fuel mixture knob instead of the carburetor heat knob, which resulted in fuel starvation and a subsequent l…The student pilot’s inadvertent use of the fuel mixture knob instead of the carburetor heat knob, which resulted in fuel starvation and a subsequent loss of engine power. |
| Feb 17, 2021 | Indian Head, MD | N8428J | Incident | substantial |
The pilot’s failure to detect water in the fuel during the preflight inspection, which resulted in a total loss of engine power. Contributing was the …The pilot’s failure to detect water in the fuel during the preflight inspection, which resulted in a total loss of engine power. Contributing was the flight instructor’s mismanagement of the precautionary landing approach. |
| Sep 20, 2017 | Rhine, GA | N3875J | Fatal (1) | substantial |
The student pilot's decision to take off from a partially-lit grass runway in dark night, marginal visual flight rules conditions, which resulted in s…The student pilot's decision to take off from a partially-lit grass runway in dark night, marginal visual flight rules conditions, which resulted in spatial disorientation, an exceedance of the airplane's critical angle of attack, and an aerodynamic stall. |
| Aug 13, 2016 | Shirley, NY | N3666J | Incident | substantial |
Maintenance personnel’s inadequate maintenance and inspection of the airplane, which resulted in the left elevator attachment bolt backing out of the …Maintenance personnel’s inadequate maintenance and inspection of the airplane, which resulted in the left elevator attachment bolt backing out of the nutplate, and partial inflight separation and damage of the elevator. |
| Mar 02, 2016 | Simmesport, LA | N3339J | Incident | substantial |
The installation of an improper bearing and thrust washer during engine overhaul, which resulted in failure of the connecting rods and a subsequent to…The installation of an improper bearing and thrust washer during engine overhaul, which resulted in failure of the connecting rods and a subsequent total loss of engine power. |
| Jul 20, 2015 | Mekoryuk, AK | N3392J | Incident | substantial | The pilot's improper decision to land on an unsuitable landing surface which resulted in a nose over. |
| Jan 09, 2015 | Pontiac, IL | N2871S | Minor | substantial |
The flight instructor’s loss of directional control during an attempted go-around with a crosswind. Contributing to the accident was the loss of engin…The flight instructor’s loss of directional control during an attempted go-around with a crosswind. Contributing to the accident was the loss of engine power for reasons that could not be determined during examination of the engine. |
| Aug 21, 2014 | Pittstown, NJ | N2466J | Incident | substantial |
A total loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any a…A total loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation. |
| Sep 06, 2013 | Denver, CO | N4791X | Incident | substantial |
The pilot's failure to maintain directional control during landing which resulted in an impact with the runway surface. A contributing factor was the …The pilot's failure to maintain directional control during landing which resulted in an impact with the runway surface. A contributing factor was the certified flight instructor delayed response to the pilot's improper landing. |
| Jun 10, 2013 | Franklin, OH | N3718J | Incident | substantial | The pilot's improper fuel planning which resulted in a loss of engine power due to fuel exhaustion. |
| Mar 17, 2013 | Baytown, TX | N6389S | Minor | substantial | The pilot’s poor in-flight decision-making and improper fuel management, which resulted in a loss of engine power due to fuel exhaustion. |
| Sep 21, 2012 | Corinth, MS | N8465J | Minor | substantial |
The improper torque application on the crankshaft gear bolt by maintenance personnel during an engine overhaul, which resulted in the fatigue failure …The improper torque application on the crankshaft gear bolt by maintenance personnel during an engine overhaul, which resulted in the fatigue failure of the locking tab washer and gear alignment dowel and subsequent engine stoppage. Contributing to the accident was the operator’s exceedence of the engine overhaul calendar year limits recommended by the engine manufacturer. |
| Aug 26, 2012 | Madera, CA | N6346S | Minor | substantial | The pilot's mismanagement of the fuel supply, which resulted in fuel exhaustion. |
| Jun 03, 2012 | Ketchikan, AK | N3235J | Incident | substantial | The pilot’s decision to take off with a quartering tailwind, which resulted in a loss of control. |
| Jan 23, 2012 | Quincy, FL | N73JK | Fatal (1) | substantial |
The non-instrument-rated pilot’s spatial disorientation in night instrument meteorological conditions, which resulted in his inability to maintain con…The non-instrument-rated pilot’s spatial disorientation in night instrument meteorological conditions, which resulted in his inability to maintain controlled flight. Contributing to the accident was the pilot’s improper decision to take off in deteriorating meteorological conditions. |
| Jan 11, 2012 | Fitchburg, MA | N4041J | Serious (1) | substantial | A partial loss of engine power due to the formation of carburetor ice and the flight instructor's improper application of carburetor heat. |
| Aug 23, 2011 | Cavanaugh Bay, ID | N2870S | Serious (1) | substantial |
The pilot’s failure to maintain adequate airspeed during an attempt to execute a go-around with a tailwind condition, which resulted in an aerodynamic…The pilot’s failure to maintain adequate airspeed during an attempt to execute a go-around with a tailwind condition, which resulted in an aerodynamic stall and spin. |
| Jul 06, 2011 | Mesa, AZ | N2878S | Incident | substantial | The pilot's failure to maintain directional control during the go around. |
| Feb 12, 2011 | Springdale, AR | N3257J | Minor | substantial | The pilot’s improper fuel management, which resulted in a loss of engine power due to fuel exhaustion. |