Cessna 150 Safety Record
Complete NTSB accident and incident history. 3241 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Sep 29, 1998 | BONNERS FERRY, ID | N19427 | Incident | substantial |
Improper maintenance by an outsourcing facility which resulted in a lack of identification of scoring of the interior of the #3 cylinder rocker shaft …Improper maintenance by an outsourcing facility which resulted in a lack of identification of scoring of the interior of the #3 cylinder rocker shaft bosses. The scoring resulted in a fatigue fracture and subsequent permanent closure of both intake and exhaust valves. Contributing factors were the lack of a suitable landing site and trees. |
| Sep 20, 1998 | YUKON, OK | N6107K | Incident | substantial | The pilot's improper landing flare which resulted in a hard landing and her improper recovery procedures for a bounced landing. |
| Sep 19, 1998 | OROVILLE, CA | N19063 | Incident | substantial | Failure of the pilot to maintain proper clearance and subsequently striking a hangar door while taxiing to parking. |
| Sep 12, 1998 | BRADENTON, FL | N6080T | Incident | substantial | The loss of engine power for undetermined reasons. |
| Sep 05, 1998 | CADILLAC, MI | N3031J | Incident | substantial |
the pilot's inadequate evaluation of the wind condition which resulted in landing on the wrong runway. A factor associated with the accident was the …the pilot's inadequate evaluation of the wind condition which resulted in landing on the wrong runway. A factor associated with the accident was the tailwind. |
| Aug 24, 1998 | ATHENS, GA | N704HU | Incident | substantial | The student pilot's failure to maintain directional control during land roll out that resulted in the on ground collision. |
| Aug 22, 1998 | CUMBERLAND, MD | N7513G | Incident | substantial | The pilot in command's improper recovery from a bounced landing. |
| Aug 21, 1998 | LAMAR, MO | N1239Y | Incident | substantial | inadequate lubrication of the torque plate holes and torque pins by the mechanic who performed the airplane's last annual inspection. |
| Aug 10, 1998 | SANTA PAULA, CA | N704UV | Incident | substantial | Failure of the number one cylinder due to a fatigue crack that had originated from corrosion pits at the cooling fin. |
| Aug 09, 1998 | PHILIP, SD | N5413Q | Incident | substantial | the fuel exhaustion due to the pilot's inadequate preflight inspection. A factor was the soft field. |
| Jul 29, 1998 | YORBA LINDA, CA | N6377G | Incident | substantial |
An oil starvation failure of the engine due to the mechanic's inadequate maintenance installation and quality control procedures, which resulted in a …An oil starvation failure of the engine due to the mechanic's inadequate maintenance installation and quality control procedures, which resulted in a shop rag being inadvertently left inside the accessory case when the starter was changed 7 hours prior to the accident. |
| Jul 21, 1998 | LITCHFIELD, IL | N9251U | Incident | substantial | Loss of engine power due to an open exhaust valve and low cylinder compression. A related factor was the tailwind. |
| Jul 18, 1998 | FRANKFORT, IN | N22047 | Incident | substantial |
the improper maintenance installation by other maintenance personnel. Factors were a missing lubricating oil drain plug, the safety wire for the plug…the improper maintenance installation by other maintenance personnel. Factors were a missing lubricating oil drain plug, the safety wire for the plug and the roadway. |
| Jul 17, 1998 | ORMOND BEACH, FL | N704FE | Incident | substantial | The student pilot's failure to maintain directional control. |
| Jul 09, 1998 | VERO BEACH, FL | N9363U | Incident | substantial |
The failure of the pilot to obtain flying speed, and the delayed decision to abort the take-off, leading to a loss of control in flight, and the subse…The failure of the pilot to obtain flying speed, and the delayed decision to abort the take-off, leading to a loss of control in flight, and the subsequent collision with a ditch. |
| Jul 07, 1998 | OREGON CITY, OR | N6417T | Incident | substantial | The pilot's improper flare. |
| Jun 16, 1998 | COLLINSVILLE, OK | N7914Z | Incident | substantial | The pilot's failure to maintain directional control during landing roll. A factor was the pilot's diverted attention. |
| Jun 13, 1998 | TAFT, TX | N10519 | Incident | substantial |
The pilot's failure to ensure that there was adequate fuel for the planned flight on board the airplane during the preflight inspection which resulted…The pilot's failure to ensure that there was adequate fuel for the planned flight on board the airplane during the preflight inspection which resulted in a loss of engine power due to fuel exhaustion. A factor was the pilot's misjudgment of the glide distance during the forced landing which resulted in the airplane impacting objects short of the intended landing site. |
| Jun 02, 1998 | MENTONE, TX | N6486T | Incident | substantial | a partial loss of engine power for undetermined reasons, and the pilot's failure to maintain directional control during landing. |
| Jun 01, 1998 | NEWTON, KS | N714FB | Incident | substantial |
the pilot's inadequate preflight planning/preparation which led to fuel exhaustion and subsequent loss of engine power. Related factors were the pilo…the pilot's inadequate preflight planning/preparation which led to fuel exhaustion and subsequent loss of engine power. Related factors were the pilot became disoriented and a dark night. |
| May 31, 1998 | PEARLAND, TX | N19271 | Incident | substantial | The pilot's selection of the wrong runway/landing area. A factor was the lack of visual runway cues available to the pilot. |
| May 21, 1998 | GRIFFITH, IN | N2916J | Incident | substantial | The aircraft's speed not maintained by the pilot, which resulted in the aircraft stalling in close proximity to the ground. |
| May 03, 1998 | BENTON, KS | N6977S | Incident | substantial |
the pilot's failure to assure an adequate fuel supply to complete the flight by refueling the airplane en route resulting in fuel exhaustion. A facto…the pilot's failure to assure an adequate fuel supply to complete the flight by refueling the airplane en route resulting in fuel exhaustion. A factor was the hedgerow which was contacted during the landing and the dark night conditions. |
| Apr 25, 1998 | OROVILLE, CA | N3376J | Incident | substantial | The pilot's failure to maintain the proper glide path, and his inadequate compensation for wind conditions, which resulted in an undershoot. |
| Apr 19, 1998 | LUMBER BRIDGE, NC | N63582 | Incident | substantial | The pilot's delay in aborting a takeoff from a wet grass runway. |