Cessna 150 Safety Record
Complete NTSB accident and incident history. 3241 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| May 08, 1999 | MAYBELL, CO | N6128K | Incident | substantial | The pilot's inadvertent stall while maneuvering. Factors were the wind gusts weather conditions, and the high density altitude weather conditions. |
| Apr 22, 1999 | VANCOUVER, WA | N3510J | Incident | substantial | The failure of the pilot of the other aircraft to maintain clearance from the pilot's stationary aircraft. |
| Apr 18, 1999 | YUBA CITY, CA | N22710 | Incident | substantial |
A total loss of engine power resulting from the fatigue failure of a cylinder's exhaust valve. A contributing factor was the uneven terrain at the fo…A total loss of engine power resulting from the fatigue failure of a cylinder's exhaust valve. A contributing factor was the uneven terrain at the forced landing site. The reason for the fatigue could not be determined. |
| Mar 31, 1999 | LEONARDTOWN, MD | N8524J | Incident | substantial | The pilot's failure to maintain control of the airplane during a crosswind landing. |
| Mar 29, 1999 | PEMBROKE PINES, FL | N60476 | Incident | substantial | The pilot's inadequate in-flight/planning decision and his mismanagement of the fuel supply. |
| Mar 16, 1999 | FAIRBANKS, AK | N8620S | Incident | substantial | The loss of engine power for an undetermined reason. |
| Feb 20, 1999 | HILLSBORO, OR | N16058 | Incident | substantial | The pilot's failure to maintain directional control of the aircraft. A related factor was the crosswind condition. |
| Feb 14, 1999 | BATON ROUGE, LA | N6405K | Incident | substantial |
The pilot's failure to maintain an adequate approach airspeed which resulted in a excessive descent rate and hard landing and the pilot's failure to r…The pilot's failure to maintain an adequate approach airspeed which resulted in a excessive descent rate and hard landing and the pilot's failure to recover from a bounced landing. A factor was the pilot's lack of total experience. |
| Feb 06, 1999 | BURNT CHIMNEY, VA | N19186 | Incident | destroyed | The pilot's decision to land on a short runway with a strong tailwind, and his failure to obtain a proper touchdown point. |
| Feb 06, 1999 | HILLMAN, MI | N3332J | Incident | substantial | the pilot's misjudging crosswinds during landing roll. Factors were crosswinds and a snow and ice covered runway, and the snowbank. |
| Jan 20, 1999 | MIDDLETON, WI | N1956Z | Incident | substantial |
inadequate aircraft preflight by the pilot and the ice in the fuel system. A factor associated with the accident was the ravine which the airplane co…inadequate aircraft preflight by the pilot and the ice in the fuel system. A factor associated with the accident was the ravine which the airplane contacted during the forced landing. |
| Jan 19, 1999 | HILLSDALE, MI | N8142F | Incident | substantial | the pilot's disregarding preparation for the flight. Factors were a frozen landing gear wheel, and the snowbank. |
| Jan 10, 1999 | CONWAY, AR | N23303 | Incident | substantial | The loss of engine power due to carburetor ice during the approach to land. A factor was the lack of suitable terrain for the forced landing. |
| Jan 08, 1999 | MADISONVILLE, TX | N66464 | Incident | substantial |
The loss of engine power due to fuel exhaustion as result of the pilot's failure to refuel. A factor was the lack of suitable terrain for the forced l…The loss of engine power due to fuel exhaustion as result of the pilot's failure to refuel. A factor was the lack of suitable terrain for the forced landing. |
| Dec 24, 1998 | PEMBROKE PINES, FL | N252WM | Incident | substantial | The pilot's decision to abort the takeoff with insufficient runway remaining. |
| Dec 06, 1998 | EAST TROY, WI | N63563 | Incident | substantial | the student pilot's failure to maintain directional control of the airplane. Factors associated with the accident were the crosswind, and the ditch. |
| Dec 05, 1998 | ADJUNTAS, PR | N5957T | Incident | substantial | The loss of engine power due to the restricted movement of the intake and exhaust valves on number 3 cylinder. |
| Dec 03, 1998 | COLUMBIA, NC | N18022 | Incident | substantial | The failure of the #2 exhaust valve that resulted in the total loss of engine power. A factor is the lack of suitable emergency landing terrain. |
| Nov 20, 1998 | TOWER, MN | N66314 | Incident | substantial |
the student pilot's failure to maintain directional control of the airplane after landing. Factors contributing to this accident were the icy runway …the student pilot's failure to maintain directional control of the airplane after landing. Factors contributing to this accident were the icy runway and the snowbank. |
| Nov 06, 1998 | WINNSBORO, SC | N330JC | Incident | substantial | The pilot's improper landing flare that resulted in overload damage to the nose wheel assembly. |
| Nov 05, 1998 | WARRENSBURG, MO | N704LV | Incident | substantial |
the student pilot's inadequate flare and his failure to maintain directional control of the airplane. Factors associated with the accident were, the …the student pilot's inadequate flare and his failure to maintain directional control of the airplane. Factors associated with the accident were, the student's lack of total experience and the dirt bank which was contacted. |
| Oct 31, 1998 | WINTER HAVEN, FL | N6679F | Incident | substantial | The student pilot's improper landing flare resulting in a hard landing and ground loop. |
| Oct 11, 1998 | CLINTON, MD | N11951 | Incident | destroyed | The student pilot's improper flare and improper recovery from a bounced landing. |
| Oct 02, 1998 | WILEY FORD, WV | N9273U | Incident | substantial |
Was the failure of the pilot to maintain directional control during an unforecast change in wind velocity. Factors were the gusts and the lack of rec…Was the failure of the pilot to maintain directional control during an unforecast change in wind velocity. Factors were the gusts and the lack of recent experience for the pilot. |
| Sep 29, 1998 | FREELAND, WA | N5867C | Incident | substantial |
Failure of the number two intake valve rocker arm in fatigue, and overload of the nose landing gear assembly. Factors include a ditch encountered du…Failure of the number two intake valve rocker arm in fatigue, and overload of the nose landing gear assembly. Factors include a ditch encountered during the forced landing. |