Luscombe Safety Record
Complete NTSB accident and incident history. 433 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jan 16, 2025 | Omaha, NE | N71586 | Serious (1) | substantial | The pilot’s inadequate preflight inspection, which resulted in a total loss of engine power due to fuel exhaustion. |
| Dec 10, 2020 | Manvel, TX | N2238K | Serious (1) | substantial |
The pilot’s failure to maintain clearance from power lines during his attempted landing and his loss of situational awareness that led to him to misid…The pilot’s failure to maintain clearance from power lines during his attempted landing and his loss of situational awareness that led to him to misidentify a pipeline field for the landing airpark. |
| Jan 05, 2019 | Casa Grande, AZ | N71155 | Serious (1) | substantial |
The pilot's failure to maintain yaw control and his exceedance of the airplane’s critical angle of attack during an aborted landing, which resulted in…The pilot's failure to maintain yaw control and his exceedance of the airplane’s critical angle of attack during an aborted landing, which resulted in an aerodynamic stall. |
| Aug 31, 2018 | New Carlisle, OH | N2305K | Serious (1) | substantial | A total loss of engine power shortly after takeoff due to carburetor ice. |
| Jun 01, 2018 | Longview, TX | N72066 | Serious (1) | substantial |
The pilot's failure to use carburetor heat for takeoff, which resulted in an interruption of continuous fuel flow to the engine and a loss of engine p…The pilot's failure to use carburetor heat for takeoff, which resulted in an interruption of continuous fuel flow to the engine and a loss of engine power during climb. Also causal was the lack of required placarding warning of the need to use full carburetor heat on takeoff and landing. |
| Aug 13, 2016 | Marlboro, NJ | N71497 | Serious (1) | substantial | The pilot's inadequate in-flight fuel management, which resulted in fuel exhaustion and the subsequent total loss of engine power. |
| Jul 22, 2015 | Perry, OK | N2789K | Serious (1) | substantial | The pilot's incapacitation and subsequent loss of airplane control due to heat exhaustion. |
| Jul 19, 2014 | Rancho Cucamonga, CA | N77942 | Serious (1) | substantial |
The loss of engine power during cruise flight for reasons that could not be determined because postaccident examination revealed no anomalies that wou…The loss of engine power during cruise flight for reasons that could not be determined because postaccident examination revealed no anomalies that would have precluded normal operation. |
| Oct 11, 2010 | Clarrisa, MN | N72060 | Serious (1) | substantial | The partial loss of engine power for undetermined reasons. |
| Jan 18, 2010 | Springfield, TN | N2111K | Serious (1) | substantial | The student pilot's failure to maintain control of the airplane during a go-around after a bounced landing. |
| Oct 11, 2009 | Weeping Water, NE | N1536B | Serious (1) | substantial |
The pilot’s failure to maintain aircraft control resulting in a stall. Contributing to the accident was the stuck exhaust valve resulting in the parti…The pilot’s failure to maintain aircraft control resulting in a stall. Contributing to the accident was the stuck exhaust valve resulting in the partial loss of engine power. |
| Jun 19, 2009 | Chipley, FL | N41915 | Serious (1) | substantial |
A partial loss of power due to the use of automotive gasoline that contained ethanol, which was prohibited by the operating limitations. Contributing…A partial loss of power due to the use of automotive gasoline that contained ethanol, which was prohibited by the operating limitations. Contributing to the accident was the pilot/owner's failure to obtain and comply with the applicable operating limitations. |
| May 01, 2007 | Fruitport, MI | N1120B | Serious (2) | substantial | The flight instructor failed to use carburetor heat during takeoff in icing conditions. A factor was the power line pole. |
| Jun 24, 2006 | Bowling Green, MO | N2890K | Serious (1) | substantial |
The loss of engine power due to fatigue fracture of the number two cylinder exhaust valve during initial climb after takeoff. A contributing factor w…The loss of engine power due to fatigue fracture of the number two cylinder exhaust valve during initial climb after takeoff. A contributing factor was the unsuitable terrain (cornfield) encountered during the forced landing. |
| Oct 17, 2004 | Jasper, GA | N1491K | Serious (1) | substantial | The pilot's excessive braking during landing roll resulted in a nose over. |
| Oct 18, 2003 | Spanaway, WA | N1806K | Serious (1) | substantial |
The pilot's misjudgment of distance and altitude resulting in an undershoot of the runway and collision with a fence. A fence was a factor in the acc…The pilot's misjudgment of distance and altitude resulting in an undershoot of the runway and collision with a fence. A fence was a factor in the accident. |
| Jan 26, 2003 | Newport, ME | N1484B | Serious (1) | substantial | The fatigue failure of a the cylinder wall. |
| Dec 04, 2002 | Tekoa, WA | C-FIIF | Serious (1) | substantial |
The pilot's failure to maintain clearance from the terrain while attempting to fly a non-IFR equipped aircraft solely by reference to its instruments …The pilot's failure to maintain clearance from the terrain while attempting to fly a non-IFR equipped aircraft solely by reference to its instruments after the aircraft's windshield became coated with freezing rain in cruise flight. A factor was the pilot's improper inflight decision to continue VFR flight in an area where rain showers where taking place while ambient temperatures where indicated to be within one degree of freezing. Additional factors include freezing rain, an iced-over windshield, and tree-covered rising terrain. |
| Dec 25, 1999 | SAN LUIS, CO | N1941B | Serious (1) | substantial |
The pilot's inadequate in-flight decision, and the subsequent inadvertent stall/mush. Factors were the pilot's lack of total experience in mountain f…The pilot's inadequate in-flight decision, and the subsequent inadvertent stall/mush. Factors were the pilot's lack of total experience in mountain flying, the high density altitude, and downdraft weather conditions. |
| May 01, 1999 | CONROE, TX | N2638K | Serious (1) | substantial | The loss of engine power due to fuel starvation as a result of a blocked fuel vent. A factor was the lack of suitable terrain for the forced landing. |
| Apr 26, 1999 | KODIAK, AK | N45627 | Serious (1) | substantial |
The pilot's inadequate terrain clearance during the initial climb, and the inadvertent stall/spin during the turn to avoid terrain. A factor in this …The pilot's inadequate terrain clearance during the initial climb, and the inadvertent stall/spin during the turn to avoid terrain. A factor in this accident was the pilot exceeding the allowable maximum gross weight of the airplane. |
| Jun 24, 1995 | HAMPSHIRE, IL | N2086K | Serious (2) | substantial | the pilot's failure to attain liftoff speed. A factor in the accident was the ditch. |
| Mar 18, 1994 | WIMAUMA, FL | N71891 | Serious | — |
THE FAILURE OF THE PERSON REMOVING THE CHOCK TO MAINTAIN SUFFICIENT CLEARANCE FROM THE PROPELLER. A CONTRIBUTING FACTOR WAS THE TOTAL LACK OF EXPERIEN…THE FAILURE OF THE PERSON REMOVING THE CHOCK TO MAINTAIN SUFFICIENT CLEARANCE FROM THE PROPELLER. A CONTRIBUTING FACTOR WAS THE TOTAL LACK OF EXPERIENCE BY PERSON ON GROUND. |
| Nov 12, 1993 | GRIFFIN, GA | N822B | Serious (1) | substantial | THE PILOT'S FAILURE TO MAINTAIN AIRSPEED WHILE MANEUVERING FOLLOWING A LOSS OF ENGINE POWER FOR UNKNOWN REASONS. |
| Sep 01, 1993 | KIJIK RIVER, AK | N71585 | Serious (1) | substantial | THE PILOT'S FAILURE TO MAINTAIN A PROPER ALTITUDE DURING THE LOW PASS. |