Luscombe 8F Safety Record
Complete NTSB accident and incident history. 38 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Apr 13, 2025 | Punta Gorda, FL | N815B | Incident | substantial | The pilot’s failure to maintain direction control of the airplane during the landing roll. |
| Apr 30, 2023 | Palmer, TX | N1113B | Incident | substantial |
The installation of an unapproved rudder control cable, which resulted in a fatigue failure and subsequent loss of rudder control during cruise flight…The installation of an unapproved rudder control cable, which resulted in a fatigue failure and subsequent loss of rudder control during cruise flight. Contributing to the accident was the mechanic’s inadequate inspection of the rudder control system. |
| Jun 21, 2011 | McCall, ID | N1459B | Incident | substantial |
The pilot's failure to maintain adequate airspeed that resulted in a stall/mush. Contributing to the accident was the pilot's failure to maintain an a…The pilot's failure to maintain adequate airspeed that resulted in a stall/mush. Contributing to the accident was the pilot's failure to maintain an adequate spacing from the aircraft ahead of him. |
| Jun 10, 2010 | Shell Knob, MO | N9932C | Incident | substantial | A total loss of engine power for undetermined reasons. |
| Apr 04, 2007 | Ocala, FL | N882JB | Incident | substantial |
The failure of the left main axle during the landing roll, which resulted in the collapse of the left main landing gear. A crosswind on the landing r…The failure of the left main axle during the landing roll, which resulted in the collapse of the left main landing gear. A crosswind on the landing runway was a factor. |
| Nov 05, 2006 | Wellsville, KS | N26324 | Incident | substantial |
A loss of engine power due to the ingestion of the number 2 intake valve into its cylinder. Contributing factors included the pilot allowing the airs…A loss of engine power due to the ingestion of the number 2 intake valve into its cylinder. Contributing factors included the pilot allowing the airspeed and altitude to drop, making a safe landing not possible. |
| Jul 31, 2005 | Sturtevant, WI | N1841B | Incident | substantial | The pilot not obtaining/maintaining airplane control during the aborted takeoff. A factor was the berm. |
| Feb 21, 2005 | Kapolei, HI | N2248B | Incident | substantial |
the pilot's inadequate compensation for the quartering tailwind conditions, and his failure to maintain directional control of the airplane during lan…the pilot's inadequate compensation for the quartering tailwind conditions, and his failure to maintain directional control of the airplane during landing. Related factors were the tailwind and crosswind. |
| Jul 04, 2004 | Andover, NJ | N803B | Incident | substantial | The pilot's failure to maintain aircraft control during approach. A factor was windshear. |
| Nov 01, 2003 | Lawrenceburg, TN | N9929C | Incident | substantial |
The pilot's failure to maintain directional control on landing rollout resulting in the airplane veering to the right and collapsing the left main lan…The pilot's failure to maintain directional control on landing rollout resulting in the airplane veering to the right and collapsing the left main landing gear with a side load. |
| Sep 24, 2003 | Bremerton, WA | N9913C | Incident | substantial | Aircraft control was not maintained during the landing roll which resulted in the aircraft nosing over. |
| Jul 17, 2002 | Farmington, MO | N840B | Incident | substantial | The locked brake and the aircraft control not being possible due to the locked brake. |
| May 31, 2001 | Salem, OR | N1389B | Incident | substantial | Loss of engine power during cruise flight for an undetermined reason. A factor in the accident was tall grass in the landing area. |
| Jun 26, 1999 | NAMPA, ID | N1895B | Incident | substantial | Directional control was not maintained. Diverted attention was a factor. |
| Nov 04, 1997 | BOISE, ID | N1895B | Incident | substantial |
The student pilot's failure to maintain directional control due to excessive taxispeed. Pressure perceived by the student pilot to expedite clearing…The student pilot's failure to maintain directional control due to excessive taxispeed. Pressure perceived by the student pilot to expedite clearing the runway after landing in order to facilitate an aircraft departure was a contributing factor. |
| Jun 15, 1997 | NEW TOWN, PA | N1894B | Incident | substantial | The pilot's improper fuel management, which resulted in an intermittent fuel supply, and a loss of engine power. |
| Nov 29, 1996 | FLOYDADA, TX | N1907K | Incident | substantial | The pilot's inadequate compensation for the crosswind during landing. Factors were the crosswind and the locked left main wheel brake. |
| Aug 03, 1996 | DOUGLAS, AZ | N1616Z | Incident | substantial |
The pilot's failure to maintain directional control of the aircraft during the landing roll. A contributing factor was the pilot's inexperience in th…The pilot's failure to maintain directional control of the aircraft during the landing roll. A contributing factor was the pilot's inexperience in the type aircraft. |
| Oct 04, 1993 | BENTON, KS | N801B | Incident | substantial |
THE FAILURE OF THE STUDENT PILOT TO MAINTAIN DIRECTIONAL CONTROL AND PROPER RUNWAY ALIGNMENT DURING THE LANDING ROLL. THE PROXIMITY OF THE DITCH TO TH…THE FAILURE OF THE STUDENT PILOT TO MAINTAIN DIRECTIONAL CONTROL AND PROPER RUNWAY ALIGNMENT DURING THE LANDING ROLL. THE PROXIMITY OF THE DITCH TO THE RUNWAY WAS A RELATED FACTOR. |
| Sep 18, 1993 | FESTUS, MO | N840B | Incident | substantial | a fatigue failure of the tailwheel spring. |
| May 26, 1990 | MORGAN, UT | N1113B | Incident | substantial | PILOT'S IMPROPER USE OF THE BRAKES DURING LANDING ROLL. |
| May 21, 1989 | RAMSEY, MN | N2746K | Incident | substantial |
THE PASSENGERS INTERFERENCE WITH THE FLIGHT CONTROLS AND THE PILOT'S FAILURE TO MAINTAIN CONTROL OF THE AIRCRAFT. CONTRIBUTING TO THE SEVERITY OF THE …THE PASSENGERS INTERFERENCE WITH THE FLIGHT CONTROLS AND THE PILOT'S FAILURE TO MAINTAIN CONTROL OF THE AIRCRAFT. CONTRIBUTING TO THE SEVERITY OF THE ACCIDENT WAS THE DITCH LOCATED SHORT OF THE RUNWAY WHICH THE AIRCRAFT CONTACTED. |
| Mar 27, 1988 | LOMPOC, CA | N1374B | Incident | substantial | Investigation pending |
| Dec 23, 1984 | NEWBURG, MD | N836B | Incident | substantial | Investigation pending |
| Jul 16, 1982 | BELLEVILLE, MI | N5PL | Incident | substantial | Investigation pending |