Cessna Safety Record
Complete NTSB accident and incident history. 28016 events recorded from 1974 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jul 17, 2011 | Porthill, ID | N733BT | Incident | substantial | The pilot's failure to maintain clearance from a pole. |
| Jul 15, 2011 | Schlater, MS | N9996N | Incident | substantial | The pilot's loss of directional control during the takeoff roll, which resulted in a runway excursion. |
| Jul 10, 2011 | McKenzie Bridge, OR | N8343Z | Incident | substantial | The pilot's improper landing flare and inadequate recovery from a bounced landing. |
| Jul 09, 2011 | Lacassine, LA | N50575 | Incident | substantial | A total loss of engine power due to fuel exhaustion, as a result of the pilot's improper fuel planning. |
| Jul 06, 2011 | Baltimore, MD | N65659 | Incident | substantial | The student pilot's failure to maintain aircraft control following a bounced landing. |
| Jul 06, 2011 | Mesa, AZ | N2878S | Incident | substantial | The pilot's failure to maintain directional control during the go around. |
| Jul 04, 2011 | Orange Beach, AL | N109DP | Incident | substantial |
The operation of the airplane using unapproved fuels, which resulted in abnormal combustion and subsequent damage to the No. 3 cylinder. Contributing …The operation of the airplane using unapproved fuels, which resulted in abnormal combustion and subsequent damage to the No. 3 cylinder. Contributing to the accident was the inadequate 100-hour inspection because the mechanic failed to note the lack of placards by either fuel filler cap specifying the minimum automotive fuel grade and no alcohol allowed as specified by the installed STC’s. |
| Jul 04, 2011 | Plymouth, MA | N150ET | Incident | substantial |
A partial loss of engine power during initial climb due to a stuck cylinder valve, which resulted from excessive corrosion and carbon deposits on the …A partial loss of engine power during initial climb due to a stuck cylinder valve, which resulted from excessive corrosion and carbon deposits on the valve springs due to inadequate maintenance. |
| Jul 02, 2011 | Weirsdale, FL | N1953Z | Incident | substantial | The pilot's failure to maintain adequate clearance from the stopped trailer while taxiing. |
| Jul 01, 2011 | Cambridge, MD | N789EP | Incident | substantial | The student pilot's improper recovery from a bounced landing. |
| Jun 30, 2011 | Page, AZ | N80293 | Incident | substantial | The pilot's decision to take off with a gusty quartering tailwind. |
| Jun 30, 2011 | Stevensville, MD | N2888R | Incident | substantial | A total loss of engine power during initial climb for undetermined reasons. |
| Jun 27, 2011 | Price, UT | N674SP | Incident | substantial |
The pilot's decision to attempt a takeoff at a density altitude outside of the takeoff performance envelope of the aircraft along with using an aircra…The pilot's decision to attempt a takeoff at a density altitude outside of the takeoff performance envelope of the aircraft along with using an aircraft flap setting higher than the manufacture's recommended setting for takeoff. |
| Jun 26, 2011 | Olympia, WA | N5366J | Incident | substantial | The pilot's failure to maintain clearance from obstacles. |
| Jun 24, 2011 | Castroville, TX | N731ST | Incident | substantial | The pilot's failure to maintain obstacle clearance during the agricultural spraying flight. |
| Jun 24, 2011 | Palo Alto, CA | N222MF | Incident | substantial | A total loss of engine power for undetermined reasons during the landing approach over unsuitable terrain. |
| Jun 23, 2011 | Warrenton, VA | N3152U | Incident | substantial | The fatigue failure of the left main landing gear due to inadequate maintenance inspection that did not detect and correct corrosion pitting. |
| Jun 21, 2011 | Phoenix, AZ | N6160Q | Incident | substantial |
The mechanic's failure to properly secure the nose landing gear actuator push-pull tube to the landing gear door hinge clevis, which resulted in the g…The mechanic's failure to properly secure the nose landing gear actuator push-pull tube to the landing gear door hinge clevis, which resulted in the gear jamming and not fully retracting after takeoff. |
| Jun 20, 2011 | Soldotna, AK | N331AA | Incident | substantial | The pilot's failure to maintain pitch control resulting in an aerodynamic stall. |
| Jun 19, 2011 | Gulfport, MS | N54120 | Incident | — |
the Gulfport control tower local controller cleared two aircraft for takeoff from runways with intersecting departure flight paths without ensuring th…the Gulfport control tower local controller cleared two aircraft for takeoff from runways with intersecting departure flight paths without ensuring the first aircraft had passed the flight path intersection prior to clearing the second aircraft for takeoff. |
| Jun 19, 2011 | Santa Teresa, NM | N739ZN | Incident | substantial | The pilot's inadequate compensation for the wind condition, resulting in a runway excursion. |
| Jun 19, 2011 | North Adams, MA | N12477 | Incident | substantial | The pilot's inadequate visual lookout and subsequent failure to maintain clearance from a light pole while taxiing. |
| Jun 18, 2011 | Trinca, NJ | N714TX | Incident | substantial | The pilot's failure to maintain directional control, and the flight instructor's inadequate remedial action, which resulted in a ground-loop. |
| Jun 18, 2011 | Bedford Park, IL | N172NT | Incident | substantial | A loss of engine power due to a fractured push rod precipitated by a stuck exhaust valve. |
| Jun 18, 2011 | Truth or Consequences, NM | N735JY | Incident | substantial | The pilot's inability to control the airplane on take off. |