Cessna Safety Record
Complete NTSB accident and incident history. 28016 events recorded from 1974 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Apr 28, 2013 | Henderson, NV | N3483E | Incident | substantial |
The pilot’s inadequate preflight planning, including operating in excess of the maximum certified gross weight and center of gravity limits at a high …The pilot’s inadequate preflight planning, including operating in excess of the maximum certified gross weight and center of gravity limits at a high density altitude, which resulted in the airplane’s inability to maintain a positive rate of climb after takeoff. |
| Apr 28, 2013 | New Orleans, LA | N737FK | Incident | substantial | The pilot's failure to perform a steep climb before going around following a low pass for a banner tow pickup. |
| Apr 28, 2013 | Bethel, ME | N180VW | Incident | substantial | The pilot’s failure to maintain directional control during landing. |
| Apr 26, 2013 | Newburgh, NY | N5314C | Incident | substantial |
The pilot’s failure to maintain directional control when the brakes bound and a subsequent ground loop. Contributing to the accident was the inadequat…The pilot’s failure to maintain directional control when the brakes bound and a subsequent ground loop. Contributing to the accident was the inadequate maintenance of the brakes by the pilot/owner. |
| Apr 24, 2013 | Nenana, AK | N756DJ | Incident | substantial |
Ice accretion in the right main landing gear wheel brake during departure, which prevented the right main landing gear from rotating on landing and re…Ice accretion in the right main landing gear wheel brake during departure, which prevented the right main landing gear from rotating on landing and resulted in a runway excursion and subsequent impact with a snow bank. |
| Apr 23, 2013 | Americus, GA | N757GX | Incident | substantial |
The pilot’s delayed decision to terminate the practice approach during a simulated loss of engine power maneuver, which resulted in an inadvertent col…The pilot’s delayed decision to terminate the practice approach during a simulated loss of engine power maneuver, which resulted in an inadvertent collision with utility wires. |
| Apr 21, 2013 | Colorado Springs, CO | N538MA | Incident | substantial | The pilot’s improper recovery from a bounced landing. |
| Apr 20, 2013 | Reading, MI | N3682L | Incident | substantial | The partial loss of engine power due to the improper securing of the throttle linkage by maintenance personnel. |
| Apr 20, 2013 | Albuquerque, NM | N6955E | Incident | substantial | The pilot’s inability to maintain airplane control during taxi due to an inadvertent encounter with a dust devil. |
| Apr 20, 2013 | Stow, MA | N739CK | Incident | substantial | The pilot’s failure to maintain directional control while landing in gusty wind conditions. |
| Apr 18, 2013 | Corvallis, OR | N711BG | Incident | substantial |
The pilot's inadvertent selection and activation of the landing gear handle rather than the flap handle during the landing roll. Contributing to the a…The pilot's inadvertent selection and activation of the landing gear handle rather than the flap handle during the landing roll. Contributing to the accident was the pilot's decision to alter the configuration of the airplane before exiting the runway. |
| Apr 18, 2013 | Lancaster, SC | N76688 | Incident | substantial |
The pilot’s decision to land with a tailwind and his failure to turn off the carburetor heat during a go-around, which resulted in degraded engine per…The pilot’s decision to land with a tailwind and his failure to turn off the carburetor heat during a go-around, which resulted in degraded engine performance and the airplane’s subsequent collision with trees at the end of the runway. |
| Apr 16, 2013 | Luxembourg, LU | LX-FGL | Incident | substantial | Investigation pending |
| Apr 16, 2013 | Palatka, FL | N812F | Incident | substantial | The pilot’s failure to retract the landing gear after takeoff from a runway, and his subsequent water landing with the wheels extended. |
| Apr 15, 2013 | Caldwell, ID | N9685X | Incident | substantial | The pilot’s failure to lower the landing gear, which resulted in a gear-up hard landing. |
| Apr 08, 2013 | Columbus, GA | N46803 | Incident | substantial | The student pilot's improper recovery from a bounced landing. |
| Apr 07, 2013 | New Castle, VA | N92804 | Incident | substantial |
The pilot's failure to abort the takeoff after recognizing that the airplane was not accelerating properly, which led to an aerodynamic stall. The rea…The pilot's failure to abort the takeoff after recognizing that the airplane was not accelerating properly, which led to an aerodynamic stall. The reason for the lack of acceleration could not be determined because postaccident examinations did not reveal any anomalies that would have precluded normal operation. |
| Apr 07, 2013 | Cottonwood, ID | N2303Y | Incident | substantial | The pilot’s failure to see and avoid an object on the grass airstrip during the takeoff. |
| Apr 04, 2013 | Phoenix, AZ | N2166K | Incident | substantial |
The student pilot's excessive directional control inputs during the takeoff roll and the flight instructor's delayed and ineffective corrective action…The student pilot's excessive directional control inputs during the takeoff roll and the flight instructor's delayed and ineffective corrective actions, which resulted in the loss of airplane control. |
| Apr 04, 2013 | Miami, FL | N6141Q | Incident | substantial |
A partial loss of engine power due to the failure of the No. 3 exhaust valve. Contributing to the accident was the airplane operator’s failure to foll…A partial loss of engine power due to the failure of the No. 3 exhaust valve. Contributing to the accident was the airplane operator’s failure to follow the engine manufacturer’s recommended engine overhaul intervals. |
| Apr 01, 2013 | Fort Lauderdale, FL | VQ-TIN | Incident | substantial |
The disconnection of the nose landing gear actuator, which resulted in the subsequent collapse of the nose landing gear. Contributing to the accident …The disconnection of the nose landing gear actuator, which resulted in the subsequent collapse of the nose landing gear. Contributing to the accident was the repair station’s inadequate maintenance, postmaintenance inspection process, and oversight of the maintenance performed and the lack of communication between the repair station personnel, the operator, and the testing technician. |
| Apr 01, 2013 | Wonewoc, WI | N8033B | Incident | substantial | The restricted vented fuel cap and obstructed fuel vent lines, which resulted in a total loss of engine power due to fuel starvation. |
| Apr 01, 2013 | Brush Praire, WA | N4342U | Incident | substantial | The pilot's failure to maintain directional control during the landing flare. |
| Mar 30, 2013 | Bally, PA | N4601D | Incident | substantial | The pilot's failure to maintain directional control during the takeoff roll. |
| Mar 30, 2013 | Willoughby, OH | N1267G | Incident | substantial | A bird strike during a practice instrument approach in visual conditions. |