Cessna 310 Safety Record
Complete NTSB accident and incident history. 584 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Sep 26, 2010 | Boerne Stage, TX | N550JW | Incident | substantial | The pilot’s failure to ensure that the landing gear was extended prior to landing, resulting in a landing on the partially extended landing gear. |
| Aug 19, 2010 | LaGrange, IN | N6762X | Incident | substantial | The pilot did not maintain altitude due to his distracted attention to a vibration of unknown origin. |
| Jul 14, 2010 | El Monte, CA | N6909L | Incident | substantial | The pilot’s failure to maintain directional control during the takeoff ground roll. |
| Dec 12, 2009 | Pasco, WA | N2640C | Incident | substantial | The failure of the right main landing gear up-lock. |
| Jul 10, 2009 | Fort Worth, TX | N3106L | Incident | substantial | The failure of the pivot pin in the side brace of the right main landing gear resulting in the gear collapse during taxi for undetermined reasons. |
| Mar 18, 2009 | Ocala, FL | N6901L | Incident | substantial |
The right main landing gear collapse as a result of the pilot's improper flare during a previous landing. Contributing to the accident was the flight …The right main landing gear collapse as a result of the pilot's improper flare during a previous landing. Contributing to the accident was the flight instructor's inadequate supervision. |
| Sep 10, 2008 | Lake Placid, NY | N115CA | Incident | substantial |
The pilot's failure to observe the ongoing construction to the closed runway while landing. Contributing to the accident was flight service's failure …The pilot's failure to observe the ongoing construction to the closed runway while landing. Contributing to the accident was flight service's failure to brief the pilot of the closed runway. |
| Apr 11, 2008 | Roswell, NM | N7935Q | Incident | substantial | The airframe and powerplant mechanic's incorrect reassembly of the landing gear. |
| Dec 19, 2007 | Dunnellon, FL | N5811M | Incident | substantial |
The improper installation of the right main landing gear scissors by company maintenance personnel, resulting in the collapse of the right main landin…The improper installation of the right main landing gear scissors by company maintenance personnel, resulting in the collapse of the right main landing gear during takeoff. |
| Dec 19, 2007 | Phoenix, AZ | N5499J | Incident | substantial |
The pilot's selection of a wrong taxi route, inadequate visual lookout, failure to maintain separation from ground obstacles, and excessive taxi speed…The pilot's selection of a wrong taxi route, inadequate visual lookout, failure to maintain separation from ground obstacles, and excessive taxi speed. |
| Dec 13, 2007 | Hilton Head Island, SC | N310RV | Incident | substantial | The pilot's failure to maintain aircraft control during a go-around. |
| Aug 03, 2007 | Brownsburg, IN | N7749Q | Incident | substantial |
The pilot's poor in-flight planning to make an off airport precautionary landing and his failure to maintain clearance from the construction equipment…The pilot's poor in-flight planning to make an off airport precautionary landing and his failure to maintain clearance from the construction equipment during the landing roll. Contributing to the accident was the construction equipment. |
| Apr 27, 2007 | Hatch, NM | N3700G | Incident | substantial |
The pilot's inattentiveness to the fuel flow and fuel selector valve position resulting in fuel starvation. Contributing factors were the pilot's fail…The pilot's inattentiveness to the fuel flow and fuel selector valve position resulting in fuel starvation. Contributing factors were the pilot's failure to follow proper engine failure procedures, and the pilot's improper in-flight planning and decision making. |
| Jan 31, 2007 | Atlantic City, NJ | N20SS | Incident | substantial | The inoperative safe gear indicator light switch. Contributing to the accident was the pilot hand-cranking the landing gear past the physical stop. |
| Dec 06, 2006 | Lake Stevens, WA | N6640B | Incident | substantial | The collapse of the main landing gear for an undetermined reason while taxiing from landing. |
| Oct 27, 2006 | Lake Havasu Cit, AZ | N56MB | Incident | substantial | the pilot's failure to extend the landing gear prior to touchdown. |
| Sep 14, 2006 | Kennett, MO | N5858M | Incident | substantial |
Separation of the left main landing gear torque link during landing resulting in a loss of control and runway excursion. Contributing factors were a …Separation of the left main landing gear torque link during landing resulting in a loss of control and runway excursion. Contributing factors were a failure to comply with the airframe manufacturer's service bulletin, and the pilot's inability to maintain directional control after the torque link separation. |
| May 10, 2006 | Allentown, PA | N1788H | Incident | substantial | The pilot's failure to lower the landing gear during landing. |
| Apr 19, 2006 | Billings, MT | N954EA | Incident | substantial | Collapse of the right main landing gear during the landing roll for an undetermined reason. |
| Apr 15, 2006 | Finleyville, PA | N93AC | Incident | substantial | The pilot's misjudged distance/speed during final approach, which resulted in an undershoot and hard landing. |
| Apr 12, 2006 | Brooksville, FL | N6981L | Incident | substantial |
The mechanic's improper maintenance that resulted in the right main landing gear's separation from the airplane and an inadvertent loss of control dur…The mechanic's improper maintenance that resulted in the right main landing gear's separation from the airplane and an inadvertent loss of control during landing. |
| Apr 03, 2006 | Lincoln, CA | N5096Q | Incident | substantial | The collapse of the nose gear due to an out of tolerance nose gear over center adjustment. |
| Jan 18, 2006 | Destin, FL | N4196Q | Incident | substantial |
The down limit switch, which operates the landing gear mechanical stop, was bent in the up position and allowed the gear motor to continued to run, ca…The down limit switch, which operates the landing gear mechanical stop, was bent in the up position and allowed the gear motor to continued to run, causing the gearbox to over-travel, pull on the landing gear rods, and retract the landing gear. |
| Jan 15, 2006 | Griffith, IN | N141DE | Incident | substantial | The overload failure of the right main landing gear locking mechanism due to undetermined reasons. |
| Jan 09, 2006 | St. Charles, MO | N310CK | Incident | substantial |
The in-flight collision with a duck during cruise flight resulting in a ruptured fuel tank and the strobe/light assembly electrical short resulting in…The in-flight collision with a duck during cruise flight resulting in a ruptured fuel tank and the strobe/light assembly electrical short resulting in a fire to the right wing tip tank. Contributing factors were the dusk light conditions. |