Cessna 310 Safety Record
Complete NTSB accident and incident history. 584 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Mar 11, 1992 | TUSCALOOSA, AL | N87355 | Incident | substantial | THE INSTRUCTOR'S INADEQUATE SUPERVISION AND THE STUDENT PILOT'S FAILURE TO FOLLOW INSTRUCTIONS. |
| Feb 25, 1992 | UNIONVILLE, PA | N6928L | Fatal (1) | destroyed |
THE PILOT DID NOT FOLLOW THE PUBLISHED IFR PROCEDURES AND ALLOWED THE AIRPLANE TO DESCEND TO AN ALTITUDE INSUFFICIENT TO CLEAR THE TERRAIN. FACTORS WH…THE PILOT DID NOT FOLLOW THE PUBLISHED IFR PROCEDURES AND ALLOWED THE AIRPLANE TO DESCEND TO AN ALTITUDE INSUFFICIENT TO CLEAR THE TERRAIN. FACTORS WHICH CONTRIBUTED TO THE ACCIDENT WERE: THE PILOT'S APPREHENSION DUE TO THE LOW FUEL STATE, THE DARK NIGHT, ADVERSE WEATHER, AND THE MOUNTAINOUS TERRAIN. |
| Jan 14, 1992 | HONOLULU, HI | N787AM | Fatal (5) | destroyed |
THE PILOT'S CONTINUATION OF VFR FLIGHT INTO INSTRUMENT METEOROLOGICAL CONDITIONS RESULTING IN SPATIAL DISORIENTATION AND LOSS OF AIRCRAFT CONTROL. FAC…THE PILOT'S CONTINUATION OF VFR FLIGHT INTO INSTRUMENT METEOROLOGICAL CONDITIONS RESULTING IN SPATIAL DISORIENTATION AND LOSS OF AIRCRAFT CONTROL. FACTORS WHICH CONTRIBUTED TO THE ACCIDENT WERE: THE ADVERSE WEATHER CONDITIONS AND THE PILOT'S FAILURE TO OBTAIN AN ADEQUATE WEATHER BRIEFING BEFORE FLIGHT. |
| Dec 02, 1991 | HAMILTON, TX | N6890T | Serious (1) | substantial |
THE INADVERTEND ENCOUNTER WITH ICING CONDITIONS. FACTORS WERE THE UNAVAILABILITY OF AN AIRPORT WEATHER OBSERVATION FACILITY AND THE DETERIORATED AIRCR…THE INADVERTEND ENCOUNTER WITH ICING CONDITIONS. FACTORS WERE THE UNAVAILABILITY OF AN AIRPORT WEATHER OBSERVATION FACILITY AND THE DETERIORATED AIRCRAFT PERFORMANCE. |
| Nov 22, 1991 | SOUTH ST PAUL, MN | N35H | Incident | substantial | THE INADEQUATE DESIGN OF THE PROPELLER HUB ASSEMBLY WHICH RESULTED IN METAL FATIGUE AND PROPELLER BLADE SEPARATION DURING INITIAL CLIMBOUT. |
| Nov 16, 1991 | WALLER, TX | N6704T | Fatal (2) | destroyed |
THE LOSS OF DIRECTIONAL CONTROL AS RESULT OF THE VELOCITY MINIMUM CONTROL AIRSPEED NOT BEING MAINTAINED. A FACTOR WAS THAT THE MANEUVER WAS INITIATED …THE LOSS OF DIRECTIONAL CONTROL AS RESULT OF THE VELOCITY MINIMUM CONTROL AIRSPEED NOT BEING MAINTAINED. A FACTOR WAS THAT THE MANEUVER WAS INITIATED AT AN INADEQUATE ALTITUDE TOO LOW FOR THE PILOT TO RECOVER. |
| Sep 20, 1991 | SUGAR GROVE, IL | N300RA | Incident | substantial |
THE BUCKLED NOSE LANDING GEAR RETRACTION/EXTENSION GEAR DRIVE TUBE. A FACTOR IN THE ACCIDENT WAS THE PILOT IN COMMAND NOT HAVING THE LANDING GEAR INSP…THE BUCKLED NOSE LANDING GEAR RETRACTION/EXTENSION GEAR DRIVE TUBE. A FACTOR IN THE ACCIDENT WAS THE PILOT IN COMMAND NOT HAVING THE LANDING GEAR INSPECTED AT THE INTERVAL RECOMMENDED BY THE MANUFACTURER. |
| Sep 02, 1991 | CORVALLIS, OR | N6788X | Incident | substantial |
A DISCONNECTED AIR INDUCTION LINE, AND THE PILOT'S INFLIGHT DECISION TO EXECUTE A 180 DEGREE TURN BACK TO THE AIRPORT. HIS LACK OF EXPERIENCE IN MULTI…A DISCONNECTED AIR INDUCTION LINE, AND THE PILOT'S INFLIGHT DECISION TO EXECUTE A 180 DEGREE TURN BACK TO THE AIRPORT. HIS LACK OF EXPERIENCE IN MULTI-ENGINE AIRCRAFT, HIS OVERALL LACK OF FAMILIARITY AND LACK OF RECENT EXPERIENCE IN THE TYPE AIRCRAFT WERE FACTORS IN THE ACCIDENT. |
| Aug 10, 1991 | PLATTSMOUTH, NE | N4827B | Incident | substantial | IMPROPER MAINTENANCE BY THE OWNER/PILOT. A FACTOR RELATED TO THE ACCIDENT WAS THE BUILT-UP OF CORROSION ON HE LANDING GEAR RETRACTION SYSTEM. |
| Jun 23, 1991 | FREDERICK, MD | N8631G | Incident | substantial | THE PILOT OF THE OTHER AIRCRAFT FAILED TO MAINTAIN ADEQUATE CLEARANCE WITH A PARKED AIRCRAFT. |
| Jun 06, 1991 | FORT WAYNE, IN | N3337X | Incident | substantial | THE IMPROPER INSTALLATION OF A BEARING BY MAINTENANCE PERSONNEL. |
| Jun 01, 1991 | WESTERLY, RI | N3227A | Incident | substantial |
IMPROPER INSTALLATION OF THE RIGHT PROPELLER WHICH RESULTED IN THREAD FAILURE IN THE PROPELLER HUB AND SEPARATION OF THE PROPELLER IN FLIGHT. A FACTO…IMPROPER INSTALLATION OF THE RIGHT PROPELLER WHICH RESULTED IN THREAD FAILURE IN THE PROPELLER HUB AND SEPARATION OF THE PROPELLER IN FLIGHT. A FACTOR RELATED TO THE ACCIDENT WAS THE RIGHT PROPELLER STRIKING THE RIGHT MAIN LANDING GEAR CAUSING ITS SEPARATION FROM THE AIRPLANE AS THE PROPELLER DEPARTED THE AIRPLANE. |
| May 07, 1991 | KENEFIC, OK | UNREG | Fatal (1) | destroyed |
IMPROPER PLANNING/DECISION BY THE PILOTS OF BOTH AIRCRAFT, AND THE MITSUBISHI PILOT'S MISJUDGMENT OF HIS POSITION, WHILE ATTEMPTING TO FLY FORMATION A…IMPROPER PLANNING/DECISION BY THE PILOTS OF BOTH AIRCRAFT, AND THE MITSUBISHI PILOT'S MISJUDGMENT OF HIS POSITION, WHILE ATTEMPTING TO FLY FORMATION AT NIGHT WITH AN AIRCRAFT THAT DID NOT HAVE ALL NAVIGATION LIGHTS OPERATIVE. FACTORS RELATED TO THE ACCIDENT WERE: BOTH PILOT'S LACK OF TRAINING IN THE TYPE OF OPERATION, DARKNESS, INOPERATIVE NAVITGATION (TAIL) LIGHT ON THE CESSNA 310, AND THE LACK OF VISUAL PERCEPTION THAT WOULD HAVE BEEN AVAILABLE TO THE MITSUBISHI PILOT. |
| May 01, 1991 | CHRISTIANSBURG, VA | N6632T | Minor | substantial | INADEQUATE MAINTENANCE. CONTRIBUTING WAS AN OBSTRUCTED AIR FILTER. |
| Jan 23, 1991 | BRUNSWICK, GA | N3602D | Fatal (1) | destroyed | THE INCAPACITATION OF THE PILOT. |
| Dec 29, 1990 | NEW SMYRNA BCH, FL | N4808B | Serious (1) | destroyed |
THE PILOT-IN-COMMAND/MECHANIC REVERSAL OF THE AILERON CONTROL CABLES ON THE SPROCKET DURING INSTALLATION. THIS RESULTED IN AN IN FLIGHT LOSS OF CONTRO…THE PILOT-IN-COMMAND/MECHANIC REVERSAL OF THE AILERON CONTROL CABLES ON THE SPROCKET DURING INSTALLATION. THIS RESULTED IN AN IN FLIGHT LOSS OF CONTROL ON TAKEOFF, UNCONTROLLED DESCENT, AND IN FLIGHT COLLISION WITH TERRAIN. |
| Dec 26, 1990 | WINDSOR, SC | N2251Q | Incident | substantial |
FAILURE OF THE OWNER OF THE PRIVATE SOD AIRPORT TO PROPERLY MAINTAIN THE RUNWAY, WHICH PRECIPITATED THE LOSS OF CONTROL OF THE AIRPLANE DURING THE LAN…FAILURE OF THE OWNER OF THE PRIVATE SOD AIRPORT TO PROPERLY MAINTAIN THE RUNWAY, WHICH PRECIPITATED THE LOSS OF CONTROL OF THE AIRPLANE DURING THE LANDING ROLL. |
| Sep 24, 1990 | COLORADO SPRING, CO | N3132L | Serious (1) | substantial |
THE LOSS OF POWER ON ONE ENGINE DUE TO EXCESSIVE FUEL PRESSURE AND THE PILOT'S FEATHERING OF THE WRONG PROPELLER. FACTOR(S) WERE: OPERATION OF AIRCRAF…THE LOSS OF POWER ON ONE ENGINE DUE TO EXCESSIVE FUEL PRESSURE AND THE PILOT'S FEATHERING OF THE WRONG PROPELLER. FACTOR(S) WERE: OPERATION OF AIRCRAFT WITH KNOWN DEFICIENCIES BY PILOT AND OPERATOR. |
| Jul 15, 1990 | HYANNIS, MA | N4855A | Incident | destroyed | A HARD LANDING DUE TO THE PILOT STALLING THE AIRPLANE DURING THE LANDING FLARE. CONTRIBUTING TO THIS ACCIDENT WAS GUSTY WIND CONDITIONS. |
| Jul 11, 1990 | MANSFIELD, OH | N3463G | Incident | substantial |
AN UNAVOIDABLE COLLISION WITH A DEER WHILE TAKING OFF WHICH BENT THE DRAG BRACE AND PREVENTED IT FROM LOCKING. FACTORS RELATED TO THE ACCIDENT WERE TH…AN UNAVOIDABLE COLLISION WITH A DEER WHILE TAKING OFF WHICH BENT THE DRAG BRACE AND PREVENTED IT FROM LOCKING. FACTORS RELATED TO THE ACCIDENT WERE THE NIGHT CONDITIONS WHICH REDUCED THE PILOTS VISIBILITY TO THE ILLUMINATED AREA OF THE LANDING LIGHTS. |
| Jul 04, 1990 | COLLEGE STATION, TX | N7546Q | Minor | substantial | THE PIC'S IMPROPER FUEL TANK SELECTION, ALLOWING BOTH ENGINE TO QUIT DUE TO FUEL STARVATION. |
| Jun 22, 1990 | MORAINE, OH | N522S | Incident | substantial |
THE PILOT-IN-COMMAND'S FAILURE TO MAINTAIN ADEQUATE GROUND CLEARANCE DURING HIS APPROACH TO LANDING. CONTRIBUTING FACTORS WERE REDUCED VISIBILITY IN F…THE PILOT-IN-COMMAND'S FAILURE TO MAINTAIN ADEQUATE GROUND CLEARANCE DURING HIS APPROACH TO LANDING. CONTRIBUTING FACTORS WERE REDUCED VISIBILITY IN FOG AND RAIN. |
| Jun 05, 1990 | ALBANY, OR | N6647B | Incident | substantial | THE PILOT'S FAILURE TO EXTEND THE LANDING GEAR BEFORE LANDING, WHEN HE BECAME DISTRACTED BY A CHANGE IN HIS NORMAL ROUTINE. |
| May 28, 1990 | OGDEN, UT | N8148M | Incident | substantial | THE FAILURE OF THE MAIN GEAR LOCKING MECHANISM. |
| May 24, 1990 | SEDONA, AZ | N161A | Minor | substantial | THE PILOT SELECTED THE WRONG RUNWAY, AND PROPER TOUCH DOWN POINT WAS NOT ATTAINED. |