Cessna 210M Safety Record
Complete NTSB accident and incident history. 65 events recorded from 1982 to 2023.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| May 04, 2023 | Pasco, WA | N777CF | Incident | substantial |
Improper maintenance on the fuel outlet line to the fuel servo, which resulted in the line partially separating from the fuel outlet fitting and the s…Improper maintenance on the fuel outlet line to the fuel servo, which resulted in the line partially separating from the fuel outlet fitting and the subsequent fuel starvation and total loss of engine power. |
| Jul 28, 2013 | Shirley, NY | N450EM | Incident | substantial | The pilot's loss of control during an aborted takeoff as a result of his failure to properly configure the elevator trim prior to flight. |
| Nov 28, 2005 | Kirbyville, TX | N761FL | Incident | substantial | The total loss of engine power for undetermined reasons. A contributing factor was the lack of suitable terrain for the forced landing. |
| Oct 10, 2004 | Salida, CO | N732TE | Incident | substantial |
The pilot's inadequate preflight planning which failed to determine the fuel supply was inadequate resulting in fuel exhaustion and the loss of engine…The pilot's inadequate preflight planning which failed to determine the fuel supply was inadequate resulting in fuel exhaustion and the loss of engine power. |
| Jul 14, 2004 | Quarryville, PA | N6043N | Incident | substantial |
Improper maintenance performed on the airplane, which resulted in a total electrical failure during cruise flight in IMC, and a subsequent precautiona…Improper maintenance performed on the airplane, which resulted in a total electrical failure during cruise flight in IMC, and a subsequent precautionary landing. A factor in the accident was the low ceiling. |
| Jun 23, 2003 | Carlisle, AR | N9TK | Incident | substantial |
The pilot's improper in-flight decision to descend for landing, at night, without the runway environment insight. Contributing factors were the pilot…The pilot's improper in-flight decision to descend for landing, at night, without the runway environment insight. Contributing factors were the pilot's disorientation, the embankment and the dark night condition. |
| Dec 04, 2002 | CINCINNATI, OH | N7660E | Incident | substantial |
Rupture of the left side, landing gear down hydraulic line due to repeated contact with the aileron cable, which resulted in a loss of hydraulic press…Rupture of the left side, landing gear down hydraulic line due to repeated contact with the aileron cable, which resulted in a loss of hydraulic pressure, a partial extension of the main landing gear, and the inability to utilize the landing gear hand pump. |
| Aug 07, 1998 | ALBUQUERQUE, NM | N732RD | Incident | substantial | A power loss for reasons undetermined. A factor was unsuitable terrain on which to make a forced landing. |
| Apr 03, 1997 | TROY, AL | N761VX | Incident | substantial |
The pilot's failure to obtain the proper touchdown point during an emergency landing resulting in an overrun and subsequent nose over. A factor in the…The pilot's failure to obtain the proper touchdown point during an emergency landing resulting in an overrun and subsequent nose over. A factor in the accident was a reported partial loss of engine power for undetermined reasons. |
| Aug 21, 1996 | OPA LOCKA, FL | N732ST | Incident | substantial |
the pilot's improper fuel management, which resulted in a loss of engine power due to fuel starvation, a forced landing, and subsequent in flight coll…the pilot's improper fuel management, which resulted in a loss of engine power due to fuel starvation, a forced landing, and subsequent in flight collision with terrain. The lack of suitable terrain for a forced landing was a related factor. |
| Apr 26, 1996 | MERIDIAN, MS | N722PD | Incident | substantial |
previous engine damage; failure of the pilot of the previous flight to report to the operator and/or mechanics that the engine had been operated with …previous engine damage; failure of the pilot of the previous flight to report to the operator and/or mechanics that the engine had been operated with low (or no) oil pressure; inadequate maintenance/inspection after most of the oil had leaked from the engine oil system during the previous flight; oil starvation; and subsequent failure of the #5 connecting rod. Factors relating to the accident were: the previous oil filter leak and loss of oil pressure. |
| Apr 06, 1996 | EVERGLADES CITY, FL | N700RP | Incident | substantial | the pilot's excessive airspeed and misjudgment of the landing distance. A factor was the right brake not working due to a hydraulic leak. |
| Dec 19, 1993 | FESTUS, MO | N761AG | Incident | substantial | IMPROPER PLANNING/DECISION BY THE PILOT. FACTORS RELATED TO THE ACCIDENT WERE: THE ICY RUNWAY, CROSSWIND AND SNOWBANK. |
| Sep 02, 1992 | SMITHFIELD, NC | N6979B | Incident | substantial |
THE PILOT'S OPERATION OF THE AIRPLANE WITH KNOWN ELECTRICAL DEFICIENCIES WHICH RESULTED IN A FAILURE OF THE LANDING GEAR HYDRAULIC POWERPACK. THE PI…THE PILOT'S OPERATION OF THE AIRPLANE WITH KNOWN ELECTRICAL DEFICIENCIES WHICH RESULTED IN A FAILURE OF THE LANDING GEAR HYDRAULIC POWERPACK. THE PILOT ALSO FAILED TO FOLLOW EMERGENCY PROCEDURES FOR LOWERING THE LANDING GEAR. FACTORS WERE AN INOPERATIVE ALTERNATOR AND A WEAK BATTERY. |
| Dec 11, 1991 | PALO ALTO, CA | N761VB | Incident | substantial | AN ENGINE POWER LOSS DUE TO A PARTIAL BLOCKAGE OF THE FUEL SELECTOR VALVE WITH DEBRIS. |
| Nov 30, 1991 | ZEPHYRHILLS, FL | N9064M | Incident | substantial |
IMPROPER PLACEMENT OF THE FUEL SELECTOR BY THE PILOT-IN-COMMAND RESULTING IN THE TOTAL LOSS OF ENGINE POWER DUE TO FUEL STARVATION. CONTRIBUTING TO T…IMPROPER PLACEMENT OF THE FUEL SELECTOR BY THE PILOT-IN-COMMAND RESULTING IN THE TOTAL LOSS OF ENGINE POWER DUE TO FUEL STARVATION. CONTRIBUTING TO THE ACCIDENT WAS AN INCORRECT FUEL QUANTITY GAGE, THE DARK NIGHT CONDITION, AND UNSUITABLE TERRAIN ENCOUNTERED. |
| Jan 05, 1991 | LUTZ, FL | N823AR | Incident | minor |
FUEL LINE CHAFING, AND IN-FLIGHT FIRE CAUSED BY SHORTING OF THE ELECTRICAL SYSTEM WHICH RESULTED IN A FORCED LANDING WITH THE LANDING GEAR NOT EXTENDE…FUEL LINE CHAFING, AND IN-FLIGHT FIRE CAUSED BY SHORTING OF THE ELECTRICAL SYSTEM WHICH RESULTED IN A FORCED LANDING WITH THE LANDING GEAR NOT EXTENDED. |
| Jan 12, 1990 | OCALA, FL | N9064M | Incident | substantial | SEPARATION OF THE THROTTLE PLATE, DUE TO IMPROPER SECURING OF THE ATTACH SCREWS DURING AN OVERHAUL. |
| Oct 11, 1988 | ORLANDO, FL | N9064M | Incident | minor | Investigation pending |
| Jul 10, 1988 | INDIANAPOLIS, IN | N210WP | Incident | substantial | Investigation pending |
| Jun 20, 1988 | TRES PINOS, CA | N732KS | Incident | substantial | Investigation pending |
| Mar 01, 1988 | ORLANDO, FL | N823AR | Incident | minor | Investigation pending |
| Jun 14, 1987 | LA PORTE, IN | N761Q | Incident | substantial | Investigation pending |
| Feb 28, 1986 | WHILE LAKE TWP., MI | N761VX | Incident | substantial | Investigation pending |
| Nov 19, 1985 | FT.LAUDERDALE, FL | N823AR | Incident | substantial | Investigation pending |