Cessna 210 Safety Record
Complete NTSB accident and incident history. 819 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jul 20, 2000 | LUBBOCK, TX | N3996Y | Minor | substantial | The pilot's improper aircraft handling as a result of his alcohol impairment. |
| Jun 16, 2000 | LOUISVILLE, KY | N485CA | Minor | substantial | The pilot's improper operation of the fuel selector. |
| Mar 02, 2000 | MACOMB, IL | N9552T | Minor | substantial |
the inadequate maintenance inspection prior to the ferry flight by the pilot/mechanic rated passenger who endorsed the airplane as airworthy, the shif…the inadequate maintenance inspection prior to the ferry flight by the pilot/mechanic rated passenger who endorsed the airplane as airworthy, the shift in the number two main bearing left half, and the fractured crankshaft. A factor was the rough/uneven terrain and the ferry permit's procedures not followed by the pilot in command. |
| Feb 08, 2000 | GLENDALE, AZ | N4946U | Minor | substantial |
the pilot's attempt to go-around with inadequate altitude and airspeed available, resulting in a power demand that exceeded the capability of the airc…the pilot's attempt to go-around with inadequate altitude and airspeed available, resulting in a power demand that exceeded the capability of the aircraft. The fully extended gear and flaps were factors in this accident. |
| Nov 07, 1999 | ROCHESTER, IN | N8235M | Minor | substantial | the pilot did not obtain the proper touchdown point. Factors included the closed runway and the culvert. |
| Aug 27, 1999 | GRAPEVINE, TX | N6657X | Minor | substantial | The pilot's failure to maintain directional control of the aircraft during landing. |
| Apr 05, 1999 | EL MONTE, CA | N2340F | Minor | substantial |
A loss of engine power due to the fatigue failure of the mixture control cable, which was due to the improper installation and adjustment of the cable…A loss of engine power due to the fatigue failure of the mixture control cable, which was due to the improper installation and adjustment of the cable 99 hours prior to the accident. |
| Feb 12, 1999 | LAKE PLACID, FL | N5874F | Minor | substantial |
a total loss of engine power due to an in-flight separation of the crankshaft, caused by a fatigue crack that originated from the aft fillet radius of…a total loss of engine power due to an in-flight separation of the crankshaft, caused by a fatigue crack that originated from the aft fillet radius of the No. 2 main journal, resulting in a forced landing in a field and impact with a tree. |
| Jan 13, 1999 | HALLANDALE BEAC, FL | N5458A | Minor | substantial | The loss of engine power for undetermined reasons. |
| Feb 23, 1998 | LAFAYETTE, LA | N7354M | Minor | substantial |
The unsecured squat switch wires located in the nose gear that were crimped (damaged) when the landing gear was retracted and shorted, resulting in an…The unsecured squat switch wires located in the nose gear that were crimped (damaged) when the landing gear was retracted and shorted, resulting in an in-flight fire. A factor was the failure of the landing gear to extend during the emergency descent/landing. |
| Jan 04, 1998 | COMPTON, CA | N9406X | Minor | substantial |
The failure of maintenance personnel to adequately inspect the aircraft during an annual inspection to detect a chafed and leaking engine fuel supply …The failure of maintenance personnel to adequately inspect the aircraft during an annual inspection to detect a chafed and leaking engine fuel supply line. |
| Jun 13, 1997 | WAYCROSS, GA | N1817F | Minor | substantial |
the private pilot's failure to maintain airspeed, while maneuvering in an attempt to reverse direction, which resulted in an inadvertent stall, and su…the private pilot's failure to maintain airspeed, while maneuvering in an attempt to reverse direction, which resulted in an inadvertent stall, and subsequent in-flight collision with terrain. |
| Nov 07, 1996 | ELK GROVE, CA | N30115 | Minor | substantial | loss of engine power for undetermined reason(s) after takeoff. The lack of maintenance/annual inspection was a related factor. |
| Oct 11, 1996 | TRUCKEE, CA | N9403X | Minor | substantial | a total loss of engine power for undetermined nonmechanical reasons. |
| Jul 05, 1996 | BOSTON, MA | N131AC | Minor | substantial | a fracture failure of the crankcase, which resulted in separation of the number five cylinder, loss of engine power, and a ditched landing. |
| Jul 25, 1995 | CODY, WY | N9492T | Minor | substantial | THE PILOT'S FAILURE TO REFUEL WHICH RESULTED IN A LOSS OF POWER DUE TO FUEL EXHAUSTION. |
| Jun 30, 1995 | TRUCKEE, CA | N300EW | Minor | substantial | fuel exhaustion due to the pilot's inadequate preflight fuel planning, and his failure to refuel the aircraft while en route. |
| Jul 31, 1994 | FLUSHING, MI | N90074 | Minor | substantial | the pilot's improper touchdown position on the runway. A factor associated with the accident is the moving vehicle on the adjacent road. |
| Jun 21, 1994 | BARTOW, FL | N9992Y | Minor | substantial |
The pilot-in-command's failure to maintain a visual lookout during a forced landing resulting in an in-flight collision with wires. Contributing to th…The pilot-in-command's failure to maintain a visual lookout during a forced landing resulting in an in-flight collision with wires. Contributing to the accident was the total loss of engine power due to the pilot's improper fuel consumption calculations, and unfamiliarity of the airplanes fuel system resulting in fuel exhaustion. |
| Mar 15, 1994 | NASHVILLE, TN | N732HA | Minor | substantial | A LOSS OF ENGINE POWER FOR UNDETERMINED REASONS. |
| Jul 09, 1993 | WEST BEND, WI | N50RD | Minor | substantial | THE INADEQUATE PREFLIGHT BY PILOT-IN-COMMAND. A FACTOR WAS THE ROUGH TERRAIN. |
| May 04, 1993 | APEX, NC | N761CQ | Minor | substantial | The pilot's inaccurate fuel consumption calculations which resulted in fuel exhaustion. |
| Mar 05, 1993 | MARCO, FL | N29WW | Minor | substantial |
THE PILOT-IN-COMMAND'S FAILURE TO ENSURE THE AIRCRAFT CONTAINED ADEQUATE FUEL FOR THE FLIGHT, RESULTING IN LOSS OF ENGINE POWER DUE TO FUEL EXHAUSTION…THE PILOT-IN-COMMAND'S FAILURE TO ENSURE THE AIRCRAFT CONTAINED ADEQUATE FUEL FOR THE FLIGHT, RESULTING IN LOSS OF ENGINE POWER DUE TO FUEL EXHAUSTION. |
| Feb 10, 1993 | HILLSBORO, TX | N3876Y | Minor | substantial |
THE POWER LOSS DUE TO FUEL EXHAUSTION FOR UNDETERMINED REASONS. FACTORS WERE THE DARK NIGHT CONDITIONS AND THE LACK OF SUITABLE TERRAIN FOR THE ENSUI…THE POWER LOSS DUE TO FUEL EXHAUSTION FOR UNDETERMINED REASONS. FACTORS WERE THE DARK NIGHT CONDITIONS AND THE LACK OF SUITABLE TERRAIN FOR THE ENSUING FORCED LANDING. |
| Sep 22, 1992 | ST. AUGUSTINE, FL | N121PL | Minor | destroyed | THE PILOT-IN-COMMAND'S FAILURE TO CONDUCT A PREFLIGHT INSPECTION OF THE FUEL TANKS PRIOR TO TAKEOFF. |