Cessna 210 Safety Record
Complete NTSB accident and incident history. 819 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jun 12, 2005 | Watsonville, CA | N9457T | Incident | substantial | the pilot's failure to extend the landing gear prior to landing. |
| May 30, 2005 | Friendship, WI | N9623X | Incident | substantial | The loss of engine power for an undetermined reason. Contributing factors to the accident were the trees and the dark night light condition. |
| May 25, 2005 | Harvey, LA | N5120Q | Incident | substantial | The loss of engine power for undetermined reasons. A contributing factor was the lack of suitable terrain for the forced landing. |
| May 15, 2005 | Houston, TX | N1766X | Incident | substantial | The pilot's failure to maintain directional control during landing roll. A contributing factor was reported partial loss of brake control. |
| Mar 24, 2005 | Bronson, MI | N2380F | Incident | substantial |
The pilot's inadequate preflight preparation which failed to detect contaminated fuel that led to a loss of engine power. The unsuitable terrain enco…The pilot's inadequate preflight preparation which failed to detect contaminated fuel that led to a loss of engine power. The unsuitable terrain encountered was a factor. |
| Mar 13, 2005 | Bradfordville, FL | N4617C | Incident | substantial |
The failure of ATC to provide traffic advisories and safety alerts required in class C airspace and the inability of both pilots to see and avoid each…The failure of ATC to provide traffic advisories and safety alerts required in class C airspace and the inability of both pilots to see and avoid each other (low wing on top, high wing below), resulting in the midair collision. |
| Mar 08, 2005 | Oxnard, CA | N2044S | Incident | substantial |
A pinhole leak in the fuel pressure line during the takeoff roll that was ignited by an electrical arc associated with wires adjacent to the fuel line…A pinhole leak in the fuel pressure line during the takeoff roll that was ignited by an electrical arc associated with wires adjacent to the fuel line. A contributing factor in the accident was the failure of maintenance personnel to comply with a manufacturer's service bulletin that addressed potential damage to the fuel line. |
| Jan 01, 2005 | Weston, FL | N6195N | Fatal (1) | destroyed |
The pilot's failure to maintain his assigned altitude, and allowed the airplane to descend for undetermined reasons resulting in an in-flight collisio…The pilot's failure to maintain his assigned altitude, and allowed the airplane to descend for undetermined reasons resulting in an in-flight collision with terrain. Factors in the accident were clouds, rain, and the dark night. |
| Nov 12, 2004 | Apple Valley, CA | N5LT | Incident | substantial |
loss of engine power due to fuel starvation/exhaustion, which was a result of the pilot's inadequate preflight inspection and failure to ensure there …loss of engine power due to fuel starvation/exhaustion, which was a result of the pilot's inadequate preflight inspection and failure to ensure there was enough fuel onboard for the flight. |
| Oct 30, 2004 | North Las Vegas, NV | N6675X | Incident | substantial | loss of engine power for undetermined reasons. |
| Oct 13, 2004 | Freeport, BF | N357RB | Incident | destroyed | Investigation pending |
| Oct 10, 2004 | Salida, CO | N732TE | Incident | substantial |
The pilot's inadequate preflight planning which failed to determine the fuel supply was inadequate resulting in fuel exhaustion and the loss of engine…The pilot's inadequate preflight planning which failed to determine the fuel supply was inadequate resulting in fuel exhaustion and the loss of engine power. |
| Sep 22, 2004 | Flagstaff, AZ | N9757X | Minor | substantial |
the pilot's improper leaning procedures and delayed decision to abort the takeoff when it became obvious that the engine was not developing full power…the pilot's improper leaning procedures and delayed decision to abort the takeoff when it became obvious that the engine was not developing full power. A factor in the accident was the pilot's decision to use a runway with a quartering tailwind. |
| Sep 09, 2004 | Livingstone, ZA | ZS-KOX | Fatal (6) | destroyed | Investigation pending |
| Jul 14, 2004 | Quarryville, PA | N6043N | Incident | substantial |
Improper maintenance performed on the airplane, which resulted in a total electrical failure during cruise flight in IMC, and a subsequent precautiona…Improper maintenance performed on the airplane, which resulted in a total electrical failure during cruise flight in IMC, and a subsequent precautionary landing. A factor in the accident was the low ceiling. |
| May 27, 2004 | Marsh Harbour, BF | N9690X | Fatal (3) | substantial | Investigation pending |
| Feb 29, 2004 | Blountville, TN | N9660T | Fatal (2) | substantial |
The pilot's improper flare, and improper recovery which resulted in a bounced landing, collapse of the left main landing gear, and the pilot's failure…The pilot's improper flare, and improper recovery which resulted in a bounced landing, collapse of the left main landing gear, and the pilot's failure to maintain airspeed while maneuvering resulting in a stall, uncontrolled descent, and collision with the ground. A factor in the accident was the flight instructor's improper supervision of the pilot. |
| Feb 22, 2004 | Valley Spring, TX | N6175Y | Fatal (1) | destroyed |
The pilot's continued flight into known adverse weather and failure to maintain control of the airplane while maneuvering in instrument meteorological…The pilot's continued flight into known adverse weather and failure to maintain control of the airplane while maneuvering in instrument meteorological conditions, due to spatial disorientation. |
| Feb 16, 2004 | Pittsburgh, PA | N4974U | Incident | substantial |
The owner/pilot-mechanic's failure to comply with an airworthiness directive, which resulted in a fatigue fracture to the left main landing gear saddl…The owner/pilot-mechanic's failure to comply with an airworthiness directive, which resulted in a fatigue fracture to the left main landing gear saddle. |
| Jan 14, 2004 | Fort Meade, FL | N453MC | Incident | substantial |
The failure of the pilot to abort the takeoff after encountering fog during the preflight and engine run-up, and also his failure to maintain proper a…The failure of the pilot to abort the takeoff after encountering fog during the preflight and engine run-up, and also his failure to maintain proper alignment with the runway during the takeoff roll due to a fogged windshield resulting in the collision with a fence. |
| Dec 30, 2003 | Rialto, CA | N6539X | Minor | substantial |
The pilot's inadequate in-flight planning/decision by his fuel mismanagement and his delay in initiating remedial action which resulted in fuel exhaus…The pilot's inadequate in-flight planning/decision by his fuel mismanagement and his delay in initiating remedial action which resulted in fuel exhaustion and the loss of engine power. |
| Dec 14, 2003 | Clarendon, TX | N718LG | Serious (1) | destroyed |
the loss of engine power due the separation of the number six cylinder as a result of a fatigue failure from the loosening of the cylinder attachment …the loss of engine power due the separation of the number six cylinder as a result of a fatigue failure from the loosening of the cylinder attachment hardware. |
| Nov 28, 2003 | Santiago, CI | CC-PIK | Minor | substantial | Investigation pending |
| Nov 16, 2003 | Tolar, TX | N777SG | Fatal (1) | destroyed | The pilot's improper pre-flight planning and loss of engine power for undetermined reasons. A factor was the fog. |
| Nov 09, 2003 | Millington, TN | N3728Y | Incident | substantial | The malfunction of the main hydraulic landing gear system actuator resulting in an emergency gear up landing. |