Cessna 210 Safety Record

Complete NTSB accident and incident history. 819 events recorded from 1982 to 2026.

819

All Events

427

Incidents

128

Minor

64

Serious

192

Fatal (413 fatalities)

Date Location Reg# Severity Damage Probable Cause
Sep 12, 2025 Gore Springs, MS N911MC Minor substantial Investigation pending
Dec 23, 2023 Gulfport, MS N6PD Minor substantial The pilot’s failure to maintain directional control during the go-around with a crosswind.
Aug 30, 2023 Wichita, KS N9663X Minor substantial Loss of engine power for reasons that could not be determined.
May 20, 2023 Redding, CA N9433T Minor substantial
A fuel leak caused by an age-degraded fuel pressure sender hose, which resulted in fuel starvation and a loss of engine power. Contributing to the acc…

A fuel leak caused by an age-degraded fuel pressure sender hose, which resulted in fuel starvation and a loss of engine power. Contributing to the accident was inadequate maintenance.

Nov 21, 2021 Brent, AL N5779J Minor substantial
The inadequate maintenance of the oil filter adapter, which resulted in in an engine oil leak and subsequent loss engine oil pressure, and the subsequ…

The inadequate maintenance of the oil filter adapter, which resulted in in an engine oil leak and subsequent loss engine oil pressure, and the subsequent off-airport landing.

May 19, 2021 Island of Utila, HO HR-AVD Minor substantial Investigation pending
Mar 05, 2020 Needles, CA N123CE Minor substantial A loss of engine power for undetermined reasons due to a lack of available evidence.
Dec 24, 2019 Concord, NC N30259 Minor substantial
A malfunction of the left main landing gear brake during landing for undetermined reasons. Contributing was the pilot’s failure to attain a proper tou…

A malfunction of the left main landing gear brake during landing for undetermined reasons. Contributing was the pilot’s failure to attain a proper touchdown point and maintain an appropriate approach speed while landing on the wet turf runway.

Apr 08, 2017 Santa Teresa, NM N3938Y Minor substantial The pilot’s improper landing flare, which resulted in a hard, porpoised landing and subsequent nose-over.
Nov 08, 2016 Metropolitana, CI CC-LLH Minor Investigation pending
Feb 02, 2016 Park Valley, UT N8340Z Minor substantial
The pilot's decision to drag the left main landing gear on a snow covered dry lake bed, which resulted in a loss of directional control and a nose ove…

The pilot's decision to drag the left main landing gear on a snow covered dry lake bed, which resulted in a loss of directional control and a nose over during an aborted landing.

Jul 12, 2015 Stafford Twp, NJ N315EC Minor substantial
The total loss of engine power due to the failure of the crankshaft, which resulted from a mechanic's failure to properly torque the engine cylinder t…

The total loss of engine power due to the failure of the crankshaft, which resulted from a mechanic's failure to properly torque the engine cylinder through bolts.

Dec 04, 2014 Sussex, NJ N8296Z Minor substantial
Maintenance personnel’s inadequate inspection of the No. 2 cylinder valve area during the most recent annual inspection, which resulted in the in-flig…

Maintenance personnel’s inadequate inspection of the No. 2 cylinder valve area during the most recent annual inspection, which resulted in the in-flight failure of the intake valve springs due to rust on the spring surfaces and subsequent fatigue cracking.

Apr 18, 2014 Searcy, AR N9421X Minor substantial The pilot's inadequate preflight inspection of the airplane, which resulted in oil starvation and a subsequent engine failure.
Dec 20, 2013 Guymon, OK N2382F Minor substantial The pilot's failure to maintain adequate airspeed during takeoff, which resulted in an aerodynamic stall and collision with terrain.
Nov 28, 2013 Montrose, PA N777BK Minor substantial The pilot’s failure to check the fuel tanks for contaminants after fueling, which resulted in a total loss of engine power due to water contamination.
Nov 09, 2012 La Grange, TX N732BL Minor substantial
The total loss of engine power due to the loss of oil to the engine. Contributing to the accident was maintenance personnel’s improper installation of…

The total loss of engine power due to the loss of oil to the engine. Contributing to the accident was maintenance personnel’s improper installation of the engine oil filter adaptor, which resulted in the loss of oil to the engine.

Jul 02, 2012 West Glacier, MT N8450Z Minor substantial
The pilot elected to abort the takeoff without sufficient runway available to land and stop the airplane. Contributing to the accident was the illusio…

The pilot elected to abort the takeoff without sufficient runway available to land and stop the airplane. Contributing to the accident was the illusion created by the rising terrain, which influenced the pilot's decision to abort the takeoff.

Apr 27, 2012 Fowler's Bluff, FL N6564X Minor substantial The pilot's inadequate in-flight fuel management, which resulted in a total loss of engine power due to fuel starvation.
Jan 25, 2012 Port Orange, FL N7130U Minor substantial The total loss of engine power for reasons that could not be conclusively determined during postaccident examination.
Jul 22, 2011 Darby, MT N8427Z Minor substantial
The fatigue failure of the aluminum air intake duct, which resulted in material being ingested into the engine cylinders and a subsequent loss of engi…

The fatigue failure of the aluminum air intake duct, which resulted in material being ingested into the engine cylinders and a subsequent loss of engine power during cruise flight.

Aug 31, 2010 Houma, LA N210PR Minor substantial The pilot’s improper fuel management, which resulted in a loss of engine power due to fuel exhaustion.
Jun 25, 2010 Babylon, NY N3973Y Minor substantial The loss of engine power due to the failure of the oil filter gasket and the subsequent engine oil depletion.
May 21, 2010 Benson, AZ N6630X Minor substantial
A loss of engine power due to fuel starvation as a result of a loss of fuel pressure caused by the fuel pump screws being loose. Contributing to the a…

A loss of engine power due to fuel starvation as a result of a loss of fuel pressure caused by the fuel pump screws being loose. Contributing to the accident was inadequate maintenance.

May 19, 2010 Arbuckle, CA N580TP Minor substantial
Insufficient clamping force to the connecting rod bolt, which resulted in looseness in the connecting rod bearing area that led to the fatigue fractur…

Insufficient clamping force to the connecting rod bolt, which resulted in looseness in the connecting rod bearing area that led to the fatigue fracture of the connecting rod and a subsequent loss of engine power.

Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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