Cessna 182N Safety Record
Complete NTSB accident and incident history. 75 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Feb 09, 2025 | Auburn, CA | N92467 | Incident | substantial | The pilot’s improper use of throttle and brakes during engine start that resulted in a loss of control and impact with a hangar. |
| Sep 04, 2022 | Blairstown, NJ | N8942G | Incident | substantial | The pilot’s decision to cross the taxiway at an unsuitable location. |
| Dec 29, 2013 | Paradis, LA | N491CC | Incident | substantial | The collision with a bird which resulted in substantial damage to the airplane. |
| May 06, 2012 | Newport, VT | N9217G | Incident | substantial | The pilot’s failure to maintain adequate airspeed during the approach, which resulted in an aerodynamic stall and hard landing. |
| Jul 26, 2008 | Big Creek, ID | N92767 | Incident | substantial | The airplane encountered a downdraft during the landing flare. Contributing to the accident was the high density altitude. |
| Apr 12, 2008 | Amarillo, TX | N9008G | Incident | substantial |
The pilot's failure to maintain aircraft control during the landing. Contributing to the accident were the crosswind, gusty wind conditions and the pi…The pilot's failure to maintain aircraft control during the landing. Contributing to the accident were the crosswind, gusty wind conditions and the pilot's inadequate compensation for the wind conditions. |
| Jun 19, 2006 | Cooperstown, ND | N9073G | Incident | substantial |
The pilot's inadequate compensation for the wind conditions which resulted in a loss of directional control while landing. Factors associated with th…The pilot's inadequate compensation for the wind conditions which resulted in a loss of directional control while landing. Factors associated with the accident were the crosswind condition, the high vegetation which the airplane contacted, and the high density altitude. |
| Jul 24, 2004 | Bainville, MT | N92824 | Incident | substantial | The pilot's misjudgment of his airspeed on landing, and his subsequent overrunning of the runway. A contributing factor was the trees. |
| Jul 05, 2004 | Lancaster, WI | N92422 | Incident | substantial | The pilot's inadequate compensation for the gusty winds and his improper flare. The wind gusts were a contributing factor. |
| Oct 12, 2001 | Graham, MO | N92913 | Incident | substantial | A loss of engine power due to the fatigue failure of the number 2 piston. Contributing to the accident was the unsuitable terrain. |
| Apr 18, 2001 | Cedarville, NJ | N9174G | Incident | substantial | The pilot's failure to maintain directional control during the landing flare. A factor was the wind gusts. |
| Jul 19, 1999 | GREEN BAY, WI | N92215 | Incident | substantial | The pilot's delayed flare and his improper recovery from a bounced landing. |
| May 21, 1999 | GRANITE, OR | N92887 | Incident | substantial | Clearance was not maintained. A sign and the selection of unsuitable terrain for landing were factors. |
| Oct 09, 1998 | GENESEE, MI | N92322 | Incident | substantial |
the pilot's failure to maintain directional control and the subsequent failure to attain clearance with the trees during takeoff. Factors associated …the pilot's failure to maintain directional control and the subsequent failure to attain clearance with the trees during takeoff. Factors associated with the accident were the trees, dark night conditions, and fog which resulted in the lack of visual detection of the surroundings. |
| Apr 14, 1998 | ALBUQUERQUE, NM | N9008G | Incident | substantial |
The pilot's failure to attain the proper touchdown point during landing, resulting in an overrun, and his exceeding the airplane's maximum crosswind c…The pilot's failure to attain the proper touchdown point during landing, resulting in an overrun, and his exceeding the airplane's maximum crosswind component. A factor was the gusty crosswind. |
| Jul 18, 1997 | SACRAMENTO, CA | N9099G | Incident | substantial |
Failure of maintenance personnel to adequately repair the pitch trim system and ensure that it was properly rigged, and the pilot's failure to maintai…Failure of maintenance personnel to adequately repair the pitch trim system and ensure that it was properly rigged, and the pilot's failure to maintain pitch control due to the distraction at liftoff of the mistrim condition. |
| Jun 11, 1997 | FREDERICK, MD | N8970G | Incident | substantial |
The private pilot's improper flare, and the certificated flight instructor's delayed decision to add power, which resulted in the subsequent hard land…The private pilot's improper flare, and the certificated flight instructor's delayed decision to add power, which resulted in the subsequent hard landing. |
| Dec 07, 1996 | OBERGON, MX | N92243 | Incident | substantial | Investigation pending |
| Jun 30, 1996 | TRUTH OR CONSEQ, NM | N9001G | Incident | substantial | The loss of engine power due to the fatigue failure of the number one piston. A factor was the lack of suitable terrain for the forced landing. |
| Oct 08, 1994 | NEW LONDON, NH | N8903G | Incident | substantial |
the failure of the number four push rod, which resulted in the complete loss of engine power and forced landing, and the subsequent nose over on soft …the failure of the number four push rod, which resulted in the complete loss of engine power and forced landing, and the subsequent nose over on soft terrain. |
| Sep 28, 1994 | CORTEZ, CO | N9ZG | Incident | substantial | THE PILOT'S IMPROPER RECOVERY FROM A BOUNCED LANDING. |
| Oct 26, 1993 | ONAGA, KS | N92881 | Incident | substantial |
the pilot-in-command's poor pre-flight planning and failure to maintain runway alignment. Factors were the dark light conditions and the lack of runw…the pilot-in-command's poor pre-flight planning and failure to maintain runway alignment. Factors were the dark light conditions and the lack of runway lights. |
| Apr 16, 1993 | ANACORTES, WA | N71131 | Incident | substantial |
THE LOSS OF CONTROL BY THE PIC WHEN HE SELECTED THE WRONG RUNWAY, FAILED TO ATTAIN THE PROPER TOUCHDOWN POINT, INADVERTENTLY STALLED THE ACFT ATTEMPTI…THE LOSS OF CONTROL BY THE PIC WHEN HE SELECTED THE WRONG RUNWAY, FAILED TO ATTAIN THE PROPER TOUCHDOWN POINT, INADVERTENTLY STALLED THE ACFT ATTEMPTING TO ABORT THE LANDING, AND FAILED TO MAINTAIN DIRECTIONAL CONTROL AFTER THE AIRCRAFT MUSHED BACK ONTO THE STRIP. A FACTOR RELATED TO THE ACCIDENT WAS THE TAILWIND CONDITIONS. |
| Feb 23, 1992 | SAN ARDO, CA | N8948G | Incident | substantial | THE PILOT'S INADEQUATE PREFLIGHT INSPECTION. CONTRIBUTING TO THIS ACCIDENT WAS WATER CONTAMINATION IN THE FUEL AND THE SOFT SOIL LANDING AREA. |
| May 11, 1991 | SHELTON, WA | N8949G | Incident | substantial |
THE TOTAL LOSS OF POWER DUE TO MECHANICAL FAILURE WHEN THE PILOT WAS OVER UNSUITABLE TERRAIN FOR A FORCED LANDING. FACTORS INCLUDE A HARD LANDING AFTE…THE TOTAL LOSS OF POWER DUE TO MECHANICAL FAILURE WHEN THE PILOT WAS OVER UNSUITABLE TERRAIN FOR A FORCED LANDING. FACTORS INCLUDE A HARD LANDING AFTER AN INADVERTENT STALL PRIOR TO TOUCHDOWN ON A HIGHWAY. |