Cessna 182D Safety Record
Complete NTSB accident and incident history. 60 events recorded from 1982 to 2024.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| May 01, 2023 | Batesville, MS | N8713X | Incident | substantial |
The pilot’s failure to maintain airplane control while landing with a left gusting crosswind. Contributing to the accident was the partial loss of eng…The pilot’s failure to maintain airplane control while landing with a left gusting crosswind. Contributing to the accident was the partial loss of engine power during the go-around. |
| Jul 06, 2022 | McGrath, AK | N8754X | Incident | substantial | A nose landing gear collapse during landing for reasons that could not be determined based on the available information. |
| Mar 02, 2022 | Desert Camp, CA | N8814X | Incident | substantial | The airplane’s loss of engine power due to carburetor icing. |
| May 18, 2018 | Crescent Mills, CA | N9163X | Incident | substantial | A total loss of engine power due to the development of carburetor icing. |
| Nov 24, 2015 | Hamlet, NE | N8983X | Incident | substantial | The student pilot's incorrect brake application which resulted in a runway excursion and a nose over. |
| May 17, 2013 | East Moriches, NY | N8775X | Incident | substantial |
The inadvertent deployment of the skydiving instructor's drogue chute when he exited the airplane, resulting in it contacting and damaging the horizon…The inadvertent deployment of the skydiving instructor's drogue chute when he exited the airplane, resulting in it contacting and damaging the horizontal stabilizer. |
| Jul 28, 2012 | Rose Hill, KS | N8882X | Incident | substantial | The inadvertent deployment of a skydiver's parachute, which struck the right horizontal stabilizer. |
| Sep 05, 2011 | Roundup, MT | N8772X | Incident | substantial | The pilot's failure to maintain clearance from an obstacle during the landing flare. |
| Feb 06, 2011 | Quartzsite, AZ | N8859X | Incident | substantial |
The pilot's inadequate compensation for the wind and subsequent loss of directional control, which resulted in a runway excursion and collision with a…The pilot's inadequate compensation for the wind and subsequent loss of directional control, which resulted in a runway excursion and collision with a parked aircraft. |
| Sep 20, 2010 | Houston, TX | N9071X | Incident | substantial |
The loss of engine power during the initial climb due to decreased engine oil quantity and pressure as a result of the engine's oil cap not being adeq…The loss of engine power during the initial climb due to decreased engine oil quantity and pressure as a result of the engine's oil cap not being adequately secured. |
| May 30, 2010 | Chateaugay, NY | N9985T | Incident | substantial | The pilot's misjudgedment of his speed and distance during landing, which resulted in an overrun. |
| Aug 06, 2008 | Gerlach, NV | N800RJ | Incident | substantial | The pilot's failure to maintain obstacle clearance during takeoff initial climb. |
| Apr 27, 2008 | Madison, IN | N9111X | Incident | substantial |
The inadequate preflight inspection of the landing gear tires by the pilot, which did not identify a worn tire and resulted in a flat tire during land…The inadequate preflight inspection of the landing gear tires by the pilot, which did not identify a worn tire and resulted in a flat tire during landing touchdown. An additional cause was the directional control not possible during the landing rollout, and the improper go-around procedure by the pilot. Contributing to the accident were the landing gear wheel fairing and the ditch. |
| Jun 18, 2007 | Phoenix, AZ | N807X | Incident | substantial | The loss of engine power due to the intake manifold disconnection to the engine's cylinders on the left side. |
| Jul 25, 2006 | Santa Clarita, CA | N8961X | Incident | substantial |
A loss of engine power due to fuel exhaustion. The fuel exhaustion was the result of a split O-ring on the right fuel cap, which allowed fuel to siph…A loss of engine power due to fuel exhaustion. The fuel exhaustion was the result of a split O-ring on the right fuel cap, which allowed fuel to siphon out of the right fuel tank during flight. |
| Mar 16, 2006 | Sandpoint, ID | N9971T | Incident | substantial |
The pilot's failure to maintain clearance from an object (snow blowing equipment) while taxiing. The snow blowing equipment, and the pilot's failure …The pilot's failure to maintain clearance from an object (snow blowing equipment) while taxiing. The snow blowing equipment, and the pilot's failure to adequately maneuver the aircraft around snow berms were factors. |
| Sep 12, 2003 | Rushville, IN | N8702X | Incident | substantial | The pilot failed to maintain control of the airplane during the initial takeoff climb which resulted in an inadvertent stall. |
| Jun 09, 1999 | ZURICH, KS | N9169X | Incident | substantial | the pilot's inadequate preflight planning/preparation. A factor was fuel exhaustion. |
| Sep 19, 1998 | FORT YUKON, AK | N8874X | Incident | substantial | A failure of the pilot to maintain the proper glidepath to the landing touch down spot. |
| Apr 05, 1997 | TUCSON, AZ | N9000X | Incident | substantial |
Fuel exhaustion due to the inadequate preflight inspections performed by both pilots. A factor in the accident was the crosswind experienced during l…Fuel exhaustion due to the inadequate preflight inspections performed by both pilots. A factor in the accident was the crosswind experienced during landing rollout. |
| Apr 22, 1995 | OVERBROOK, OK | N9104X | Incident | substantial | THE PILOT'S FAILURE TO MAINTAIN FLYING SPEED, RESULTING IN AN INADVERTENT STALL. A FACTOR WAS THE CROSSWINDS. |
| Jan 22, 1994 | DONALSONVILLE, GA | N8980X | Incident | destroyed | THE PILOT'S FAILURE TO CLEAR THE INDUCTION SYSTEMS OF EXCESSIVE FUEL. |
| Jun 06, 1992 | BEEVILLE, TX | N8979X | Incident | substantial | ENGINE POWER LOSS FOR UNDETERMINED CAUSE. A FACTOR WAS THE PILOTS' FAILURE TO LOWER FLAPS FOR THE SHORT FIELD LANDING. |
| Feb 20, 1992 | MONROE, UT | N9030X | Incident | substantial | AN ABORTED TAKEOFF WAS NOT PERFORMED. THE WET, SOFT RUNWAY WAS A FACTOR. |
| Dec 15, 1991 | CARLISLE, AR | N8883X | Incident | substantial |
THE PARACHUTE JUMPER'S RESERVE PARACHUTE INADVERTENTLY OPENING, FOR UNDETERMINED REASONS, RESULTING IN THE JUMPER IMPACTING THE RIGHT HORIZONTAL STABI…THE PARACHUTE JUMPER'S RESERVE PARACHUTE INADVERTENTLY OPENING, FOR UNDETERMINED REASONS, RESULTING IN THE JUMPER IMPACTING THE RIGHT HORIZONTAL STABILIZER. |