Cessna 150 Safety Record
Complete NTSB accident and incident history. 3241 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| May 26, 2012 | San Diego, CA | N7093F | Incident | substantial |
A total loss of engine power while maneuvering for reasons that could not be determined because postaccident examination did not reveal any anomalies …A total loss of engine power while maneuvering for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation. |
| May 23, 2012 | Tulare, CA | N11428 | Incident | substantial | A partial loss of engine power, which was likely the result of carburetor icing. |
| Apr 14, 2012 | Cedartown, GA | N714JJ | Incident | substantial | The pilot’s failure to maintain directional control during takeoff. |
| Jan 13, 2012 | El Dorado, KS | N714BS | Incident | substantial |
The loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any anoma…The loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation. |
| Oct 07, 2011 | Vidalia, LA | N642EZ | Incident | substantial | A total loss of engine power likely due to carburetor ice. |
| Oct 05, 2011 | Punta Gorda, FL | N11280 | Incident | substantial | The partial loss of engine power due to contamination of the fuel system that was not detected because of the pilot’s inadequate preflight inspection. |
| Jul 20, 2011 | Elizabethtown, KY | N8576U | Incident | substantial | A total loss of engine power for undetermined reasons. |
| Jul 09, 2011 | Lacassine, LA | N50575 | Incident | substantial | A total loss of engine power due to fuel exhaustion, as a result of the pilot's improper fuel planning. |
| Jul 06, 2011 | Mesa, AZ | N2878S | Incident | substantial | The pilot's failure to maintain directional control during the go around. |
| Jul 04, 2011 | Plymouth, MA | N150ET | Incident | substantial |
A partial loss of engine power during initial climb due to a stuck cylinder valve, which resulted from excessive corrosion and carbon deposits on the …A partial loss of engine power during initial climb due to a stuck cylinder valve, which resulted from excessive corrosion and carbon deposits on the valve springs due to inadequate maintenance. |
| Jul 02, 2011 | Weirsdale, FL | N1953Z | Incident | substantial | The pilot's failure to maintain adequate clearance from the stopped trailer while taxiing. |
| May 31, 2011 | Sully, IA | N7818F | Incident | substantial |
The pilot's failure to attain an adequate climb rate during the initial takeoff, resulting in the airplane settling back down and departing the runway…The pilot's failure to attain an adequate climb rate during the initial takeoff, resulting in the airplane settling back down and departing the runway. Contributing to the accident was the pilot's inadequate preflight planning and preparation. |
| May 20, 2011 | Greenville, KY | N68844 | Incident | substantial | The pilot's loss of control during takeoff after he reached to secure a seatbelt that was wedged in the passenger door. |
| Apr 24, 2011 | College Place, WA | N23295 | Incident | substantial |
The pilot’s delayed use of carburetor heat while operating the airplane in atmospheric conditions conducive to carburetor icing, which resulted in a t…The pilot’s delayed use of carburetor heat while operating the airplane in atmospheric conditions conducive to carburetor icing, which resulted in a total loss of engine power due to carburetor icing during final approach. |
| Apr 02, 2011 | Factoryville, PA | N7225X | Incident | substantial | The pilot's inadequate flare during the gusty crosswind landing, which resulted in a hard landing. |
| Mar 26, 2011 | Hannawana Falls, NY | N8830G | Incident | substantial | The pilot's improper fuel management, which resulted in a loss of engine power due to fuel exhaustion. |
| Mar 20, 2011 | Maury City, TN | N6555S | Incident | substantial | The pilot's failure to attain the proper glidepath during on off-airport landing. |
| Feb 17, 2011 | Jonesborough, TN | N7237S | Incident | substantial | A partial loss of engine power during initial climb for undetermined reasons. |
| Feb 12, 2011 | Trenton, MI | N6622G | Incident | substantial |
The loss of preload torque on a connecting rod nut and bolt, which precipitated a separation of the connecting rod from the engine's crankshaft and re…The loss of preload torque on a connecting rod nut and bolt, which precipitated a separation of the connecting rod from the engine's crankshaft and resulted in the total loss of engine power. |
| Feb 05, 2011 | Gonzales, LA | N11790 | Incident | substantial | The flight instructor's failure to monitor the available fuel supply, which resulted in a loss of engine power due to fuel exhaustion. |
| Oct 01, 2010 | North Pole, AK | N3569L | Incident | substantial | The overstress separation of the left nose wheel steering linkage rod end during the takeoff roll, which resulted in a loss of control. |
| Sep 14, 2010 | Bethel, AK | N45624 | Incident | substantial | The pilot's failure to maintain altitude/clearance during a night approach, resulting in a collision with terrain short of the runway. |
| Sep 12, 2010 | Kenai, AK | N1612Q | Incident | substantial |
The pilot's decision to takeoff from a remote lake after overloading the airplane. Contributing to the accident was the pilot's lack of a seaplane rat…The pilot's decision to takeoff from a remote lake after overloading the airplane. Contributing to the accident was the pilot's lack of a seaplane rating. |
| Sep 03, 2010 | Fields, OR | N2068Z | Incident | substantial |
The pilot's misjudged landing flare, resulting in a bounced landing and loss of directional control. Contributing to the accident was the pilot's inac…The pilot's misjudged landing flare, resulting in a bounced landing and loss of directional control. Contributing to the accident was the pilot's inaccurate perception of the airplane’s proximity to the ground as a result of the featureless white landing area. |
| Jul 22, 2010 | Knoxville, TN | N45220 | Incident | substantial | The student pilot's improper recovery from a bounced landing. |