Bellanca 17-30A Safety Record
Complete NTSB accident and incident history. 139 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Dec 30, 2023 | Washington, MO | N678MJ | Serious (1) | substantial |
Fuel starvation and a total loss of engine power due to an obstructed fuel vapor return path. Contributing to the accident was the pilot’s inadvertent…Fuel starvation and a total loss of engine power due to an obstructed fuel vapor return path. Contributing to the accident was the pilot’s inadvertent aerodynamic stall/spin, which likely increased the severity of the ground impact. |
| Mar 25, 2022 | Ash Flat, AR | N8869V | Serious (1) | substantial |
The partial loss of engine power during a go-around resulting in an inadvertent entry into an aerodynamic stall. Contributing to the accident was the …The partial loss of engine power during a go-around resulting in an inadvertent entry into an aerodynamic stall. Contributing to the accident was the inexperience of the low-time pilot. |
| Mar 01, 2017 | Carson City, NV | N39894 | Serious (1) | substantial |
A total loss of engine power due to internal corrosion of the fuel manifold valve. Also causal was the pilot's decision to return to the runway follow…A total loss of engine power due to internal corrosion of the fuel manifold valve. Also causal was the pilot's decision to return to the runway following the loss of engine power shortly after takeoff, and his exceedance of the airplane's critical angle of attack during the turn, which resulted in an aerodynamic stall. |
| Sep 14, 2014 | Monroe, GA | N6648V | Serious (2) | substantial | The improper installation of the oil filter adapter at an unknown time, which resulted in an oil leak and subsequent oil starvation to the engine. |
| Feb 02, 2008 | Mukilteo, WA | N8794V | Serious (1) | substantial | Loss of engine power while on final approach for undetermined reasons. Contributing to the accident was a power line. |
| Feb 17, 2007 | Fountain, FL | N6641V | Serious (2) | destroyed |
A loss of engine power due to a cracked engine exhaust muffler. Contributing to the accident were the inadequate inspection procedures of the muffler…A loss of engine power due to a cracked engine exhaust muffler. Contributing to the accident were the inadequate inspection procedures of the muffler system and the routing of the "P" leads wiring for the magnetos. |
| Dec 16, 2005 | Columbus, TX | N78SV | Serious (1) | substantial | The loss of engine power for undetermined reasons. A contributing factor was the lack of suitable terrain for the forced landing. |
| May 22, 2005 | Houston, TX | N39821 | Serious (2) | substantial | The pilot's mismanagement of the fuel and his inadequate monitoring of the fuel supply which resulted in fuel starvation. |
| Jun 09, 2002 | FALLON, NV | N8249R | Serious (1) | substantial |
the pilot's failure to attain an adequate takeoff airspeed, which resulted in a stall/mush. The high gross weight and density altitude were contribut…the pilot's failure to attain an adequate takeoff airspeed, which resulted in a stall/mush. The high gross weight and density altitude were contributing factors. |
| Nov 11, 2001 | Nevada, MO | N76SV | Serious (1) | substantial |
The inadequate fuel consumtion calculations by the pilot resulting in fuel starvation during the aborted landing, and the overloaded steering link for…The inadequate fuel consumtion calculations by the pilot resulting in fuel starvation during the aborted landing, and the overloaded steering link for undetermined reasons resulting in the lack of directional control during landing. Factors were the electrical system failure for undetermined reasons, the visual approach slope indicator (VASI) system, and the altitude/clearance from the VASI not possible by the pilot. |
| Jun 30, 2000 | ALBANY, GA | N8787V | Serious (2) | substantial |
The dual student's failure to purge the fuel lines of air after a fuel tank was run dry on the previous flight and the failure of the electric fuel bo…The dual student's failure to purge the fuel lines of air after a fuel tank was run dry on the previous flight and the failure of the electric fuel boost pump on or low position due to a loose wire which resulted in failure of the engine due to air in the lines and collision with trees during a forced landing. |
| Aug 23, 1999 | ROBBINS, TN | N42VB | Serious (1) | substantial |
The total loss of engine power due to failure of maintenance personnel to assure that the thru bolt nut at the Nos. 2 and 3 cylinders was adequately t…The total loss of engine power due to failure of maintenance personnel to assure that the thru bolt nut at the Nos. 2 and 3 cylinders was adequately torqued following removal and replacement of the No. 3 cylinder approximately 328 hours earlier. Also, the unsuitable terrain encountered by the pilot during the forced landing. A factor in the accident was the operation of the airplane by the owner exceeding the recommended oil change intervals. |
| Dec 18, 1997 | STEUBENVILLE, OH | N28122 | Serious (2) | destroyed | Collision with deer on runway during initial takeoff and climb. |
| Nov 09, 1996 | BRUNSWICK, GA | N86DR | Serious (1) | substantial | a complete loss of engine power as a result of piston failure, oil starvation, and the subsequent forced landing in unsuitable terrain. |
| Oct 08, 1996 | JACKPOT, NV | N28172 | Serious (1) | destroyed | the pilot's inadvertent disorientation in dark night time conditions and failure to maintain a proper climbing attitude. |
| May 21, 1995 | CONROE, TX | N8872V | Serious (1) | substantial |
THE FAILURE OF BOTH PILOTS TO MAINTAIN ADEQUATE VISUAL LOOKOUT. A FACTOR RELATING TO THE ACCIDENT WAS: FAILURE OF THE BELLANCA PILOT TO ADEQUATELY CO…THE FAILURE OF BOTH PILOTS TO MAINTAIN ADEQUATE VISUAL LOOKOUT. A FACTOR RELATING TO THE ACCIDENT WAS: FAILURE OF THE BELLANCA PILOT TO ADEQUATELY COMMUNICATE HIS INTENTIONS ON THE UNICOM FREQUENCY. |
| Dec 04, 1994 | KENT, WA | N39852 | Serious (2) | substantial |
FUEL STARVATION DUE TO THE UNPORTING OF THE USEABLE FUEL SUPPLY, AND THE PILOT'S FAILURE TO FOLLOW THE AIRPLANE'S PUBLISHED ENGINE STARTING PROCEDURES…FUEL STARVATION DUE TO THE UNPORTING OF THE USEABLE FUEL SUPPLY, AND THE PILOT'S FAILURE TO FOLLOW THE AIRPLANE'S PUBLISHED ENGINE STARTING PROCEDURES AFTER THE LOSS OF FUEL FLOW DURING DESCENT. FACTORS CONTRIBUTING TO THE ACCIDENT ARE THE PILOT'S LACK OF FAMILIARITY WITH THE AIRPLANE, AND A BERM. |
| Jul 11, 1992 | ORTONVILLE, MI | N6617V | Serious (2) | substantial | IMPROPER USE OF THE FUEL TANK SELECTOR SWITCH AND INADEQUATE EMERGENCY PROCEDURES BY THE PILOT IN COMMAND. |
| Oct 28, 1991 | COTULLA, TX | N6307Y | Serious (2) | substantial |
THE PILOT'S FAILURE TO MAINTAIN AIRCRAFT CONTROL. FACTORS RELATED TO THE ACCIDENT WERE: DARKNESS, AND A SHORT IN THE ELECTRICAL SYSTEM WHICH RESULTED…THE PILOT'S FAILURE TO MAINTAIN AIRCRAFT CONTROL. FACTORS RELATED TO THE ACCIDENT WERE: DARKNESS, AND A SHORT IN THE ELECTRICAL SYSTEM WHICH RESULTED IN PARTIAL FAILURE OF THE INSTRUMENT LIGHTS AND A MALFUNCTION OF THE AUTOPILOT. |
| Oct 06, 1987 | NEWPORT, VT | N39857 | Serious (1) | destroyed | Investigation pending |
| Sep 16, 1987 | LOUISVILLE, KY | N7378V | Serious (1) | substantial | Investigation pending |
| Jul 15, 1987 | MC KINNEY, TX | N28157 | Serious (1) | substantial | Investigation pending |
| Sep 24, 1985 | BURLINGTON, WA | N6627V | Serious (1) | substantial | Investigation pending |
| Mar 31, 1985 | ROANOKE, VA | N8233R | Serious (1) | substantial | Investigation pending |
| Sep 17, 1984 | BISHOP, CA | N14728 | Serious (1) | substantial | Investigation pending |