Bell 47 Safety Record
Complete NTSB accident and incident history. 744 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jun 05, 1990 | HOUMA, LA | N73241 | Incident | substantial | THE PILOT'S FAILURE TO MAINTAIN ROTOR RPM AND AN EXCESSIVE SINK RATE. |
| May 31, 1990 | BECKET, MA | N39268 | Incident | substantial |
A POWER LOSS DUE TO OIL STARVATION, AFTER MAINTENANCE PERSONNEL FAILED TO COMPLY WITH LYCOMING DIRECTIVES DURING THE ENGINE OVERHAUL. FACTORS RELATED …A POWER LOSS DUE TO OIL STARVATION, AFTER MAINTENANCE PERSONNEL FAILED TO COMPLY WITH LYCOMING DIRECTIVES DURING THE ENGINE OVERHAUL. FACTORS RELATED TO THE ACCIDENT WERE: IMPROPER ADJUSTMENT OF THE ENGINE OIL PRESSURE BY MAINTENANCE PERSONNEL AND UNSUITABLE TERRAIN. |
| May 21, 1990 | LAKE WALES, FL | N1390X | Minor | destroyed |
THE PILOT'S FAILURE TO MAINTAIN ADEQUATE CLEARANCE BETWEEN THE MAIN ROTOR BLADES AND A POWER LINE POLE WHILE MANEUVERING DURING AN AERIAL APPLICATION …THE PILOT'S FAILURE TO MAINTAIN ADEQUATE CLEARANCE BETWEEN THE MAIN ROTOR BLADES AND A POWER LINE POLE WHILE MANEUVERING DURING AN AERIAL APPLICATION FLIGHT. |
| May 14, 1990 | WYNNE, AR | N41SD | Serious (1) | substantial | LANDING GEAR SKID ENTANGLED WITH A FUEL HOSE. A FACTOR WAS THE PILOT'S INADEQUATE PREFLIGHT INSPECTION. |
| May 13, 1990 | BALTIMORE, MD | N4229A | Incident | substantial | THE PILOT APPLIED EXCESSIVE CYCLIC CONTROL, CAUSING THE MAIN ROTOR TO FLEX AND SEVERE THE TAIL CONE. |
| May 04, 1990 | RIVERSIDE, CA | N9FK | Minor | substantial |
THE PILOT'S FAILURE TO MAINTAIN CONTROL OF THE HELICOPTER. A FACTOR RELATED TO THE ACCIDENT WAS: THE PILOT'S LACK OF EXPERIENCE IN THE TYPE OF AIRCRAF…THE PILOT'S FAILURE TO MAINTAIN CONTROL OF THE HELICOPTER. A FACTOR RELATED TO THE ACCIDENT WAS: THE PILOT'S LACK OF EXPERIENCE IN THE TYPE OF AIRCRAFT. |
| Apr 26, 1990 | MARION, MA | N8591F | Incident | substantial | IMPROPER USE OF CARBURETOR HEAT BY THE PILOT RESULTING IN A LOSS OF ENGINE POWER. THE LACK OF SUITABLE TERRAIN FOR A FORCED LANDING WAS A FACTOR. |
| Apr 24, 1990 | HICKMAN, KY | N2134 | Incident | substantial | IMPROPER IN-FLIGHT PLANNING/DECISION BY THE PILOT. THE RESULTANT TAILWIND WAS A RELATED FACTOR. |
| Apr 18, 1990 | OAKDALE, MN | N5120B | Serious (1) | substantial | A SLIPPING ROTOR DRIVE CLUTCH ASSEMBLY DUE TO IMPROPER MAINTENANCE BY COMPANY PERSONNEL. CONTRIBUTING FACTORS WERE STATIC WIRES IN THE PATH. |
| Apr 14, 1990 | BIXBY, OK | N2238W | Minor | destroyed | LOSS OF CONTROL DUE TO UNDETERMINED MECHANICAL FAILURE. |
| Apr 12, 1990 | HARRISBURG, AR | N4779U | Incident | substantial | FAILURE OF THE GENERATOR, AND FAILURE OF THE PILOT TO MAINTAIN ROTOR RPM. |
| Apr 04, 1990 | LA VERNE, CA | N739B | Incident | substantial |
THE HELICOPTER'S ROTOR SYSTEM BEING ALLOWED TO UNDERSPEED AS A RESULT OF IMPROPER USE OF FLIGHT CONTROLS BY THE DUAL STUDENT; IMPROPER SUPERVISION BY …THE HELICOPTER'S ROTOR SYSTEM BEING ALLOWED TO UNDERSPEED AS A RESULT OF IMPROPER USE OF FLIGHT CONTROLS BY THE DUAL STUDENT; IMPROPER SUPERVISION BY THE CERTIFIED FLIGHT INSTRUCTOR; AND DELAYED REMEDIAL ACTION BY THE CERTIFIED FLIGHT INSTRUCTOR WHICH ALLOWED THE IN FLIGHT COLLISION WITH THE RUNWAY. |
| Apr 02, 1990 | Hillsboro, OR | N9449J | Serious (1) | substantial | THE PILOT'S FAILURE TO REFUEL RESULTING IN FUEL EXHAUSTION. |
| Mar 25, 1990 | ROCKLEDGE, FL | N10326 | Incident | substantial | FAILURE OF A CONNECTING ROD. |
| Mar 03, 1990 | MIAMI, FL | N4837 | Minor | substantial |
INADEQUATE PREFLIGHT BY THE PILOT, WHICH RESULTED IN FUEL EXHAUSTION DUE TO AN INADEQUATE SUPPLY OF FUEL. THE LOCATION OF TREES WAS A RELATED FACTOR I…INADEQUATE PREFLIGHT BY THE PILOT, WHICH RESULTED IN FUEL EXHAUSTION DUE TO AN INADEQUATE SUPPLY OF FUEL. THE LOCATION OF TREES WAS A RELATED FACTOR IN THAT THE PILOT WAS UNABLE TO MAINTAIN ROTOR RPM WHILE ATTEMPTING TO REACH A SUITABLE LANDING AREA DURING THE AUTOROTATION. |
| Feb 16, 1990 | REDLANDS, CA | N11HU | Incident | destroyed | FAILURE OF THE PILOT TO USE CARBURETOR HEAT WHEN WARRENTED BY CONDITIONS. |
| Jan 17, 1990 | LAFAYETTE, IN | N90836 | Incident | substantial |
THE HELICOPTER STUDENT'S IPROPER USE OF THE COLLECTIVE PITCH LEVER DURING THE LANDING PHASE OF FLIGHT. THE PILOT'S LACK OF TOTAL EXPEREINCE, THE RELAT…THE HELICOPTER STUDENT'S IPROPER USE OF THE COLLECTIVE PITCH LEVER DURING THE LANDING PHASE OF FLIGHT. THE PILOT'S LACK OF TOTAL EXPEREINCE, THE RELATIVELY HIGH WIND, AND INADVERTENT LIFTOFF OF THE HELICOPTER WERE FACTORS RELATED TO THE ACCIDENT. |
| Dec 04, 1989 | ARDMORE, OK | N2202C | Serious (1) | substantial | PILOT'S INADEQUATE COMPENSATION FOR EXISTING WIND CONDITIONS. CONTRIBUTING TO THE ACCIDENT WERE THE GUSTY TAIL WINDS. |
| Dec 02, 1989 | RIALTO, CA | N2899B | Minor | destroyed |
THE PILOT'S LOSS OF DIRECTIONAL CONTROL AND SUBSEQUENT OVERCONTROL WHILE HOVERING. CONTRIBUTING TO THE ACCIDENT WERE THE GUSTY WIND CONDITIONS AND THE…THE PILOT'S LOSS OF DIRECTIONAL CONTROL AND SUBSEQUENT OVERCONTROL WHILE HOVERING. CONTRIBUTING TO THE ACCIDENT WERE THE GUSTY WIND CONDITIONS AND THE PILOT'S INEXPERIENCE. |
| Nov 25, 1989 | EWELL, AL | N1358X | Serious (2) | substantial |
THE LOSS OF ENGINE POWER, FOR UNDETERMINED REASONS, AT LOW ALTITUDE DURING A PRACTICE AUTOROTATION. CONTRIBUTING TO THE ACCIDENT WAS THE INSTRUCTOR'S …THE LOSS OF ENGINE POWER, FOR UNDETERMINED REASONS, AT LOW ALTITUDE DURING A PRACTICE AUTOROTATION. CONTRIBUTING TO THE ACCIDENT WAS THE INSTRUCTOR'S FAILURE TO PROPERLY PLAN THE DEMONSTRATED AUTOROTATION SO AS TO PRECLUDE AN ACCIDENT, IN THE EVENT THAT POWER WAS NOT AVAILABLE. |
| Nov 06, 1989 | ELBERTON, GA | N73871 | Fatal (1) | destroyed | A LOSS OF ENGINE POWER DUE TO CARBURETOR ICE. |
| Nov 04, 1989 | WESTFIELD, MA | N57919 | Minor | substantial | LOSS OF AIRCRAFT CONTROL FOR AN UNDETERMINED REASON, WHICH RESULTED IN THE TAIL ROTOR STRIKING THE GROUND AND SEPARATING FROM THE HELICOPTER. |
| Nov 02, 1989 | LOXAHATCHEE, FL | N93067 | Serious (2) | substantial | FAILURE OF THE PILOT TO MAINTAIN ROTOR RPM AFTER PULLING UP FROM A SWATH RUN. A RELATED FACTOR WAS THE PRESENCE OF TREES. |
| Nov 01, 1989 | GUADALUPE, CA | N4798R | Incident | substantial |
THE PILOT'S FAILURE TO MAINTAIN SUFFICIENT CLEARANCE ALLOWING THE AIRCRAFT TO COLLIDE WITH A WOODEN POWER POLE. CONTRIBUTING TO THE ACCIDENT WAS THE S…THE PILOT'S FAILURE TO MAINTAIN SUFFICIENT CLEARANCE ALLOWING THE AIRCRAFT TO COLLIDE WITH A WOODEN POWER POLE. CONTRIBUTING TO THE ACCIDENT WAS THE SUNGLARE WHICH INHIBITED THE PILOT'S VISION. |
| Oct 29, 1989 | PLYMOUTH, IN | N500CD | Incident | substantial | THE STUDENT'S IMPROPER USE OF THE CYCLIC CONTROL AND THE INSTRUCTOR'S (CFI'S) INADEQUATE SUPERVISION. |