Cessna 182G
Single Engine Piston
Aircraft Details
Seller reportedDescription
N2314R S/N 182-55414. Cont. O-470-R; AF: 2,364; TSOH: 1468; TSPOH: 1468; Useful load 1,199; Horton STOL kit, Aspen Avionics Evolution EFD 1000; TruTrack Autopilot; JPI EGT-730 engine monitor; Harness seatbelts; Compressions: 78/80, 76/80, 76/80, 70/80, 70/80, 64/80. Extra parts, always hangared, will come with fresh annual. Based at Mineola Wisener Airport (3F9),.
Description and equipment details provided by the seller. AeroGurus does not verify seller-provided information.
Price Comparison 1 active offer
| Source | Price | Location | Listed | Days on Market | Status | Action |
|---|---|---|---|---|---|---|
|
Lupita Wisener
barnstormers.com
|
$130,000
|
Mineola, TX | May 22, 2026 | — | Active |
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AeroGurus Data & Analysis
Independent data from FAA, NTSB, and market analysis
About This Cessna 182G
This Cessna 182G (N2314R) is a 4-seat single engine piston . There are currently 3 182G aircraft listed for sale with asking prices ranging from $119,950 to $150,000. This aircraft is priced below the market average at $130,000.
The 182G cruises at 140 kts (259 km/h) with a range of 915 nm (1,695 km) — ideal for short hops and local flights. Service ceiling of 18,100 ft allows operation above most weather.
Operating costs: Fuel burn is 12.5 GPH (47 L/h), which at current Jet-A prices (~$5.50/gal) means approximately $69/hr in fuel alone. Total variable cost including maintenance reserves is approximately $160/hr. Annual fixed costs (hangar, insurance, crew, annual inspection) average $20,000.
NTSB records show 0 incidents for this airframe — a clean safety record. Mechanics have filed 10 service difficulty reports for this type — common maintenance items to discuss during pre-buy.
Pre-Purchase Checklist
Cessna 182G — Model Specs
Model specificationStandard specs for this model. Actual aircraft may differ.
Estimated Cost of Ownership
AeroGurus estimateCESSNA 182
AeroGurus estimates based on industry averages for the CESSNA 182. Actual costs vary by location, usage, maintenance history, and configuration. Not a financial quote.
Ownership & Registration
FAA registration data pending for N2314R.
Location & Ownership
Title Status
No FAA title records
Available for US-registered aircraft only
Source: FAA Aircraft Registry, FAA Civil Aviation Registry (DocIndex). Title data may be delayed. Always verify with an aviation attorney before purchase.
Safety Record
NTSB safety data coming soon.
We'll check N2314R against the NTSB accident database.
Service Difficulty Reports — Cessna 182G
SDRs are reports filed by mechanics about problems found during maintenance. 10 recent reports for this aircraft type.
DURING ACCIDENT INVESTIGATION OF N3267S, THE FORWARD OUTBOARD ATTACH BOLT P/N NAS147-34 HAD A PREEXISTING CRACK AT THE BEGINNING OF THE THREADS FROM THE SHAFT WITH THE PRESENCE OF CORROSION. THIS LEAD TO AN INSTANTANEOUS FAIL OF THE BOLT UPON LANDING...
(CAN) WHILE IN CRUISE FLIGHT, PILOT NOTICED INCREASED RPM AND VIBRATION. PILOT DECREASED RMP AND CARRIED OUT A PRECAUTIONARY LANDING. PROPELLER TECH HISTORY, PROPELLER O/H 21-FEB-11 -AT 1.3 TSO PROPELLER BLADES REPAINTED DUE TO POOR ADHESION -AT 3...
CASTING CRACK FOUND BY VISUAL INSPECTION DURING COURSE OF ANNUAL INSPECTION. THE CRACK IS LOCATED ON THE FORWARD END OF THE SUPPORT CASTING AND RUNS FROM 1/4 INCH FROM MOUNT HOLES ON THE OUTBOARD SIDE TO WITHIN 1/4 INCH OF THE MOUNT HOLES ON THE INB...
ON INSPECTION, A CRACK WAS IDENTIFIED IN THE FORGING FOR THE UPPER TORQUE LINK FOR THE NOSE LANDING GEAR. THE CRACK WAS ON BOTH SIDES OF THE BEAM SECTION ADJACENT TO THE EXTENSION STOP FOR THE GEAR.(AFT SIDE)
PILOT REPORTED THAT AFTER A NORMAL START, HE WAS UNABLE TO ADVANCE THE THROTTLE CONTROL TO CRUISE OR TAKEOFF POWER. A PARTIAL DISASSEMBLY OF THE CARBURETOR REVEALED THAT THE AIR METERING PIN/AIR METERING JET WAS BLOCKING THE THROTTLE SHAFT TRAVEL. ...
(CAN) MINOR PLAY (UP AND DOWN) ON THE RT ELEVATOR CAUSE BY LOOSE RIVETS ON THE TORQUE TUBE (TC NR 20070823010)
(CAN) NOSE GEAR UPPER TORQUE LINK WAS FOUND CRACKED INSIDE UPPER CORNER ON THE LT SIDE. FORGING NR 0543034-497, 2014 KAE-2A (TC NR20060327004)
LEFT HAND MAIN LANDING GEAR SPRING ASSEMBLY BROKE OF AT FUSELAGE WHILE TAXIING FOR FLIGHT. THERE WAS NO VISUAL EVIDENCE OF A PREVIOUS CRACK. THE GEAR LEG WAS SENT TO TRANSPORT SAFETY BOARD TO BE ANALYZED.
(AUS) AILERON MASS BALANCE WEIGHT ATTACHMENT RIVETS FAULTY. APPROXIMATELY HALF OF THE RIVETS FAILED TESTING AND INSPECTION IAW AD/CESSNA180/28.
THIS DEFECT WAS FOUND AS A RESULT OF INSPECTION REQUIRED BY AD. THIS PART WAS REPLACED AT THIS TIME JUNE 17, 2003. TT 5187.97. THIS REPORT REQUIRED BY AD PART (I).
Source: FAA Service Difficulty Reporting System. Shows maintenance issues reported by mechanics for this aircraft type.