Waco YMF Safety Record
Complete NTSB accident and incident history. 25 events recorded from 1986 to 2021.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Aug 06, 2021 | Yvoy-le-Marron, FR | F-GYMF | Serious (1) | destroyed | Investigation pending |
| Jun 13, 2020 | Ghent, NY | N323TX | Incident | substantial | A loss of directional control on takeoff, which resulted in a runway excursion and collision with trees. |
| Jun 22, 2019 | Bar Harbor, ME | N63WC | Incident | substantial | A total loss of engine power due to a cylinder failure for undetermined reasons. |
| Jul 02, 2016 | Austin, TX | N30AB | Minor | substantial | A total loss of engine power for undetermined reasons. |
| Dec 25, 2015 | Fullerton, CA | N99Y | Incident | substantial | The pilot's failure to maintain directional control during the landing roll. |
| Mar 30, 2013 | Thermal, CA | N14080 | Incident | substantial | The pilot’s failure to maintain directional control while landing in a gusting crosswind. |
| Dec 28, 2005 | Lihue, HI | N572TB | Incident | substantial | the pilot's inadequate compensation for the crosswind condition and failure to maintain directional control of the aircraft on landing. |
| Oct 02, 2005 | Kensington, NH | N89B | Incident | substantial | An overload fracture of the right main landing gear during the landing roll, which resulted in a nose over. |
| Jul 05, 2004 | Lansing, IL | N620CR | Incident | substantial |
The pilot's inadequate compensation for wind conditions and his failure to maintain directional control. The crosswind and the ditch were contributin…The pilot's inadequate compensation for wind conditions and his failure to maintain directional control. The crosswind and the ditch were contributing factors. |
| Sep 07, 2003 | Taos, NM | N455RT | Incident | substantial | the pilot's failure to maintain directional control during landing roll which resulted in the subsequent ground loop/swerve and impact with the ditch. |
| Apr 02, 1999 | BOCA RATON, FL | N820MM | Serious (1) | substantial |
The pilot's failure to select a suitable forced landing site following a partial loss of engine power due to failed cylinder holdddown studs, and the …The pilot's failure to select a suitable forced landing site following a partial loss of engine power due to failed cylinder holdddown studs, and the subsequent collision with trees. A factor in the accident was the reduced forward visibility from the dual open cockpits due to windshield obscuration by engine oil. |
| Jan 21, 1999 | EDMOND, OK | N19Y | Incident | substantial |
The pilot's failure to attain the proper touchdown point due to excessive airspeed and his failure to abort the landing. Factors were the pilot's exc…The pilot's failure to attain the proper touchdown point due to excessive airspeed and his failure to abort the landing. Factors were the pilot's excessive braking and the short, grass runway. |
| May 19, 1998 | SEDONA, AZ | N43064 | Serious | minor | The failure of the pilot to secure the ignition system and magnetos in the off position before asking the ground crewman to rotate the propeller. |
| Nov 08, 1997 | SEDONA, AZ | N369DP | Serious (1) | destroyed | The failure and separation of the propeller for undetermined reasons. |
| Jul 28, 1997 | LAKE BUENA VIST, FL | N14128 | Incident | substantial |
failure of maintenance personnel to follow installation procedures pertaining to the torque of the propeller retention nut, which resulted in a loose …failure of maintenance personnel to follow installation procedures pertaining to the torque of the propeller retention nut, which resulted in a loose propeller retention nut, subsequent fatigue failure of the crankshaft, and loss of engine power. The lack of suitable terrain for an emergency landing was a related factor. |
| Jun 14, 1997 | LONGVILLE, MN | N820MM | Incident | substantial | failure of the pilot to maintain directional control of the airplane. Factors relating to the accident were: the gusty wind condition and the ditch. |
| Jun 08, 1997 | OCEAN CITY, MD | N34SK | Incident | substantial |
The pilot's failure to maintain directional control and his improper compensation for the wind conditions. Contributing factors were the lack of recen…The pilot's failure to maintain directional control and his improper compensation for the wind conditions. Contributing factors were the lack of recent experience in the airplane, and gusty wind conditions. |
| Oct 24, 1996 | PUNTA GORDA, FL | N723SR | Incident | substantial | the pilot's improper flare during touchdown. |
| Feb 24, 1994 | CARLSBAD, CA | N50YM | Minor | substantial |
THE PILOT'S FAILURE TO FOLLOW THE CORRECT PROCEDURES WHEN HE RELEASED THE PARKING BRAKE. THE INADVERTENTLY ENGAGED PARKING BRAKE AND THE OUTDATED FLIG…THE PILOT'S FAILURE TO FOLLOW THE CORRECT PROCEDURES WHEN HE RELEASED THE PARKING BRAKE. THE INADVERTENTLY ENGAGED PARKING BRAKE AND THE OUTDATED FLIGHT MANUAL WERE FACTORS IN THIS ACCIDENT. |
| Nov 02, 1993 | VALPARAISO, IN | N369DP | Incident | substantial |
THE PILOT'S INADEQUATE COMPENSATION FOR WIND CONDITIONS WHILE LANDING IN A GUSTY CROSSWIND. FACTORS ASSOCIATED WITH THE ACCIDENT ARE THE GUSTY CROSSWI…THE PILOT'S INADEQUATE COMPENSATION FOR WIND CONDITIONS WHILE LANDING IN A GUSTY CROSSWIND. FACTORS ASSOCIATED WITH THE ACCIDENT ARE THE GUSTY CROSSWIND AND THE PILOT'S LACK OF EXPERIENCE IN THIS TYPE AIRPLANE. |
| Aug 28, 1991 | JAMESTOWN, RI | N44JS | Minor | substantial | THE PILOT'S IMPROPER USE OF CARBURETOR HEAT, RESULTING IN CARBURETOR ICE FORMATION AND SUBSEQUENT LOSS OF ENGINE POWER AND A FORCED LANDING IN TREES. |
| Mar 31, 1990 | MARATHON, FL | N89B | Minor | substantial |
FAILURE OF THE PILOT TO MAINTAIN DIRECTIONAL CONTROL DURING TAKEOFF, WHICH RESULTED IN AN INADVERTENT GROUND SWERVE. FACTORS RELATED TO THE ACCIDENT W…FAILURE OF THE PILOT TO MAINTAIN DIRECTIONAL CONTROL DURING TAKEOFF, WHICH RESULTED IN AN INADVERTENT GROUND SWERVE. FACTORS RELATED TO THE ACCIDENT WERE: THE CROSSWIND, THE PILOT'S EXCESSIVE COMPENSATION FOR THE WIND CONDITION, AND HIS LACK OF EXPERIENCE IN THE MAKE AND MODEL OF AIRCRAFT. |
| Apr 23, 1989 | LANSING, MI | N455RT | Incident | substantial |
PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL DURING THE LANDING ROLL, AND HIS EXCESSIVE BRAKE APPLICATION AS THE AIRCRAFT DEPARTED THE RUNWAY, WHIC…PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL DURING THE LANDING ROLL, AND HIS EXCESSIVE BRAKE APPLICATION AS THE AIRCRAFT DEPARTED THE RUNWAY, WHICH RESULTED IN THE AIRCRAFT NOSING OVER. THE PILOT'S INEXPERIENCE IN TAILDRAGGER AIRCRAFT, AND THE INADEQUATE SUPERVISION ON THE PART OF THE CHECK PILOT WERE CONTRIBUTING FACTORS. |
| Feb 03, 1989 | KEY WEST, FL | N99Y | Minor | substantial | THE INABILITY OF THE PLT TO MAINTAIN CONTROL AFTER ENCOUNTERING HIS OWN WAKE TURBULENCE AT A LOW ALTITUDE DURING A STEEP TURNING MANEUVER. |
| Oct 15, 1986 | KEY WEST, FL | N99Y | Incident | substantial | Investigation pending |