Piper PA28R Safety Record

Complete NTSB accident and incident history. 112 events recorded from 1983 to 2025.

112

All Events

59

Incidents

9

Minor

13

Serious

29

Fatal (58 fatalities)

Date Location Reg# Severity Damage Probable Cause
Sep 21, 2020 Moosic, PA N3790T Serious (1) substantial
The inadequate torquing of anchored-thru and free-thru studs during installation of the No. 2 cylinder, resulting in their fatigue fracture and subseq…

The inadequate torquing of anchored-thru and free-thru studs during installation of the No. 2 cylinder, resulting in their fatigue fracture and subsequent total loss of engine power. Contributing to the undershoot landing was the pilot’s failure to divert to closer airports than the original diversion airport after experiencing engine performance issues.

Jul 28, 2020 Houston, TX N15302 Serious (2) substantial The loss of engine power for a reason that could not be determined based on available evidence.
Nov 17, 2019 Ogden, UT N3206R Serious (2) substantial
The flight instructor’s failure to raise the landing gear using the alternate system, which resulted in a reduced climb rate and impact with an obstac…

The flight instructor’s failure to raise the landing gear using the alternate system, which resulted in a reduced climb rate and impact with an obstacle. Contributing to the accident was the flight instructor’s lack of understanding of the backup landing gear extender system.

Jun 19, 2019 Pointe-A-Pitre, FR F-ODSM Serious (1) destroyed Investigation pending
Apr 11, 2019 Meriden, CT N38658 Serious (2) substantial The loss of engine power for undetermined reasons.
Apr 03, 2019 Prairieville, LA N41AT Serious (1) minor
Installation of an incorrect engine oil drain valve, which resulted in damage to the valve during landing gear retraction and subsequent engine failur…

Installation of an incorrect engine oil drain valve, which resulted in damage to the valve during landing gear retraction and subsequent engine failure due to oil starvation. Contributing to the accident was the failure of maintenance personnel to comply with the Airworthiness Directive regarding the engine oil drain valve.

Nov 11, 2018 Lake City, FL N52737 Serious (3) substantial
The pilot's failure to attain adequate airspeed before attempting the takeoff with a tailwind, which resulted in the airplane being unable to sustain …

The pilot's failure to attain adequate airspeed before attempting the takeoff with a tailwind, which resulted in the airplane being unable to sustain flight.

Feb 19, 2017 Bayonne, NJ N15745 Serious (1) substantial
Maintenance personnel’s incorrect installation of the No. 3 cylinder’s hydraulic valve tappet plunger, which resulted in a failure of the No. 3 cylind…

Maintenance personnel’s incorrect installation of the No. 3 cylinder’s hydraulic valve tappet plunger, which resulted in a failure of the No. 3 cylinder’s intake valve and the subsequent partial loss of engine power.

Jun 12, 2016 Taylorsville, KY N42JA Serious (1) destroyed
The pilot's improper decision to continue a takeoff with a partial loss of engine power that occurred early in the takeoff roll. The reason for the pa…

The pilot's improper decision to continue a takeoff with a partial loss of engine power that occurred early in the takeoff roll. The reason for the partial loss of engine power could not be determined because postaccident fire damage to the engine precluded an examination.

Oct 10, 2015 Savannah, GA N9312N Serious (2) substantial
The pilot's inadequate preflight fuel planning and in-flight fuel management, which resulted in fuel exhaustion and a total loss of engine power durin…

The pilot's inadequate preflight fuel planning and in-flight fuel management, which resulted in fuel exhaustion and a total loss of engine power during approach. Contributing to the accident were the pilot’s failure to maintain adequate airspeed and his exceedance of the airplane’s critical angle-of-attack, which resulted in an aerodynamic stall.

Mar 26, 2000 LEHIGHTON, PA N55820 Serious (1) destroyed The pilot's inadequate compensation for the crosswind. A factor in this accident was the gusty crosswind condition.
Sep 12, 1997 RENO, NV N69645 Serious (4) substantial
The pilot's failure to maintain an adequate airspeed during a go-around, which resulted in an inadvertent stall/mush. Factors in the accident were: th…

The pilot's failure to maintain an adequate airspeed during a go-around, which resulted in an inadvertent stall/mush. Factors in the accident were: the pilot's lack of qualification in the aircraft; the FAA pilot certification system's failure to transfer the medical limitations imposed on the pilot to his private pilot certificate; the pilot's inadequate preflight and in-flight fuel planning/decisions that caused the aircraft to arrive with a critically low fuel state, which resulted in a momentary loss of power due to an unporting of the fuel tank supply pickup at a critical time in the go-around; and, the maintenance facilities' failure to properly connect the landing gear indicator circuit breaker to the bus pane.

Mar 13, 1988 BULLHEAD CITY, AZ N694ME Serious (2) substantial Investigation pending
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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