North American Navion Safety Record
Complete NTSB accident and incident history. 49 events recorded from 1982 to 2024.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Oct 05, 2018 | Stonewall, MS | N969TR | Incident | substantial | The fatigue failure of the No. 3 cylinder exhaust valve, which resulted in a fractured camshaft and a total loss of engine power. |
| Aug 27, 2017 | Fortuna, CA | N8695H | Incident | substantial |
A total loss of engine power for reasons that could not be determined because postaccident examination of the engine revealed no evidence of any preac…A total loss of engine power for reasons that could not be determined because postaccident examination of the engine revealed no evidence of any preaccident mechanical malfunctions or failures that would have that would have precluded normal operation. |
| Oct 05, 2016 | Palmer, AK | N8895H | Incident | substantial | The pilot's failure to extend the landing gear for landing. |
| Aug 29, 2016 | Monett, MO | N91488 | Incident | substantial | Maintenance personnel’s failure to properly rig the right main landing gear locking mechanism, which resulted in a gear collapse during landing. |
| Jun 24, 2016 | Alamogordo, NM | N91137 | Incident | substantial | The failure of the No. 5 exhaust valve key spring, which resulted in a total loss of engine power. |
| Jun 16, 1999 | OSCEOLA, WI | N109F | Incident | substantial |
the pilot's mismanagement of the fuel system in that he had the fuel selector positioned to a tank which did not contain sufficient fuel for the fligh…the pilot's mismanagement of the fuel system in that he had the fuel selector positioned to a tank which did not contain sufficient fuel for the flight. Factors associated with the accident were the crop and the ditch which the airplane encountered during the forced landing. |
| Jun 26, 1998 | SAN ANDREAS, CA | N1400Z | Incident | substantial | The pilot's improper reinstallation of the fuel selector valve handle, which led to the selection of the wrong fuel tank and fuel starvation. |
| May 18, 1997 | MORRISTOWN, AZ | N8551H | Incident | substantial |
failure to replace an old and abraded oil feedline hose which led to its rupture and the in-flight loss of engine oil pressure. A related factor was …failure to replace an old and abraded oil feedline hose which led to its rupture and the in-flight loss of engine oil pressure. A related factor was the pilot's misjudgment of distance-to-go versus altitude remaining during the subsequent forced landing. |
| Jun 09, 1992 | SPOKANE, WA | N91132 | Incident | substantial | THE PARTIAL FAILURE OF THE NOSE GEAR TRUNNION. FACTORS INCLUDE THE PILOT'S DECISION TO LAND WITH THE GEAR IN THE UP POSITION. |
| Oct 20, 1991 | LAKE GENEVA, WI | N10JF | Incident | substantial | FATIGUE FAILURE OF THE CRANKSHAFT. A FACTOR IN THE ACCIDENT WAS INADEQUATE QUALITY CONTROL BY OTHER MAINTENANCE PERSONNEL. |
| Oct 20, 1991 | DENISON, TX | N8560H | Incident | substantial | THE EXCEEDING OF THE AIRPLANE'S TAKEOFF PERFORMANCE CAPABILITY BY THE PILOT'S INADEQUATE PREFLIGHT PREPARATION.. |
| Jan 20, 1990 | APPLE VALLEY, CA | N727G | Incident | substantial | THE PILOT FAILED TO PROPERLY PREFLIGHT THE AIRPLANE AND DEPARTED ON THE ACCIDENT FLIGHT WITH MINIMAL FUEL. |
| Aug 08, 1987 | CHILLICOTHE, MO | N8569H | Incident | substantial | Investigation pending |
| May 31, 1987 | DEFUNIAK SPRING, FL | N4007K | Incident | substantial | Investigation pending |
| Apr 03, 1987 | LOS ALAMOS, NM | N91735 | Incident | substantial | Investigation pending |
| Jun 16, 1986 | SAN JOSE, CA | N91608 | Incident | substantial | Investigation pending |
| Oct 05, 1985 | TALLAHASSEE, FL | N4007K | Incident | substantial | Investigation pending |
| Jun 30, 1985 | COOPER CITY, FL | N8784H | Incident | substantial | Investigation pending |
| Jul 28, 1984 | ATIGUN PASS, AK | N225G | Incident | substantial | Investigation pending |