Mooney M20 Safety Record
Complete NTSB accident and incident history. 1232 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Aug 31, 2003 | Watsonville, CA | N707JH | Serious (3) | substantial |
the non-instrument rated pilot's intentional continuance of VFR flight into instrument meteorological conditions and failure to maintain clearance wit…the non-instrument rated pilot's intentional continuance of VFR flight into instrument meteorological conditions and failure to maintain clearance with terrain. |
| Jul 06, 2003 | Leadville, CO | N37JK | Serious (1) | substantial |
the pilot's inadequate compensation for wind conditions and his failure to attain adequate airspeed resulting in an inadvertent stall/mush. Contributi…the pilot's inadequate compensation for wind conditions and his failure to attain adequate airspeed resulting in an inadvertent stall/mush. Contributing factors were the wind shear, runway light, fence post, and unsuitable terrain. |
| Apr 11, 2003 | West Milford, NJ | N231LS | Serious (1) | substantial |
The pilot's inadequate compensation for the crosswind and his failure to maintain directional control. Factors in the accident were the crosswind and…The pilot's inadequate compensation for the crosswind and his failure to maintain directional control. Factors in the accident were the crosswind and landing at night. |
| Apr 01, 2003 | Lakeland, FL | N2652W | Serious | minor |
The inadequate visual lookout of the pilot and the ground marshaller resulting in the ground marshaller being struck by the wing of the taxiing airpla…The inadequate visual lookout of the pilot and the ground marshaller resulting in the ground marshaller being struck by the wing of the taxiing airplane and receiving serious injury. |
| Mar 02, 2003 | Destin, FL | N101PB | Serious (1) | substantial |
The inadequate annual/100-hour inspection of the engine by the mechanic for his failure to properly secure the tailpipe assembly to the turbocharger r…The inadequate annual/100-hour inspection of the engine by the mechanic for his failure to properly secure the tailpipe assembly to the turbocharger resulting in separation of the tailpipe and subsequent in-flight fire. Contributing factors in the accident were the inadequate design of the plastic brake line in the cockpit adjacent to the firewall by the airplane manufacturer, and the inadequate certification of the airplane by the FAA for failure to take into account radiant heat when designing components aft of the firewall. |
| Sep 16, 2002 | Canadaigua, NY | N201ZC | Serious (1) | substantial | The pilot's inadequate preflight inspection of the airplane, which resulted in a loss of engine power due to fuel contamination. |
| Aug 14, 2002 | Newberg, OR | N1024Z | Serious (1) | substantial | The pilot's inadequate flare and his delay in executing an aborted landing. A contributing factor was the dark night conditions. |
| Jun 20, 2002 | Hagerstown, MD | N3282F | Serious (2) | substantial |
The pilot's failure to perform a go-around and obtain the proper touchdown point, which resulted in an overrun. A factor in the accident was the cros…The pilot's failure to perform a go-around and obtain the proper touchdown point, which resulted in an overrun. A factor in the accident was the crosswind condition. |
| Jun 08, 2002 | Placerville, CA | N1285X | Serious (1) | substantial | A loss of engine power due to the pilot's inadequate in-flight planning/decision which led to fuel exhaustion. |
| Mar 21, 2001 | Gresham, OR | N8346E | Serious (1) | substantial | The pilot's inadequate decision in which he failed to refuel while en route, resulting in fuel exhaustion and loss of engine power. |
| Jan 13, 2001 | Somerset, MA | N1398W | Serious (1) | substantial | The pilot's inadequate visual lookout. A factor was the dusk lighting conditions. |
| Jun 04, 2000 | CARSON CITY, NV | N201CE | Serious (4) | substantial |
a loss of engine power due to contamination of the fuel system resulting in partial blockage of the cylinder number 2 fuel injection nozzle. A factor…a loss of engine power due to contamination of the fuel system resulting in partial blockage of the cylinder number 2 fuel injection nozzle. A factor in the accident was the high density altitude. |
| May 31, 2000 | GRT BARRINGTON, MA | N1154K | Serious (1) | substantial |
The pilot's failure to perform a go around and his inadequate recovery from a bounced landing. Factors in the accident were the pilot's s failure to …The pilot's failure to perform a go around and his inadequate recovery from a bounced landing. Factors in the accident were the pilot's s failure to maintain the proper glide path and to reach the proper touchdown point. |
| Nov 28, 1999 | HILLSBORO, TX | N6766U | Serious (1) | substantial | The pilot's failure to maintain directional control of the airplane during the go-around. A factor was the gust of wind. |
| Aug 20, 1999 | LAKEPORT, CA | N6022Q | Serious (1) | substantial |
The failure of engine shop maintenance personnel to tighten the fuel line fitting during assembly of the engine, and failure of the installing mainten…The failure of engine shop maintenance personnel to tighten the fuel line fitting during assembly of the engine, and failure of the installing maintenance personnel to detect and tighten the loose fitting during the engine installation and annual inspection. |
| Aug 15, 1999 | PRATTSBURG, NY | N3243F | Serious (2) | destroyed |
Propeller blade separation, resulting from fatigue cracking initiated by intergranular corrosion. A factor was the lack of propeller blade corrosion …Propeller blade separation, resulting from fatigue cracking initiated by intergranular corrosion. A factor was the lack of propeller blade corrosion inspection requirements. |
| Aug 07, 1999 | GAINESVILLE, MO | N11652 | Serious (2) | destroyed |
the inadequate preflight planning/preparation by the pilot and all available runway exceeded by the pilot. The trees and power lines were contributin…the inadequate preflight planning/preparation by the pilot and all available runway exceeded by the pilot. The trees and power lines were contributing factors. |
| Jul 31, 1999 | MONTROSE, CO | N9390V | Serious (1) | substantial | The pilot's inadequate preflight planning and preparation and his failure to maintain clearance from the signpost. A factor was the signpost. |
| Apr 07, 1999 | VIENNA, IL | N9969X | Serious (2) | destroyed | The worn ignition points/cam follower assembly, and uneven landing terrain. |
| Nov 19, 1998 | UPLAND, CA | N3500X | Serious (1) | destroyed |
Loss of engine power due to water contaminated fuel and the pilot's inadequate preflight inspection of the airplane. A factor was the failure of the …Loss of engine power due to water contaminated fuel and the pilot's inadequate preflight inspection of the airplane. A factor was the failure of the owner/pilot to properly maintain the airplane. |
| Oct 21, 1998 | ENGLEWOOD, CO | N6405U | Serious (1) | substantial |
The undertorquing of the camshaft gear retaining bolts during engine overhaul by maintenance personnel. A factor was the unsuitable terrain for a for…The undertorquing of the camshaft gear retaining bolts during engine overhaul by maintenance personnel. A factor was the unsuitable terrain for a forced landing. |
| Aug 07, 1998 | MARATHON, FL | N8385E | Serious (2) | substantial |
The inadequate inspection of the fuel pump during the last engine overhaul, that subsequently resulted in a worn diaphragm, fuel venting overboard, an…The inadequate inspection of the fuel pump during the last engine overhaul, that subsequently resulted in a worn diaphragm, fuel venting overboard, and loss of engine power from fuel exhaustion during a critical phase of flight. |
| Feb 08, 1998 | DAVIS, WV | N4120H | Serious (1) | substantial | A loss of power due to blockage of the fuel screen and one of the four fuel injector nozzles. A contributing factor was snow covered terrain. |
| Dec 20, 1997 | SAFFORD, AZ | N2965L | Serious (2) | destroyed |
The pilot's poor in-flight judgement and intentional flight into known adverse weather conditions. Related factors were, mountainous terrain, rain an…The pilot's poor in-flight judgement and intentional flight into known adverse weather conditions. Related factors were, mountainous terrain, rain and fog. |
| Oct 19, 1997 | COLLEGE STATION, TX | N7433V | Serious (2) | substantial |
The pilot's failure to maintain airspeed during a go-around. Factors were :the pilot's premature retraction of the flaps, his lack of total experience…The pilot's failure to maintain airspeed during a go-around. Factors were :the pilot's premature retraction of the flaps, his lack of total experience in the airplane, the dark night illumination, pilot fatigue, and pressure induced by the passengers to complete the night flight. |