Mooney M20 Safety Record
Complete NTSB accident and incident history. 1232 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Mar 19, 2014 | Lamar, CO | N201VA | Serious (1) | substantial | The pilot allowed the airplane to liftoff without sufficient airspeed which resulted in a stall and subsequent impact with the terrain. |
| Oct 08, 2013 | Sedona, AZ | N5760Y | Serious (2) | substantial | The pilot's inadequate flare which resulted in a bounced landing and subsequent loss of aircraft control during an aborted landing. |
| Mar 12, 2013 | Middletown, OH | N199Q | Serious (1) | substantial |
The total loss of engine power due to fuel exhaustion, which resulted from the noncurrent pilot’s improper in-flight fuel management and decision-maki…The total loss of engine power due to fuel exhaustion, which resulted from the noncurrent pilot’s improper in-flight fuel management and decision-making and his decision to conduct the flight after consuming alcohol. |
| Aug 26, 2012 | East Hampton, NY | N557M | Serious (2) | substantial |
A loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any failures or malfunct…A loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any failures or malfunctions that would have precluded normal operation. |
| Jul 21, 2012 | Oshkosh, WI | N339PB | Serious (1) | substantial | The pilot’s excessive airspeed at touchdown and his loss of control of the airplane during the landing roll. |
| Jul 09, 2012 | Scottsdale, AZ | N137MP | Serious (1) | substantial |
The pilot's failure to maintain airplane control during an aborted landing, and the flight instructor’s delayed remedial action. Contributing to the a…The pilot's failure to maintain airplane control during an aborted landing, and the flight instructor’s delayed remedial action. Contributing to the accident were the pilot’s improper landing flare, which resulted in a bounced landing, and his premature flap retraction while performing a go-around maneuver. |
| Jun 28, 2012 | Mc Kinnon, TN | N174JB | Serious (1) | substantial |
The separation of the piston connecting rod from the crankshaft due to inadequate installation from a mechanic, resulting in a total loss of engine po…The separation of the piston connecting rod from the crankshaft due to inadequate installation from a mechanic, resulting in a total loss of engine power. |
| Jun 12, 2012 | Hooker, OK | N6455Q | Serious (2) | substantial |
The pilot’s loss of airplane control after a partial loss of engine power for reasons that could not be determined because postaccident examination of…The pilot’s loss of airplane control after a partial loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures, which resulted in an aerodynamic stall. Contributing to the accident was the pilot’s impairment as a result of his recent use of illicit drugs. |
| Apr 19, 2012 | McKinnon, TN | N9722M | Serious (3) | substantial |
The pilot's delayed decision to go-around after failing to recognize that he was attempting to land with a tailwind, and his failure to retract the la…The pilot's delayed decision to go-around after failing to recognize that he was attempting to land with a tailwind, and his failure to retract the landing gear and wing flaps for the go-around, which resulted in a collision with trees and terrain near the departure end of the runway. |
| Mar 24, 2012 | Bloomfield, IN | N201QB | Serious (2) | substantial |
The pilot's failure to land with sufficient runway remaining to stop, which resulted in an unsuccessful aborted landing, inadvertent stall, and collis…The pilot's failure to land with sufficient runway remaining to stop, which resulted in an unsuccessful aborted landing, inadvertent stall, and collision with terrain. |
| Mar 03, 2012 | Amisville, VA | N486KC | Serious (2) | substantial | A total loss of engine power during cruise flight for reasons that could not be determined because of the damage due to the postcrash fire. |
| May 10, 2011 | Ravenna, OH | N9149R | Serious (3) | substantial | The pilot's improper fuel management, which resulted in a loss of engine power due to fuel starvation. |
| Dec 11, 2010 | Chino, CA | N4326H | Serious (1) | substantial |
The student pilot's failure to properly position the flaps for the takeoff, failure to maintain airplane control during the procedure, and the flight …The student pilot's failure to properly position the flaps for the takeoff, failure to maintain airplane control during the procedure, and the flight instructor's delayed remedial action. |
| Nov 03, 2009 | Fairview, NC | N6896U | Serious (2) | substantial | A total loss of engine power due to fuel exhaustion as a result of the pilot’s inadequate preflight fuel planning. |
| Aug 03, 2009 | Suffolk, VA | N3549N | Serious (1) | substantial |
A loss of engine power due to fuel exhaustion as a result of the pilot’s failure to accurately calculate the fuel required for the flight. Contributin…A loss of engine power due to fuel exhaustion as a result of the pilot’s failure to accurately calculate the fuel required for the flight. Contributing to the accident was a malfunction of the fuel quantity indicators. |
| Dec 13, 2008 | Sebastian, FL | N6871N | Serious (1) | substantial | The loss of engine power for undetermined reasons. |
| Jul 07, 2008 | Big Creek, ID | N5652Q | Serious (2) | substantial |
The pilot's delayed decision to abort the landing and failure to achieve the proper touchdown point. Contributing to the accident was a high density …The pilot's delayed decision to abort the landing and failure to achieve the proper touchdown point. Contributing to the accident was a high density altitude. |
| Dec 16, 2007 | Phillipsburg, KS | N63LH | Serious (1) | destroyed |
Total loss of engine power due to contamination of the carburetor, total blockage of the fuel inlet screen, and partial blockage of the fuel lines and…Total loss of engine power due to contamination of the carburetor, total blockage of the fuel inlet screen, and partial blockage of the fuel lines and fittings. Contributing to the accident were the dark night light conditions and the trees. |
| May 23, 2006 | Blacksburg, SC | N3217F | Serious (2) | destroyed |
The pilot's failure to abort the takeoff after the airplane failed to achieve adequate airspeed on the takeoff roll for undetermined reasons. This res…The pilot's failure to abort the takeoff after the airplane failed to achieve adequate airspeed on the takeoff roll for undetermined reasons. This resulted in an abrupt pull up, inadvertent stall, and in flight collision with wires, trees and the ground. |
| May 18, 2006 | Lantana, FL | N12RH | Serious (2) | substantial |
The pilot's inadequate preflight inspection, which resulted in a loss of engine power during initial climb due to water contamination in the fuel. Con…The pilot's inadequate preflight inspection, which resulted in a loss of engine power during initial climb due to water contamination in the fuel. Contributing factors were the deteriorated fuel cap o-ring and the pilot's failure to maintain adequate airspeed. |
| Feb 17, 2006 | Willits, CA | N9704M | Serious (2) | substantial |
The pilot's failure to maintain visual contact with the runway at night, which resulted in a descent below the proper glide path and a collision with …The pilot's failure to maintain visual contact with the runway at night, which resulted in a descent below the proper glide path and a collision with a tree. Also causal was the flight instructor's inadequate supervision of the flight. |
| Jun 26, 2005 | Hailey, ID | N201U | Serious (1) | substantial | The pilot's failure to maintain aircraft control while on final approach for undetermined reasons. |
| Jun 13, 2005 | Jefferson City, MO | N231HX | Serious (1) | substantial |
The pilot's delay in diverting to an alternate destination due to low fuel indications which led to the fuel exhaustion, loss of engine power and the …The pilot's delay in diverting to an alternate destination due to low fuel indications which led to the fuel exhaustion, loss of engine power and the subsequent forced landing. Factors were the pilot's improper preflight inspection which resulted in an undetected fuel drain leak and his misjudged glidepath during the precautionary landing which led to a go-around and the subsequent fuel exhaustion. |
| Jun 10, 2004 | Golden, MO | N3911N | Serious (1) | substantial | The pilot's failure to maintain directional control and his failure to maintain clearance from the trees. The trees were a contributing factor. |
| Sep 09, 2003 | Rockford, OH | N1072B | Serious (1) | destroyed |
The pilot's failure to maintain the proper altitude/clearance, which resulted in an in-flight collision with a utility wire. The owner's improper dec…The pilot's failure to maintain the proper altitude/clearance, which resulted in an in-flight collision with a utility wire. The owner's improper decision to allow the airplane to be operated by an uncertificated pilot was also causal. |