Mooney M20 Safety Record

Complete NTSB accident and incident history. 1232 events recorded from 1982 to 2025.

1232

All Events

546

Incidents

193

Minor

137

Serious

353

Fatal (633 fatalities)

Date Location Reg# Severity Damage Probable Cause
Apr 21, 1995 MARSHFIELD, MA N252DX Incident substantial
the pilot misjudged the flare, resulting in a bounced landing and impact with the terrain. A factor in this accident was an improper recovery from a …

the pilot misjudged the flare, resulting in a bounced landing and impact with the terrain. A factor in this accident was an improper recovery from a bounced landing.

Apr 03, 1995 TIJERAS, NM N4478H Incident substantial
FUEL STARVATION DUE TO FOREIGN MATERIAL PARTIALLY BLOCKING THE FUEL SCREEN, AND THE PILOT'S FAILURE TO SWITCH FUEL TANKS. A FACTOR WAS THE LACK OF SUI…

FUEL STARVATION DUE TO FOREIGN MATERIAL PARTIALLY BLOCKING THE FUEL SCREEN, AND THE PILOT'S FAILURE TO SWITCH FUEL TANKS. A FACTOR WAS THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING.

Mar 03, 1995 OMAK, WA N7836V Incident substantial
THE ELEVATOR PUSH ROD SEPARATION DUE TO FATIGUE. FACTORS CONTRIBUTING TO THE ACCIDENT WERE THE PILOT IN COMMAND'S FAILURE TO INSURE COMPLIANCE WITH TH…

THE ELEVATOR PUSH ROD SEPARATION DUE TO FATIGUE. FACTORS CONTRIBUTING TO THE ACCIDENT WERE THE PILOT IN COMMAND'S FAILURE TO INSURE COMPLIANCE WITH THE AIRWORTHINESS DIRECTIVE AND THE FROZEN PUSH ROD BEARING.

Feb 23, 1995 MCLAIN, MS N7142U Incident substantial
THE IMPROPER REASSEMBLY OF THE SERVO FUEL INJECTOR DURING OVERHAUL BY MAINTENANCE PERSONNEL. THIS RESULTED IN A TOTAL LOSS OF ENGINE POWER DURING CRU…

THE IMPROPER REASSEMBLY OF THE SERVO FUEL INJECTOR DURING OVERHAUL BY MAINTENANCE PERSONNEL. THIS RESULTED IN A TOTAL LOSS OF ENGINE POWER DURING CRUISE FLIGHT DUE TO FUEL STARVATION, FORCED LANDING, AND SUBSEQUENT ON-GROUND COLLISION WITH A FIXED OBJECT DURING LANDING ROLL OUT.

Dec 28, 1994 MINNEAPOLIS, MN N3983H Incident substantial
the pilot's misjudging of distance and airspeed during the approach to landing which resulted in an overrun. Factors associated with the accident wer…

the pilot's misjudging of distance and airspeed during the approach to landing which resulted in an overrun. Factors associated with the accident were the separation of the exhaust pipe and the pilot's not understanding communications from the air traffic control tower.

Dec 27, 1994 HUBER HEIGHTS, OH N201JT Incident substantial
The pilot's inadequate inflight decision/planning, which resulted in fuel exhaustion and the loss of engine power. A factor is the pilot's inadequate…

The pilot's inadequate inflight decision/planning, which resulted in fuel exhaustion and the loss of engine power. A factor is the pilot's inadequate preflight planning.

Dec 20, 1994 SPANISH CAY, BF N201TB Incident substantial Investigation pending
Oct 21, 1994 GREELEY, CO N6958V Incident substantial INADVERTENT LANDING GEAR RETRACTION BY THE PILOT FLYING THE AIRCRAFT. A FACTOR WAS INADEQUATE SUPERVISION BY THE FLIGHT INSTRUCTOR.
Sep 22, 1994 CHAMBLEE, GA N97136 Incident substantial
THE PILOT'S IMPROPER FLARE THAT RESULTED A IN HARD LANDING, FOLLOWED BY HIS IMPROPER RECOVERY FROM A BOUNCED LANDING, AND HIS FAILURE TO MAINTAIN DIRE…

THE PILOT'S IMPROPER FLARE THAT RESULTED A IN HARD LANDING, FOLLOWED BY HIS IMPROPER RECOVERY FROM A BOUNCED LANDING, AND HIS FAILURE TO MAINTAIN DIRECTIONAL CONTROL DURING THE ATTEMPTED GO- AROUND.

Sep 14, 1994 PLYMOUTH, MI N6944U Incident substantial the pilot's improper (maintenance) modification and his initiating an operation with known deficiencies in equipment
Jul 27, 1994 MACON, MO N6327Q Incident substantial
the student pilot's decision to land on a closed runway under construction. A factor associated with the accident is the partial loss of engine power…

the student pilot's decision to land on a closed runway under construction. A factor associated with the accident is the partial loss of engine power for an undetermined reason.

Jun 20, 1994 BIG BEAR, CA N201NK Incident substantial a loss of engine power from a malfunctioning magneto due to a loose oil seal in an overhauled magneto.
Jun 18, 1994 LEESBURG, VA N6679U Incident substantial
THE PILOT'S FAILURE TO MAINTAIN THE MINIMUM DESCENT ALTITUDE UNTIL THE PUBLISHED APPROACH FIX. FACTORS RELATED TO THE ACCIDENT WAS PILOT FATIGUE, LOW…

THE PILOT'S FAILURE TO MAINTAIN THE MINIMUM DESCENT ALTITUDE UNTIL THE PUBLISHED APPROACH FIX. FACTORS RELATED TO THE ACCIDENT WAS PILOT FATIGUE, LOW CEILINGS, OBSCURATION, AND FOG.

Jun 09, 1994 WAMSUTTER, WY N711LP Incident substantial CLEARANCE NOT MAINTAINED. A FACTOR TO THE ACCIDENT WAS: TRANSMISSION WIRE.
May 27, 1994 OMAHA, NE N6942U Incident substantial
inaccurate fuel consumption calculations and the inadequate fuel supply for the flight. Factors related to the accident were the ditch and the quanti…

inaccurate fuel consumption calculations and the inadequate fuel supply for the flight. Factors related to the accident were the ditch and the quantity gage which gave a false indication.

May 27, 1994 APALACHICOLA, FL N201NH Incident substantial
THE PILOT'S INADEQUATE COMPENSATION FOR THE CROSSWIND RESULTING IN NOT MAINTAINING ALIGNMENT WITH THE RUNWAY AND THE PILOT'S DELAY IN ABORTING THE LAN…

THE PILOT'S INADEQUATE COMPENSATION FOR THE CROSSWIND RESULTING IN NOT MAINTAINING ALIGNMENT WITH THE RUNWAY AND THE PILOT'S DELAY IN ABORTING THE LANDING. THE CROSSWIND WAS A FACTOR.

May 26, 1994 WILLCOX, AZ N50105 Incident substantial
THE FAILURE OF THE CONNECTING ROD DUE TO LACK OF LUBRICATION. FACTORS WERE THE PREVIOUS DAMAGE TO THE ENGINE, AND THE UNSUITABLE TERRAIN AT THE PILOT'…

THE FAILURE OF THE CONNECTING ROD DUE TO LACK OF LUBRICATION. FACTORS WERE THE PREVIOUS DAMAGE TO THE ENGINE, AND THE UNSUITABLE TERRAIN AT THE PILOT'S DISPOSAL FOR THE FORCED LANDING.

Apr 05, 1994 DAYTONA BEACH, FL N187ER Incident substantial COLLAPSE OF THE LEFT MAIN LANDING GEAR FOR UNKNOWN REASONS.
Mar 25, 1994 MUSCLE SHOALS, AL N4780H Incident substantial
WAS THE LOOSE THROTTLE CABLE, AND THE PILOT'S FAILURE TO ABORT THE TAKEOFF WHEN THE ENGINE DID NOT PRODUCE FULL POWER. A FACTOR WAS THE INADEQUATE MAI…

WAS THE LOOSE THROTTLE CABLE, AND THE PILOT'S FAILURE TO ABORT THE TAKEOFF WHEN THE ENGINE DID NOT PRODUCE FULL POWER. A FACTOR WAS THE INADEQUATE MAINTENANCE INSPECTION OF THE ENGINE.

Mar 10, 1994 RICHLAND CENTER, WI N6811N Incident substantial improper use of carburetor heat. Factors related to the accident were carburetor icing conditions, and the sign and fence poles.
Feb 24, 1994 GALLUP, NM N201SX Incident substantial
THE LOSS OF ENGINE POWER DUE TO THE FAILURE OF THE NUMBER 3 EXHAUST VALVE. A FACTOR WAS THE LACK OF SUITABLE TERRAIN AVAILABLE TO EXECUTE THE FORCED L…

THE LOSS OF ENGINE POWER DUE TO THE FAILURE OF THE NUMBER 3 EXHAUST VALVE. A FACTOR WAS THE LACK OF SUITABLE TERRAIN AVAILABLE TO EXECUTE THE FORCED LANDING.

Sep 02, 1993 DAYTONA BEACH, FL N191ER Incident substantial CONTAMINATION/BLOCKAGE OF THE FUEL INJECTION CONTROL SYSTEM.
Aug 28, 1993 KELLEY'S ISLAND, OH N202WB Incident substantial
The pilot's failure to maintain adequate airspeed which resulted in an inadvertent stall. A factor was the pilot's inadequate handling of the airplan…

The pilot's failure to maintain adequate airspeed which resulted in an inadvertent stall. A factor was the pilot's inadequate handling of the airplane.

Aug 24, 1993 LANDOVER, MD N74580 Incident substantial
FATIGUE FAILURE OF A PROPELLER BLADE, WHICH RESULTED IN SEVERE ENGINE VIBRATION AND SUBSEQUENT DAMAGE TO THE AIRPLANE. THE LACK OF SUITABLE TERRAIN FO…

FATIGUE FAILURE OF A PROPELLER BLADE, WHICH RESULTED IN SEVERE ENGINE VIBRATION AND SUBSEQUENT DAMAGE TO THE AIRPLANE. THE LACK OF SUITABLE TERRAIN FOR A FORCED LANDING WAS A RELATED FACTOR.

Aug 06, 1993 KING CITY, CA N1153K Incident substantial the pilot's loss of directional control during the takeoff ground roll due to the inadvertent interference with the controls by a passenger.
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
← Mooney M20 For Sale All Mooney Models
Data source: NTSB Aviation Accident Database · About our data