Cessna Safety Record
Complete NTSB accident and incident history. 28016 events recorded from 1974 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Mar 16, 2000 | FORT LAUDERDALE, FL | N251RS | Minor | substantial |
Separation of the right main landing gear tire recap during takeoff resulting in the pilot's loss of directional control, the aircraft departing the r…Separation of the right main landing gear tire recap during takeoff resulting in the pilot's loss of directional control, the aircraft departing the runway, collapse of the landing gear, and collision with the airport fence. |
| Mar 14, 2000 | RIFLE, CO | N8236M | Minor | substantial | Loss of engine power for undetermined reasons. A factor was unsuitable terrain on which to make a forced landing. |
| Mar 10, 2000 | DELTA JUNCTION, AK | N75703 | Minor | substantial |
The disintegration of the number two piston. A factor in this accident was the subsequent metal fouling of the spark plugs, which resulted in total l…The disintegration of the number two piston. A factor in this accident was the subsequent metal fouling of the spark plugs, which resulted in total loss of engine power. |
| Mar 07, 2000 | MANILLA, AR | N20179 | Minor | substantial | The pilot's performance of low altitude flight and his failure to maintain clearance with the power lines. |
| Mar 07, 2000 | INCLINE VILLAGE, NV | N4021Y | Minor | substantial | The pilot's inadvertent landing on water with the wheels of the amphibious float plane extended. |
| Mar 02, 2000 | MACOMB, IL | N9552T | Minor | substantial |
the inadequate maintenance inspection prior to the ferry flight by the pilot/mechanic rated passenger who endorsed the airplane as airworthy, the shif…the inadequate maintenance inspection prior to the ferry flight by the pilot/mechanic rated passenger who endorsed the airplane as airworthy, the shift in the number two main bearing left half, and the fractured crankshaft. A factor was the rough/uneven terrain and the ferry permit's procedures not followed by the pilot in command. |
| Feb 19, 2000 | WEIR, TX | N76190 | Minor | substantial | The delayed aborted takeoff by the pilot. Factors were the pilot's intentional ground loop/swerve and the tail wind. |
| Feb 08, 2000 | GLENDALE, AZ | N4946U | Minor | substantial |
the pilot's attempt to go-around with inadequate altitude and airspeed available, resulting in a power demand that exceeded the capability of the airc…the pilot's attempt to go-around with inadequate altitude and airspeed available, resulting in a power demand that exceeded the capability of the aircraft. The fully extended gear and flaps were factors in this accident. |
| Feb 08, 2000 | ENGLEWOOD, FL | N6630F | Minor | substantial |
The failure of the pilot to retract the flaps from the fully extended position following the last landing resulting in the failure to maintain airspee…The failure of the pilot to retract the flaps from the fully extended position following the last landing resulting in the failure to maintain airspeed and subsequent descent for a forced landing. A contributing factor in the accident was the pilot's disregard for the wind direction resulting in a 12 knot tailwind on departure. |
| Feb 07, 2000 | LOVELAND, CO | N721 | Minor | substantial | Failure of the pilot in command to maintain directional control, resulting in an inadvertent ground loop. A factor was the crosswind. |
| Jan 26, 2000 | OKLAHOMA CITY, OK | N7VS | Minor | substantial | The failure of the pilot to deice the airplane prior to departure. |
| Jan 17, 2000 | LIBERAL, KS | N12654 | Minor | substantial |
the pilot not maintaining proper glidepath on the ILS approach, the pilot's improper decision to continue the approach below the glidepath, and the pi…the pilot not maintaining proper glidepath on the ILS approach, the pilot's improper decision to continue the approach below the glidepath, and the pilot's failure to perform a missed approach. Factors relating to the accident were the low ceiling and visibility, and the fog. |
| Jan 02, 2000 | DOS PALOS, CA | N7249T | Minor | substantial |
A partial loss of engine power due to the failure of maintenance personnel to properly install and safety the throttle arm to the carburetor throttle …A partial loss of engine power due to the failure of maintenance personnel to properly install and safety the throttle arm to the carburetor throttle shaft. |
| Dec 24, 1999 | BETHEL, AK | N1864 | Minor | substantial | The pilot's failure to remove frost from the airplane prior to flight, and an inadvertent stall/mush. |
| Dec 17, 1999 | CONCORD, CA | N738UA | Minor | substantial | the pilot's failure to use a checklist and remove the control gust lock. |
| Dec 15, 1999 | WOODVILLE, FL | N460TC | Minor | substantial | The pilot's improper preflight planning resulting in loss of engine power due to fuel exhaustion and the collision with trees during a forced landing. |
| Dec 12, 1999 | SPRINGHILL, LA | N739ST | Minor | substantial |
The pilot's inadequate compensation for the wind conditions, which resulted in a loss of aircraft control. Factors were the gusty winds, and the pilo…The pilot's inadequate compensation for the wind conditions, which resulted in a loss of aircraft control. Factors were the gusty winds, and the pilot's inadequate weather evaluation. |
| Dec 05, 1999 | CLARKSVILLE, MD | N5260S | Minor | substantial | Deer that entered the runway environment while the pilot was executing a takeoff. |
| Dec 04, 1999 | PORT TOWNSEND, WA | N1936V | Minor | substantial | Compensation for wind conditions was inadequate. Gusting wind conditions were a factor. |
| Nov 23, 1999 | GREENFIELD, IN | N65668 | Minor | substantial | The student pilot not maintaining aircraft control. A contributing factor was the student's aural perception. |
| Nov 16, 1999 | DILLINGHAM, AK | N9933M | Minor | substantial | Failure of the pilot to remove frost from the wings prior to flight, and the resulting inadvertent stall/mush. |
| Nov 07, 1999 | ROCHESTER, IN | N8235M | Minor | substantial | the pilot did not obtain the proper touchdown point. Factors included the closed runway and the culvert. |
| Oct 31, 1999 | BENTON, KS | N759NT | Minor | substantial |
the pilot's failure to maintain aircraft control, and the physiological impairment of the pilot due to a brain anomaly. The pilots improper decision …the pilot's failure to maintain aircraft control, and the physiological impairment of the pilot due to a brain anomaly. The pilots improper decision to operate the airplane with a known medical deficiency, and the ditch were contributing factors. |
| Oct 29, 1999 | BAY SPRINGS, MS | N6444F | Minor | substantial | The pilot's failure to maintain flying speed that resulted in a loss of control and stall. A factor was a stuck exhaust valve. |
| Oct 29, 1999 | PINEVILLE, LA | N5301E | Minor | substantial | The student pilot's misjudgment of distance/speed during approach resulting in his failure to attain the proper touchdown point. |