Cessna Safety Record
Complete NTSB accident and incident history. 28016 events recorded from 1974 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Feb 10, 2019 | Arlington, WA | N9101X | Incident | substantial |
The pilot's distraction during the engine warm-up, which resulted in the airplane's collision with a hangar. Contributing to the accident was the pilo…The pilot's distraction during the engine warm-up, which resulted in the airplane's collision with a hangar. Contributing to the accident was the pilot's failure to set the brakes. |
| Feb 04, 2019 | Hanover, VA | N9525V | Incident | substantial |
The student pilot's improper decision to release the seat latch to adjust the seat position during taxi, which resulted in his inability to reach the …The student pilot's improper decision to release the seat latch to adjust the seat position during taxi, which resulted in his inability to reach the rudder or brake pedals and a subsequent loss of directional control and impact with a ditch and fence. |
| Feb 02, 2019 | Knotts Island, NC | N6789F | Incident | substantial | A total loss of engine power due to fuel exhaustion, which resulted from the pilot's improper fuel planning. |
| Jan 29, 2019 | Reno, NV | N670CS | Incident | substantial | The student pilot's failure to maintain directional control during a rejected takeoff, which resulted in a runway excursion and impact with a ditch. |
| Jan 29, 2019 | Grand Prairie, TX | N52243 | Incident | substantial |
The failure of the pilots of both airplanes to see and avoid the other airplane while entering the airport traffic pattern in visual meteorological co…The failure of the pilots of both airplanes to see and avoid the other airplane while entering the airport traffic pattern in visual meteorological conditions. Contributing to the accident was the tower controller's failure to recognize the proximity of the airplanes to each other, to issue a safety alert to the pilots of either airplane, and to establish a landing sequence for the airplanes. |
| Jan 27, 2019 | Selah, WA | N4087V | Incident | substantial |
The pilot's failure to use carburetor heat while operating in conditions conducive to carburetor icing, which resulted in a partial loss of engine pow…The pilot's failure to use carburetor heat while operating in conditions conducive to carburetor icing, which resulted in a partial loss of engine power and a subsequent forced landing and impact with a fence. |
| Jan 26, 2019 | Troutdale, OR | N736QV | Incident | substantial |
The student pilot's failure to maintain the proper pitch attitude during touchdown, which resulted in a bounced landing and subsequent propeller strik…The student pilot's failure to maintain the proper pitch attitude during touchdown, which resulted in a bounced landing and subsequent propeller strike. |
| Jan 24, 2019 | Ogden, UT | N736TB | Incident | substantial |
The student pilot's failure to maintain the runway heading during a touch-and-go landing and the flight instructor's delayed remedial action, which re…The student pilot's failure to maintain the runway heading during a touch-and-go landing and the flight instructor's delayed remedial action, which resulted in the airplane departing the left side of the runway, impacting snow, and nosing over. |
| Jan 19, 2019 | MIAMI, FL | N734AY | Incident | substantial |
The student pilot's failure to control the airplane's speed and direction during the approach, which resulted in landing long, a runway excursion, and…The student pilot's failure to control the airplane's speed and direction during the approach, which resulted in landing long, a runway excursion, and impact with a windsock. |
| Jan 10, 2019 | Port Lavaca, TX | N2391S | Incident | substantial | A total loss of engine power for reasons that could not be determined based on the available information. |
| Jan 06, 2019 | Flint, MI | N1237M | Incident | substantial |
The failure of the nose landing gear actuator hydraulic hose, which resulted in the loss of hydraulic fluid and hydraulic system pressure and a subseq…The failure of the nose landing gear actuator hydraulic hose, which resulted in the loss of hydraulic fluid and hydraulic system pressure and a subsequent gear-up landing. |
| Jan 06, 2019 | Tooradin, AS | VH-DGF | Incident | substantial | Investigation pending |
| Jan 02, 2019 | Appleton, MN | N12181 | Incident | substantial |
The student pilot’s loss of directional control while landing on an ice-covered runway, which resulted in a loss of directional control, and his failu…The student pilot’s loss of directional control while landing on an ice-covered runway, which resulted in a loss of directional control, and his failure to attain sufficient airspeed during a subsequent aborted landing, which resulted in a nose-over. |
| Dec 31, 2018 | Apopka, FL | N78JE | Incident | substantial |
A partial loss of engine power during a go-around for reasons that could not be determined based on the available information, which resulted in a for…A partial loss of engine power during a go-around for reasons that could not be determined based on the available information, which resulted in a forced landing. |
| Dec 30, 2018 | Caldwell, NJ | N2651R | Incident | substantial | The student pilot's failure to maintain directional control during the takeoff roll. |
| Dec 27, 2018 | Sugar Land, TX | N17SJ | Incident | substantial | The student pilot's failure to maintain directional control during takeoff, which resulted in a runway excursion and impact with a sign. |
| Dec 24, 2018 | Fort Lauderdale, FL | N3015E | Incident | substantial | A total loss of engine power due to the fatigue fracture of the No. 2 exhaust rocker arm stud. |
| Dec 23, 2018 | Big Lake, AK | N93018 | Incident | substantial |
The pilot's improper decision to land on a roadway during dark night conditions with inoperable landing and taxi lights, which resulted in an impact w…The pilot's improper decision to land on a roadway during dark night conditions with inoperable landing and taxi lights, which resulted in an impact with a snow berm. |
| Dec 23, 2018 | Norwood, CO | N3120S | Incident | substantial | The partial loss of engine power for undetermined reasons. |
| Dec 21, 2018 | Marshall, TX | N23YR | Incident | substantial | The pilot's failure to maintain directional control during landing. |
| Dec 21, 2018 | Abilene, TX | N254RA | Incident | substantial |
The pilot's failure to see and avoid a cell tower wire during a pipeline patrol flight. Contributing to the accident was the pilot's distraction due t…The pilot's failure to see and avoid a cell tower wire during a pipeline patrol flight. Contributing to the accident was the pilot's distraction due to writing down observations about the pipeline while flying. |
| Dec 17, 2018 | Bell Glade, FL | N4886B | Incident | substantial |
A partial loss of engine power due to the No. 1 cylinder's valve keeper becoming dislodged, which ultimately resulted in the intake valve becoming stu…A partial loss of engine power due to the No. 1 cylinder's valve keeper becoming dislodged, which ultimately resulted in the intake valve becoming stuck in the valve guide and in the loss of compression to the cylinder. |
| Dec 16, 2018 | Riggins, ID | N4385B | Incident | substantial | The pilot's improper preflight performance planning and his subsequent failure to attain sufficient speed for the airplane to climb with a tailwind. |
| Dec 15, 2018 | MORIARTY, NM | N188H | Incident | substantial | The pilot's failure to see and avoid a parked glider while taxiing from the runway. |
| Dec 15, 2018 | Beaumont, KS | N2496N | Incident | substantial |
The right brake being locked during the landing roll on the turf runway for reasons that could not be determined during postaccident examinations, whi…The right brake being locked during the landing roll on the turf runway for reasons that could not be determined during postaccident examinations, which resulted in a noseover. |