Cessna Safety Record
Complete NTSB accident and incident history. 28016 events recorded from 1974 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jun 02, 2010 | Anchorage, AK | N59352 | Fatal (1) | substantial |
The pilot’s decision to load the airplane well beyond its allowable weight and center of gravity limits, resulting in a loss of control during the ini…The pilot’s decision to load the airplane well beyond its allowable weight and center of gravity limits, resulting in a loss of control during the initial climb. Contributing to the severity of the injuries was the pilot’s decision to allow two child passengers to sit on other passenger's laps without restraints, and his failure to properly secure the cargo in the cabin. Also contributing was the pilot's excessive extension of the wing flaps. |
| Jun 01, 2010 | Greenfield, IN | N1448Z | Incident | substantial | The pilot's improper landing flare and recovery from a bounced landing. |
| Jun 01, 2010 | Dania Beach, FL | N1435F | Minor | substantial | The pilot’s improper fuel management, which resulted in a loss of engine power due to fuel exhaustion. |
| May 31, 2010 | Oliver Springs, TN | N8311S | Minor | substantial | The pilot's failure to execute a go-around, which resulted in a long landing, runway overrun, and the airplane's subsequent descent into a stream. |
| May 31, 2010 | Sterling, MA | N6371D | Incident | substantial |
The pilot’s decision to not continue with the go-around, which resulted in a collision with trees. Contributing to the accident was the pilot’s distra…The pilot’s decision to not continue with the go-around, which resulted in a collision with trees. Contributing to the accident was the pilot’s distraction due to the passenger’s panicked condition. |
| May 31, 2010 | Wellington, KS | N78612 | Incident | substantial | The pilot's failure to properly secure the airplane while manually starting the engine with the propeller. |
| May 31, 2010 | Glasco, KS | N9388U | Minor | substantial | The pilot’s delay in applying full power to arrest a sink rate at low altitude. |
| May 30, 2010 | Chateaugay, NY | N9985T | Incident | substantial | The pilot's misjudgedment of his speed and distance during landing, which resulted in an overrun. |
| May 30, 2010 | Las Cruces, NM | N2723U | Serious (1) | destroyed |
A loss of engine power due to fuel starvation as a result of water contamination in the fuel, and the pilot's inadequate preflight inspection. Contrib…A loss of engine power due to fuel starvation as a result of water contamination in the fuel, and the pilot's inadequate preflight inspection. Contributing the accident was an inoperative number 5 cylinder exhaust valve. |
| May 29, 2010 | Atchison, KS | N76287 | Incident | substantial | The loss of engine power for undetermined reasons. |
| May 28, 2010 | White Plains, NY | N662QS | Incident | minor | The flight crew's failure to ensure that the cabin door was secured/locked prior to takeoff. |
| May 27, 2010 | High Springs, FL | N72268 | Minor | substantial |
The pilot's failure to follow the published engine-out procedures after a total loss of power in the rear engine. Contributing to the accident was the…The pilot's failure to follow the published engine-out procedures after a total loss of power in the rear engine. Contributing to the accident was the inadequate maintenance and inspection of the engine by the pilot and maintenance personnel. |
| May 25, 2010 | Merced, CA | N69254 | Incident | substantial | The pilot's improper recovery from a bounced landing. |
| May 24, 2010 | East Haddam, CT | N169ER | Incident | substantial | The pilot's delayed decision to attempt a go-around, and his subsequent failure to maintain directional control while landing. |
| May 23, 2010 | Kettle Falls, WA | N9104R | Incident | substantial |
The pilot's failure to maintain clearance from obstacles during the landing roll. Contributing to the accident was the reduced visibility due to preci…The pilot's failure to maintain clearance from obstacles during the landing roll. Contributing to the accident was the reduced visibility due to precipitation. |
| May 22, 2010 | Las Vegas, NV | N529MC | Incident | substantial | The pilot's inadequate compensation for the wind conditions and failure to maintain directional control during taxi. |
| May 22, 2010 | Petaluma, CA | N210SL | Incident | substantial |
The pilot's inadequate compensation for the crosswind condition and failure to maintain directional control during the landing roll in gusty crosswind…The pilot's inadequate compensation for the crosswind condition and failure to maintain directional control during the landing roll in gusty crosswind conditions. |
| May 21, 2010 | Cambridge, NY | N234JK | Incident | substantial | The pilot's loss of directional control during takeoff. |
| May 21, 2010 | Rio Negro, Bolivar, VE | YV158E | Fatal (2) | destroyed | Investigation pending |
| May 21, 2010 | Benson, AZ | N6630X | Minor | substantial |
A loss of engine power due to fuel starvation as a result of a loss of fuel pressure caused by the fuel pump screws being loose. Contributing to the a…A loss of engine power due to fuel starvation as a result of a loss of fuel pressure caused by the fuel pump screws being loose. Contributing to the accident was inadequate maintenance. |
| May 21, 2010 | Plattekill, NY | N739RK | Serious (2) | substantial |
The pilot's failure to place the fuel selector valve in the appropriate position for takeoff resulting in a partial loss of engine power. Contributing…The pilot's failure to place the fuel selector valve in the appropriate position for takeoff resulting in a partial loss of engine power. Contributing to the accident was the pilot's attempted takeoff at a higher than allowed gross weight. |
| May 19, 2010 | Renton, WA | N66033 | Incident | substantial | The pilot's inadequate compensation for the wind conditions, resulting in the loss of directional control during the landing roll. |
| May 19, 2010 | Arbuckle, CA | N580TP | Minor | substantial |
Insufficient clamping force to the connecting rod bolt, which resulted in looseness in the connecting rod bearing area that led to the fatigue fractur…Insufficient clamping force to the connecting rod bolt, which resulted in looseness in the connecting rod bearing area that led to the fatigue fracture of the connecting rod and a subsequent loss of engine power. |
| May 17, 2010 | Spring Branch, TX | N50LP | Incident | substantial | A loss of engine power due to fuel contamination. |
| May 16, 2010 | Duluth, MN | N6545A | Incident | substantial | The pilot's failure to maintain directional control during landing. |