Cessna Safety Record
Complete NTSB accident and incident history. 28016 events recorded from 1974 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Mar 24, 2015 | Flushing, MI | N7987E | Minor | substantial | Loss of engine power due to fuel contamination. A factor contributing to the accident was the pilot's inadequate preflight. |
| Mar 24, 2015 | Verdigris, OK | N106BZ | Minor | substantial |
The fuel pump gear manufacturer’s allowance of set-up gears made from a nonconforming material to be put in the production inventory system, the insta…The fuel pump gear manufacturer’s allowance of set-up gears made from a nonconforming material to be put in the production inventory system, the installation of a nonconforming gear in the accident airplane’s production fuel pump, and the gear’s failure, which resulted in a loss of fuel flow to the engine and the subsequent loss of engine power. |
| Mar 16, 2015 | Easton, MD | N2026V | Minor | substantial | The pilot's failure to maintain directional control during the landing roll. |
| Mar 15, 2015 | Williamson, GA | N8452X | Minor | substantial |
The separation of the nosewheel upon landing due to a missing bolt that attached the upper torque assembly to the nosewheel steering arm assembly. Whe…The separation of the nosewheel upon landing due to a missing bolt that attached the upper torque assembly to the nosewheel steering arm assembly. When and how the bolt separated could not be determined. |
| Mar 03, 2015 | Venice, FL | N498TC | Minor | substantial | A total loss of engine power for reasons that could not be determined because postaccident testing of the engine revealed no anomalies. |
| Feb 09, 2015 | Kernville, CA | CFGQQ | Minor | substantial |
The pilot's inadequate flare and failure to maintain airplane control during the landing with a tailwind which resulted in a bounce, long landing, and…The pilot's inadequate flare and failure to maintain airplane control during the landing with a tailwind which resulted in a bounce, long landing, and subsequent runway excursion. |
| Jan 26, 2015 | Makaha, HI | N422BP | Minor | substantial | A partial loss of engine power for reasons that could not be determined because the airplane was ditched and not recovered. |
| Jan 26, 2015 | Fort Morgan, CO | N8997T | Minor | substantial |
The pilot's improper fuel planning/management, which resulted in the total loss of engine power due to fuel exhaustion and the subsequent forced landi…The pilot's improper fuel planning/management, which resulted in the total loss of engine power due to fuel exhaustion and the subsequent forced landing in a pasture. |
| Jan 25, 2015 | Silver Springs, NV | N4017U | Minor | substantial | The loss of engine power for reasons that could not be determined during a postaccident examination of the airplane. |
| Jan 10, 2015 | Cullman, AL | N89921 | Minor | substantial | The student pilot’s failure to maintain airplane control after engine start, which resulted in a ground collision with trees. |
| Jan 09, 2015 | Pontiac, IL | N2871S | Minor | substantial |
The flight instructor’s loss of directional control during an attempted go-around with a crosswind. Contributing to the accident was the loss of engin…The flight instructor’s loss of directional control during an attempted go-around with a crosswind. Contributing to the accident was the loss of engine power for reasons that could not be determined during examination of the engine. |
| Jan 03, 2015 | Key West, FL | N2534X | Minor | substantial | A total loss of engine power for reasons that could not be determined during postaccident examinations and testing. |
| Jan 01, 2015 | Yuma, AZ | N2841N | Minor | substantial |
The pilot's failure to compensate for crosswind conditions during takeoff, which resulted in the loss of directional control and collision with terrai…The pilot's failure to compensate for crosswind conditions during takeoff, which resulted in the loss of directional control and collision with terrain. |
| Dec 22, 2014 | South Bimini, BF | N12182 | Minor | substantial |
The total loss of engine power for reasons that could not be determined because examination of the engine did not reveal any anomalies that would have…The total loss of engine power for reasons that could not be determined because examination of the engine did not reveal any anomalies that would have precluded normal operation, which resulted in a subsequent ditching in the ocean. |
| Dec 09, 2014 | Jeffrey, WY | N4881K | Minor | substantial |
The pilot's inadequate approach and excessive airspeed, which resulted in a long landing, the subsequent runway overrun, and impact with terrain. Cont…The pilot's inadequate approach and excessive airspeed, which resulted in a long landing, the subsequent runway overrun, and impact with terrain. Contributing to the accident was the pilot's delay in aborting the landing. |
| Dec 05, 2014 | Brookline, NH | N50709 | Minor | substantial |
The student pilot’s failure to maintain clearance from a wire during an off-airport landing following a partial loss of engine power for reasons that …The student pilot’s failure to maintain clearance from a wire during an off-airport landing following a partial loss of engine power for reasons that could not be determined during postaccident examination. |
| Dec 04, 2014 | Sussex, NJ | N8296Z | Minor | substantial |
Maintenance personnel’s inadequate inspection of the No. 2 cylinder valve area during the most recent annual inspection, which resulted in the in-flig…Maintenance personnel’s inadequate inspection of the No. 2 cylinder valve area during the most recent annual inspection, which resulted in the in-flight failure of the intake valve springs due to rust on the spring surfaces and subsequent fatigue cracking. |
| Nov 02, 2014 | Jacksonville, OR | N1593M | Minor | substantial | A loss of engine power during cruise flight due to the failure of the No. 6 connecting rod, which resulted from oil starvation. |
| Oct 12, 2014 | Boca Raton, FL | N2590K | Minor | substantial |
Maintenance personnel’s failure to apply proper torque to the cylinder flange nuts and through bolts, which resulted in shifting of the Nos. 1 and 2 m…Maintenance personnel’s failure to apply proper torque to the cylinder flange nuts and through bolts, which resulted in shifting of the Nos. 1 and 2 main bearings, loss of lubrication, failure of the crankshaft, and a subsequent total loss of engine power. |
| Oct 05, 2014 | Sedona, AZ | N2179L | Minor | substantial | The pilot's failure to maintain airplane control during the landing roll out. |
| Sep 28, 2014 | Port Eads, LA | N2011R | Minor | substantial | The pilot's improper decision to depart from a runway not suitable for takeoff, which resulted in a loss of aircraft control. |
| Sep 27, 2014 | Silver City, NM | N2309R | Minor | substantial |
The pilot overcorrected when the airplane experienced a downdraft during the takeoff which resulted in the airplane stalling and impacting the terrain…The pilot overcorrected when the airplane experienced a downdraft during the takeoff which resulted in the airplane stalling and impacting the terrain. |
| Sep 22, 2014 | Brookfield, WI | N50889 | Minor | substantial | The pilot's inadequate maintenance and preflight of the airplane which resulted in a total loss of engine power due to oil starvation. |
| Sep 19, 2014 | Piscataquis County, ME | N180GK | Minor | substantial |
The fatigue fracture of the No. 3 exhaust valve, which initiated at the outer surface of the valve stem and resulted in the subsequent total loss of e…The fatigue fracture of the No. 3 exhaust valve, which initiated at the outer surface of the valve stem and resulted in the subsequent total loss of engine power over terrain unsuitable for landing. |
| Sep 11, 2014 | Spruce Creek, FL | N63835 | Minor | substantial | A total loss of engine power due to fuel exhaustion, which resulted from the pilots’ improper preflight and in-flight fuel planning. |