Cessna Safety Record
Complete NTSB accident and incident history. 28016 events recorded from 1974 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Sep 07, 2017 | Fairfield, MT | N735KQ | Minor | destroyed |
The pilot's failure to secure the right fuel cap during the preflight inspection, which resulted in fuel exhaustion, a total loss of engine power, and…The pilot's failure to secure the right fuel cap during the preflight inspection, which resulted in fuel exhaustion, a total loss of engine power, and an off-airport hard landing. |
| Sep 01, 2017 | Harpswell, ME | N4615X | Minor | substantial |
A total loss of engine power due to maintenance personnel's failure to apply proper torque to the cylinder flange nuts and through bolts, which result…A total loss of engine power due to maintenance personnel's failure to apply proper torque to the cylinder flange nuts and through bolts, which resulted in shifting of the Nos. 1, 2, and 3 main bearings, loss of lubrication, and failure of the crankshaft. |
| Aug 30, 2017 | Belle Fourche, SD | N2982U | Minor | substantial |
The flight instructor's failure to maintain adequate airspeed and his exceedance of the airplane’s critical angle of attack during a go-around in gust…The flight instructor's failure to maintain adequate airspeed and his exceedance of the airplane’s critical angle of attack during a go-around in gusting crosswind conditions, which resulted in an aerodynamic stall. |
| Aug 27, 2017 | Wurtsboro, NY | N1834 | Minor | substantial | A fatigue fracture of the left main landing gear axle. |
| Aug 24, 2017 | Salt Lake City, UT | N8170M | Minor | substantial | A loss of engine power for reasons that could not be determined based on the available information. |
| Aug 12, 2017 | Quitman, MS | N147DD | Minor | substantial | The student pilot’s failure to maintain directional control during takeoff in gusting wind conditions after passing a large hill. |
| Aug 09, 2017 | Wellston, OH | N5274Q | Minor | substantial | The failure of a connecting rod small end bushing, which resulted in a loss of engine power. |
| Jul 31, 2017 | Seattle, WA | N957TA | Minor | substantial |
The total loss of engine power due to oil starvation as a result of the loose right magneto, which allowed oil to escape and the engine to seize. Cont…The total loss of engine power due to oil starvation as a result of the loose right magneto, which allowed oil to escape and the engine to seize. Contributing to the accident was inadequate maintenance, which failed to identify the loose magneto bolt. |
| Jul 22, 2017 | Austin, TX | N3119D | Minor | substantial |
The pilot's improper decision to attempt to take off after two previous failed attempts from choppy water with a high outside temperature and the airp…The pilot's improper decision to attempt to take off after two previous failed attempts from choppy water with a high outside temperature and the airplane near its maximum gross weight, which degraded the airplane’s performance and resulted in its inability to maintain adequate airspeed and sustain a climb. |
| Jul 14, 2017 | Key Biscayne, FL | N80457 | Minor | substantial |
The nearly complete blockage of the right fuel tank strainer with organic material, which resulted in fuel starvation and the subsequent total loss of…The nearly complete blockage of the right fuel tank strainer with organic material, which resulted in fuel starvation and the subsequent total loss of engine power. Contributing to the fuel starvation was the pilot receiving instruction’s and the flight instructor’s failure to identify that the fuel was burning unevenly during the flight. |
| Jul 09, 2017 | Anchorage, AK | N2429C | Minor | substantial | A total loss of engine power due to fuel starvation for undetermined reasons. |
| Jul 07, 2017 | Cape Coral, FL | N2492U | Minor | substantial |
A total loss of engine power due to fuel contamination with water and the pilot's inadequate preflight inspection that detected, but did not fully res…A total loss of engine power due to fuel contamination with water and the pilot's inadequate preflight inspection that detected, but did not fully resolve, the water contamination of the fuel system. |
| Jul 07, 2017 | Greenwood, SC | N337J | Minor | substantial |
The pilots' inadequate preflight inspection, during which they failed to adequately verify the quantity of fuel, which resulted in fuel exhaustion, a …The pilots' inadequate preflight inspection, during which they failed to adequately verify the quantity of fuel, which resulted in fuel exhaustion, a subsequent total loss of power to both engines, and a forced landing into trees. Contributing to the accident were the erroneous fuel quantity displayed by the fuel quantity indicating system fuel sender units and the operator's failure to comply with a mandatory service bulletin addressing inaccuracies in the fuel quantity indicating system. |
| Jul 07, 2017 | Vacaville, CA | N7532V | Minor | substantial |
The total loss of engine power during initial climb for reasons that could not be determined because postaccident examination of the engine revealed n…The total loss of engine power during initial climb for reasons that could not be determined because postaccident examination of the engine revealed no mechanical failure or malfunction that would have precluded normal operation. |
| Jul 05, 2017 | Wauseon, OH | N3225T | Minor | substantial | The flight instructor’s inadequate preflight fuel planning, which resulted in a total loss of engine power due to fuel exhaustion. |
| Jul 04, 2017 | Willits, CA | N66NF | Minor | substantial |
The pilot’s failure to maintain directional control while landing in gusting wind conditions. Contributing to the accident was the pilot’s failure to …The pilot’s failure to maintain directional control while landing in gusting wind conditions. Contributing to the accident was the pilot’s failure to go around after the unstabilized approach. |
| Jul 03, 2017 | Alpine, TX | N9714B | Minor | substantial |
Fracture of a compressor turbine (CT) blade due to operational overtemperatures and the failure of a maintenance technician to detect an existing crac…Fracture of a compressor turbine (CT) blade due to operational overtemperatures and the failure of a maintenance technician to detect an existing crack in the CT blade during the last engine inspection. |
| Jun 26, 2017 | Vinalhaven, ME | N207GM | Minor | substantial |
The pilot’s failure to maintain a stabilized approach, which resulted in a bounced landing and subsequent go-around with insufficient distance to clea…The pilot’s failure to maintain a stabilized approach, which resulted in a bounced landing and subsequent go-around with insufficient distance to clear trees during the climb. |
| Jun 25, 2017 | San Martin, CA | N524BF | Minor | substantial |
The pilot’s failure to attain a proper glidepath on approach for landing, which resulted in an impact with a guard rail and post. Contributing to the …The pilot’s failure to attain a proper glidepath on approach for landing, which resulted in an impact with a guard rail and post. Contributing to the accident was the pilot’s failure to ensure that sufficient fuel was onboard for nonlevel flight, which resulted in fuel starvation. |
| Jun 24, 2017 | Fulton, MO | N6474B | Minor | substantial | The partial loss of engine power due to water contamination in the fuel system. |
| Jun 13, 2017 | West Creek, NJ | N206TF | Minor | substantial | The pilot's improper fuel management, which resulted in fuel starvation and the subsequent total loss of engine power. |
| Jun 06, 2017 | Chugiak, AK | N35700 | Minor | substantial | The pilot's improper in-flight fuel management, which resulted in a total loss of engine power due to fuel starvation. |
| Jun 04, 2017 | Payson, AZ | N50526 | Minor | destroyed |
The pilot’s inadequate preflight planning that did not account for high-density altitude conditions and his subsequent attempted go-around in conditio…The pilot’s inadequate preflight planning that did not account for high-density altitude conditions and his subsequent attempted go-around in conditions that prevented the airplane from attaining a positive climb rate and resulted in its subsequent descent and impact with rising terrain. |
| May 27, 2017 | El Monte, CA | N6832D | Minor | substantial |
The flight instructor's delayed remedial action, which resulted in an exceedance of the airplane's critical angle of attack and an aerodynamic stall a…The flight instructor's delayed remedial action, which resulted in an exceedance of the airplane's critical angle of attack and an aerodynamic stall and loss of control. Contributing to the accident was the student pilot's failure to maintain runway alignment on approach. |
| May 26, 2017 | Plainwell, MI | N30462 | Minor | substantial | The pilot's improper approach to landing and his failure to perform a go-around, which resulted in a runway overrun. |