Cessna U206 Safety Record
Complete NTSB accident and incident history. 376 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Sep 04, 2017 | Kodiak, AK | N16GP | Incident | substantial |
***This probable cause was modified on November 27, 2018. Please see the docket for this accident to view the original probable cause.*** The pilo…***This probable cause was modified on November 27, 2018. Please see the docket for this accident to view the original probable cause.*** The pilot's improper decision to takeoff in an area of rough water and ocean swells, which resulted in a failure of the right float struts. |
| Jun 23, 2017 | Page, AZ | N71001 | Incident | substantial |
The failure of the throttle control cable due to fatigue and maintenance personnel’s failure to replace the cable at the last engine overhaul, which r…The failure of the throttle control cable due to fatigue and maintenance personnel’s failure to replace the cable at the last engine overhaul, which resulted in the pilots’ inability to control engine power and led to a precautionary landing during which the airplane impacted bushes. |
| May 23, 2017 | Noatak, AK | N9575G | Incident | destroyed | A fire in the airplane's cabin, which initiated for reasons that could not be determined due to extensive thermal damage. |
| May 17, 2017 | Diamond Point, NY | N4804F | Incident | substantial | The pilot’s failure to maintain directional control during the takeoff roll with gusting wind conditions. |
| Aug 17, 2016 | Sleetmute, AK | N8076Z | Incident | substantial | The pilot's exceedance of the critical angle of attack during the landing flare, which resulted in an aerodynamic stall and a hard landing. |
| Jul 31, 2016 | Sleetmute, AK | N206JC | Incident | substantial |
The pilot's failure to maintain adequate airspeed during the initial climb after taking off from a wet runway and his exceedance of the airplane’s cri…The pilot's failure to maintain adequate airspeed during the initial climb after taking off from a wet runway and his exceedance of the airplane’s critical angle of attack, which resulted in an aerodynamic stall. |
| Jul 20, 2016 | Cordova, AK | N1222V | Incident | substantial | The pilot's improper landing flare, which resulted in a hard landing and subsequent landing gear separation and collapse. |
| Jun 30, 2016 | Ely, NV | N9304R | Incident | substantial | The flight instructor's incorrect pitch control during the landing flare, which resulted in a tail strike. |
| Jun 25, 2016 | Fresh Creek, BF | N9662G | Incident | substantial | Investigation pending |
| May 23, 2016 | Chinita Bay, AK | N4596U | Incident | substantial | The pilot's selection of unsuitable terrain for taxi, resulting in a tail strike and aft fuselage substantial damage. |
| Apr 29, 2016 | Port Alsworth, AK | N9610Z | Incident | substantial |
The pilot's failure to maintain an appropriate descent rate during the landing flare in gusty crosswind conditions, which resulted in a hard landing, …The pilot's failure to maintain an appropriate descent rate during the landing flare in gusty crosswind conditions, which resulted in a hard landing, aerodynamic stall, impact with terrain, nose gear collapse, and nose over. |
| Apr 15, 2016 | Atlantic Ocean, AO | N1346Q | Incident | substantial | A total loss of engine power for reason(s) that could not be determined because the airplane was not recovered. |
| Jul 22, 2015 | Kasilof, AK | N206CL | Incident | substantial |
The pilot's selection of unsuitable terrain for takeoff, which resulted in a jammed elevator and subsequent loss of control and collision with terrain…The pilot's selection of unsuitable terrain for takeoff, which resulted in a jammed elevator and subsequent loss of control and collision with terrain. |
| Jun 27, 2015 | Anchorage, AK | N756BW | Incident | substantial | The pilot's improper recovery from a bounced landing, and his failure to maintain directional control. |
| Nov 15, 2014 | La Verne, CA | N9420R | Incident | substantial |
The pilot's loss of directional control during the landing roll for reasons that could not be determined, because postaccident examination of the nose…The pilot's loss of directional control during the landing roll for reasons that could not be determined, because postaccident examination of the nosewheel assembly revealed no anomalies that would have precluded normal operation. |
| Sep 06, 2014 | Gustavus, AK | N3862G | Incident | substantial |
The motor vehicles operators' lack of attention, and improper decision to cross the runway with the runway alert system active, resulting in a collisi…The motor vehicles operators' lack of attention, and improper decision to cross the runway with the runway alert system active, resulting in a collision with the airplane. |
| Jun 21, 2014 | Abbeyshrule, EI | G-SKYE | Incident | substantial | <br /><br /> |
| Jun 09, 2014 | Chitina, AK | N29137 | Incident | substantial |
The failure of the engine’s No. 1 piston connecting rod retaining bolts due to fatigue, which resulted in a total loss of engine power during cruise f…The failure of the engine’s No. 1 piston connecting rod retaining bolts due to fatigue, which resulted in a total loss of engine power during cruise flight. |
| Aug 30, 2013 | Rumney, NH | N208LH | Incident | substantial |
The pilot's failure to ensure that the amphibious airplane's landing gear was properly configured for a landing on water and his failure to properly c…The pilot's failure to ensure that the amphibious airplane's landing gear was properly configured for a landing on water and his failure to properly configure the airplane during the attempted go-around. |
| Aug 24, 2013 | Tokotna, AK | N35952 | Incident | substantial |
A total loss of engine power due to the failure of the crankshaft, which resulted from a mechanic’s application of insufficient torque on the cylinder…A total loss of engine power due to the failure of the crankshaft, which resulted from a mechanic’s application of insufficient torque on the cylinder through bolts. |
| Aug 05, 2013 | Kokhanok, AK | N5364Q | Incident | substantial | The pilot’s selection of unsuitable terrain for takeoff, which resulted in a loss of control and collision with terrain. |
| May 31, 2013 | Fairbanks, AK | N4571K | Incident | substantial | The pilot’s inadequate flare, which resulted in a nose-low impact with glassy water and a subsequent nose-over. |
| May 30, 2013 | King Salmon, AK | N77206 | Incident | substantial | The pilot's inadequate airspeed control during a glassy water landing, which resulted in an excessive sink rate, and a hard landing. |
| May 14, 2013 | Friday Harbor, WA | N707WJ | Incident | substantial | A collision with a bird while on the downwind leg of the traffic pattern. |
| Apr 24, 2013 | Nenana, AK | N756DJ | Incident | substantial |
Ice accretion in the right main landing gear wheel brake during departure, which prevented the right main landing gear from rotating on landing and re…Ice accretion in the right main landing gear wheel brake during departure, which prevented the right main landing gear from rotating on landing and resulted in a runway excursion and subsequent impact with a snow bank. |