Cessna P210N Safety Record

Complete NTSB accident and incident history. 198 events recorded from 1982 to 2025.

198

All Events

78

Incidents

32

Minor

32

Serious

56

Fatal (119 fatalities)

Date Location Reg# Severity Damage Probable Cause
Dec 02, 2023 Big Bear, CA N7LV Serious (1) substantial A loss of engine power during the initial climb for undetermined reasons, which resulted in an aborted takeoff and runway excursion.
Jun 21, 2022 Cresson, TX N7361K Serious (1) substantial
The pilot's failure to complete proper preflight performance planning and his operation of the airplane outside of the manufacturer's specified weight…

The pilot's failure to complete proper preflight performance planning and his operation of the airplane outside of the manufacturer's specified weight and balance limitations, which resulted in the airplane’s inability to maintain altitude and an impact with trees and terrain during an attempted forced landing.

Sep 01, 2018 Crete, NE N210PF Serious (2) substantial
The stuck turbocharger wastegate in the closed position for reasons that could not be determined based on the available information. Also causal was t…

The stuck turbocharger wastegate in the closed position for reasons that could not be determined based on the available information. Also causal was the pilot's failure to reduce the throttle during takeoff when the manifold pressure and fuel flow exceeded the takeoff limitations and the pilot's decision to turn on the fuel boost pump, which exacerbated the excessively rich fuel mixture and resulted in a total loss of engine power.

May 09, 2017 San Vicente Tancoayalab, MX N116DC Serious (1) destroyed Investigation pending
Nov 13, 2016 Pleasanton, TX N44C Serious (1) substantial
Maintenance personnel's improper installation of the throttle linkage attachment hardware, which resulted in a partial loss of engine power when the h…

Maintenance personnel's improper installation of the throttle linkage attachment hardware, which resulted in a partial loss of engine power when the hardware separated in flight.

Feb 16, 2016 Bryan, TX N732FU Serious (1) substantial A failure of the crankshaft due to improper torque of the crankcase through bolts.
Sep 23, 2011 South Deerfield, MA N210LE Serious (2) substantial
The failure of the electrical system due to an alternator failure during flight in instrument meteorological conditions, and the pilot’s inadequate pr…

The failure of the electrical system due to an alternator failure during flight in instrument meteorological conditions, and the pilot’s inadequate preflight inspection and failure to use the approved checklist for the dual alternator system. Contributing to the accident was the inadequate maintenance because the alternator restart battery pack was not replaced annually, as required by the airplane service manual.

Mar 03, 2010 Arcadia, FL N4797K Serious (1) substantial The total loss of engine power due to a fatigue fracture of the crankshaft resulting from worn bearings.
Mar 29, 2009 Georgetown, TX N210BF Serious (1) substantial
A loss of engine power due to fuel starvation as a result of the pilot's inadequate fuel management. Contributing to the accident was the pilot's impr…

A loss of engine power due to fuel starvation as a result of the pilot's inadequate fuel management. Contributing to the accident was the pilot's improper engine restart procedures.

Apr 06, 2008 Louisville, KY N734JV Serious (1) substantial The pilot's failure to maintain airspeed while maneuvering, which resulted in an inadvertent stall/spin.
Nov 10, 2007 Midland, TX N7716K Serious (1) substantial The pilot's failure to maintain directional control during the landing roll. Contributing factors were the prevailing tailwind and an airport sign.
Aug 09, 2001 Mackinac Island, MI N5268W Serious (2) destroyed
The pilot's failure to maintain proper glidepath during the landing approach resulting in the pilot not maintaining clearance from the trees. Factors…

The pilot's failure to maintain proper glidepath during the landing approach resulting in the pilot not maintaining clearance from the trees. Factors were the haze, the gusty winds, and the trees.

Feb 16, 2001 Seminole, AL N210FW Serious (1) substantial
the pilot's improper inflight planning/decision and failure to refuel en route and ensure an adequate supply of fuel to safely complete the flight to …

the pilot's improper inflight planning/decision and failure to refuel en route and ensure an adequate supply of fuel to safely complete the flight to his destination with adequate reserves, which resulted in fuel exhaustion, subsequent engine failure, and a forced landing into a wooded area at night.

Jul 17, 2000 RICHFIELD SPRNG, NY N5256W Serious (2) substantial Failure of the number two cylinder main bearing for undetermined reasons.
Jul 07, 2000 BOONE, NC N7VZ Serious (1) substantial
The failure of the inter-cooler duct connecting the inter-cooler to the engine due to inadequate attachment of the inter-cooler to the aircraft which …

The failure of the inter-cooler duct connecting the inter-cooler to the engine due to inadequate attachment of the inter-cooler to the aircraft which resulted in loss of turbocharger air overboard and loss of engine power and damage to the aircraft during a forced landing. Contributing to the accident was inadequate inspection requirements for the inter-cooler system and inadequate inspection of the inter-cooler system by the mechanic during the last inspection.

May 31, 1999 RENO, NV N37MJ Serious (1) substantial Fuel starvation resulting from the pilot's inattentive monitoring and management of the fuel system.
May 06, 1998 CHESTERFIELD, VA N4543K Serious (2) destroyed The pilot's inadequate in-flight planning/decision which led to fuel exhaustion and subsequent loss of engine power.
Dec 18, 1996 MUSKOGEE, OK N210BG Serious (1) substantial
the pilot's improper planning/decision and inaccurate fuel consumption calculations, which resulted in an inadequate supply of fuel, fuel exhaustion, …

the pilot's improper planning/decision and inaccurate fuel consumption calculations, which resulted in an inadequate supply of fuel, fuel exhaustion, and a subsequent forced landing at night. Darkness was a related factor.

Jul 30, 1995 SPRINGFIELD, MO N6322W Serious (1) substantial the partial loss of engine power due to fouled spark plugs as a result of an improper fuel/air mixture. A factor in the accident was the powerlines.
Apr 26, 1995 DODGE CITY, KS N4614K Serious (3) minor
fatigue and subsequent catastrophic failure of the connecting rod originating from the decarburized area on the shank of the rod. Factors were the lo…

fatigue and subsequent catastrophic failure of the connecting rod originating from the decarburized area on the shank of the rod. Factors were the low cloud weather condition and the ditch.

Jan 01, 1995 ALBUQUERQUE, NM N6106W Serious (2) substantial
THE PILOT DID NOT ALIGN THE AIRCRAFT WITH THE RUNWAY. FACTORS WERE THE DUSK LIGHT CONDITIONS AND THE PILOT'S FAILURE TO ACTIVATE THE PILOT CONTROLLED …

THE PILOT DID NOT ALIGN THE AIRCRAFT WITH THE RUNWAY. FACTORS WERE THE DUSK LIGHT CONDITIONS AND THE PILOT'S FAILURE TO ACTIVATE THE PILOT CONTROLLED RUNWAY LIGHTS.

Jan 15, 1994 NEW CASTLE, DE N5088W Serious (1) substantial LOSS OF PARTIAL ENGINE POWER DUE TO UNDETERMINED REASONS.
Jan 10, 1994 SAN MARTIN, CA N5384W Serious (2) destroyed
the pilot's improper aircraft preflight inspection, and his failure to use pitot heat during the takeoff in icing conditions, which led to a blocked p…

the pilot's improper aircraft preflight inspection, and his failure to use pitot heat during the takeoff in icing conditions, which led to a blocked pitot tube. The blockage resulted in erroneous airspeed indications during the initial climb, which induced the pilot to reduce the aircraft pitch attitude to a point where the aircraft entered an uncorrected descent to ground impact.

May 01, 1993 OAKLAND, CA N731HP Serious (1) destroyed
the pilot's poor decision to continue flying the airplane with a known deficiency and the poorly performed major overhaul of the engine. The failed c…

the pilot's poor decision to continue flying the airplane with a known deficiency and the poorly performed major overhaul of the engine. The failed crankshaft due to fatigue are factors in this accident.

Jan 16, 1990 NEWTON, KS N4589K Serious (1) substantial LOSS OF ENGINE POWER FOR AN UNDETERMINED REASON. DARKNESS AND THE RESULTANT DELAY IN FLARING TO LAND WERE RELATED FACTORS.
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
← Cessna P210N For Sale All Cessna Models
Data source: NTSB Aviation Accident Database · About our data
View 26 Cessna P210N for sale ↓