Cessna 421 Safety Record
Complete NTSB accident and incident history. 326 events recorded from 1982 to 2024.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Sep 15, 2002 | Ithaca, NY | N23RL | Incident | substantial | The pilot's failure to maintain directional control during the landing roll. A factor in the accident was the wet runway. |
| Apr 25, 2002 | Tampa, FL | N237SM | Incident | substantial |
the fracture of the landing gear upper barrel due to fatigue cracking, caused by improper machining after the barrel was assembled during the manufact…the fracture of the landing gear upper barrel due to fatigue cracking, caused by improper machining after the barrel was assembled during the manufacturing process, resulting in damage to the airplane. |
| Mar 02, 2002 | Hailey, ID | N421DG | Incident | substantial |
Water contamination within the aircraft's landing gear hydraulic line(s) which froze and blocked the line(s) preventing extension of the right main ge…Water contamination within the aircraft's landing gear hydraulic line(s) which froze and blocked the line(s) preventing extension of the right main gear. A factor was the below freezing environmental conditions which the aircraft was operating in prior to and during the approach and landing. |
| Aug 17, 2001 | New Braunfels, TX | N5286Z | Incident | substantial | the pilot's inadequate flare of the airplane resulting in a hard landing. A contributing factor was the crosswind. |
| May 29, 2001 | Greenville, MS | N51ER | Incident | substantial |
The improper installation by maintenance personnel of the push-pull rod assembly on the right elevator trim tab horn resulted in an in-flight separati…The improper installation by maintenance personnel of the push-pull rod assembly on the right elevator trim tab horn resulted in an in-flight separation of the right elevator trim tab. |
| Dec 14, 2000 | PENSACOLA, FL | N781SL | Incident | substantial |
The failure of the left main landing gear scissors washer during taxi for takeoff, and collapse of the left main landing gear. A factor in the acciden…The failure of the left main landing gear scissors washer during taxi for takeoff, and collapse of the left main landing gear. A factor in the accident was the failure of unknown maintenance personnel to comply with a manufacturers service letter concerning the scissors washers. |
| Jul 25, 2000 | HOMEWOOD, MS | N1477D | Incident | substantial |
The inadequate installation of the right propeller by the mechanic for his failure to properly torque the eight nuts resulting in fatigue failure of t…The inadequate installation of the right propeller by the mechanic for his failure to properly torque the eight nuts resulting in fatigue failure of the studs and separation of the right propeller during cruise flight. Findings in the investigation were 1) the mechanic who installed the right propeller used un-calibrated torque wrenches, and 2) the mechanic who installed the right propeller used an outdated Service Manual. |
| Dec 11, 1999 | GILLETTE, WY | N3912C | Incident | substantial | The collision with a deer on the runway during a night landing. A factor was the dark night. |
| Oct 05, 1999 | MONTAGUE, CA | N69GP | Incident | substantial |
The collapse of the left main landing gear during the landing rollout for undetermined reasons, which resulted in the pilot's loss of directional cont…The collapse of the left main landing gear during the landing rollout for undetermined reasons, which resulted in the pilot's loss of directional control. |
| Jan 15, 1999 | YOUNGSTOWN, OH | N882BB | Incident | substantial | The pilot's failure to maintain aircraft control. A factor was the icy runway. |
| Mar 18, 1998 | SHOW LOW, AZ | N70PD | Incident | substantial | The pilot's failure to attain the proper alignment on the runway due to the obscuration by snow of the runway and on the airplane's windows. |
| Nov 07, 1997 | TOMAHAWK, WI | N2957Q | Incident | substantial |
the elevator trim tab bolt backed out, allowing the trim tab to flutter, and destroy the elevator. The factors involved were improper annual inspecti…the elevator trim tab bolt backed out, allowing the trim tab to flutter, and destroy the elevator. The factors involved were improper annual inspection by the maintenance personnel, and the inadequate aircraft preflight done by the pilot. |
| Apr 21, 1997 | PIERRE, SD | N283PT | Incident | substantial |
the pilot's inadvertent activation of the number one throttle/power control. Factors were: the pilot left the cockpit unattended with the engines run…the pilot's inadvertent activation of the number one throttle/power control. Factors were: the pilot left the cockpit unattended with the engines running and a wet ramp. |
| Feb 06, 1997 | CEDAR CITY, UT | N45MV | Incident | substantial |
water contamination in the hydraulic system, which froze in the (right) main gear hydraulic actuator, and restricted movement of the (right) main gear…water contamination in the hydraulic system, which froze in the (right) main gear hydraulic actuator, and restricted movement of the (right) main gear retraction and extension system. |
| Nov 19, 1996 | OLYMPIA, WA | N8005Q | Incident | substantial |
inoperative deicing equipment, due to multiple wing boot holes and malfunctioning control/shuttle valves; subsequent build-up of airframe (wing) ice; …inoperative deicing equipment, due to multiple wing boot holes and malfunctioning control/shuttle valves; subsequent build-up of airframe (wing) ice; and failure of the pilot to maintain adequate airspeed during the flare for landing. Factors relating to the accident included: the adverse weather (icing) conditions, and inadequate maintenance concerning the deicing equipment. |
| Jul 02, 1996 | STILLWATER, OK | N450SU | Incident | substantial |
the failure of the pilots of the Cessna 421B, N450SU, and the Cessna 152, N94532, to maintain visual lookout. Factors were: the inadequate radio commu…the failure of the pilots of the Cessna 421B, N450SU, and the Cessna 152, N94532, to maintain visual lookout. Factors were: the inadequate radio communications maintained by both pilots, and the failure of the student pilot of the Cessna 152 to take evasive action. |
| Nov 17, 1995 | PEACHTREE CITY, GA | N707WC | Incident | substantial | Deer on the runway during a night landing that resulted in the collision. |
| Nov 12, 1995 | ROMEO, MI | N1588G | Incident | substantial | the failure of the pilot to maintain sufficient airspeed during landing, causing the inadvertent stall. A factor was the icing conditions. |
| Sep 07, 1995 | ALBUQUERQUE, NM | N5368J | Incident | substantial | THE PILOT'S INADEQUATE COMPENSATION FOR THE CROSSWIND CONDITION. A FACTOR WAS THE CROSSWIND. |
| Aug 28, 1995 | CHINLE, AZ | N745CA | Incident | substantial |
the pilot's selection of a runway inappropriate for the tailwind condition and his resultant failure to achieve a touchdown point which would allow th…the pilot's selection of a runway inappropriate for the tailwind condition and his resultant failure to achieve a touchdown point which would allow the aircraft to stop prior to over running the departure end. The rough condition of the dirt runway, the lack of lighted wind indicators, and the operator's failure to develop procedures for night operations at the airport are factors in the accident. |
| Aug 18, 1995 | CRESWELL, OR | N3121K | Incident | substantial | the company mechanic's failure to properly fabricate a fuel line. |
| Jan 21, 1995 | ANGOLA, IN | N421AW | Incident | substantial | OVERLOAD FAILURE OF THE RIGHT MAIN LANDING GEAR SHOCK STRUT SLEEVE FOR AN UNKNOWN REASON. |
| Dec 14, 1994 | CHINLE, AZ | N746CA | Incident | substantial | the overload failure of the nose gear trunion for undetermined reasons. |
| Oct 03, 1994 | STUART, FL | N701AM | Incident | substantial |
THE IMPROPER RIGGING OF THE LANDING GEAR SAFETY SQUAT SWITCH BY OTHER MAINTENANCE PERSONNEL. CONTRIBUTING TO THE ACCIDENT WAS THE CONTAMINATION OF THE…THE IMPROPER RIGGING OF THE LANDING GEAR SAFETY SQUAT SWITCH BY OTHER MAINTENANCE PERSONNEL. CONTRIBUTING TO THE ACCIDENT WAS THE CONTAMINATION OF THE GEAR SQUAT SWITCH WITH CORROSION AND WATER. |
| Jul 29, 1994 | OSHKOSH, WI | N819RA | Incident | substantial | the pilot-in-command's misjudging the flare and his failure to maintain airspeed. |