Cessna 421 Safety Record
Complete NTSB accident and incident history. 326 events recorded from 1982 to 2024.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jul 01, 2018 | Clifton, TX | N7625Q | Incident | substantial | The pilot's improper landing flare in crosswind conditions, which resulted in a hard landing. |
| Jun 11, 2018 | Plant City, FL | N13RF | Minor | substantial |
The pilot's delayed decision to abort the takeoff, which resulted in a runway overrun. Contributing to the accident was an engine anomaly for reasons …The pilot's delayed decision to abort the takeoff, which resulted in a runway overrun. Contributing to the accident was an engine anomaly for reasons that could not be determined based on the available information, and the pilot's failure to activate the runway lighting system before takeoff. |
| Jun 05, 2018 | Rock Sound, BF | N421MM | Fatal (3) | destroyed | Investigation pending |
| May 21, 2018 | Sandersville, GA | N427JM | Incident | substantial | A nose landing gear collapse for reasons that could not be determined based on the available information. |
| Nov 22, 2017 | Presque Isle, ME | N421RX | Minor | substantial |
The in-flight leakage of fuel from the fuel injection system's mixture shaft onto the hot turbocharger, which resulted in an in-flight fire, and the p…The in-flight leakage of fuel from the fuel injection system's mixture shaft onto the hot turbocharger, which resulted in an in-flight fire, and the pilot's inability to see the runway due to reduced visibility conditions and conduct a successful landing. |
| Jul 01, 2017 | Catawba, WI | N2655B | Fatal (6) | destroyed | A loss of control and subsequent in-flight breakup for reasons that could not be determined based on the available information. |
| Jun 22, 2017 | Carlsbad, CA | N380AL | Incident | substantial | The right main landing gear collapse for undetermined reasons. |
| Apr 25, 2017 | Huntsville, TX | N421TK | Fatal (1) | destroyed |
The pilot's failure to identify the alternate runway, to perform a timely precautionary landing, and to maintain airplane control. Contributing to the…The pilot's failure to identify the alternate runway, to perform a timely precautionary landing, and to maintain airplane control. Contributing to the accident was the failure of the left engine due to oil starvation for reasons that could not be determined based on the postaccident examination. |
| Mar 04, 2017 | Canton, GA | N421KL | Fatal (1) | substantial |
The pilot's failure to maintain control of the airplane during a night visual landing approach. Contributing to the accident was the pilot's impairmen…The pilot's failure to maintain control of the airplane during a night visual landing approach. Contributing to the accident was the pilot's impairment due to his use of a combination of medications. |
| Jan 07, 2017 | Jackson, CA | N71RC | Incident | substantial | The failure of the right main landing gear torque link bolt in overstress, which resulted in the collapse of the landing gear during the landing roll. |
| Apr 26, 2016 | Foley, AL | N3372Q | Minor | destroyed |
The pilot's failure to obtain proper takeoff speed before breaking ground, which resulted in the airplane’s failure to gain altitude and a collision w…The pilot's failure to obtain proper takeoff speed before breaking ground, which resulted in the airplane’s failure to gain altitude and a collision with trees and terrain. |
| Apr 13, 2016 | Death Valley, CA | N21SG | Incident | substantial | A runway overrun for reasons that could not be determined based on the available information. |
| Oct 14, 2015 | Amarillo, TX | N19CH | Incident | substantial |
The loss of directional control during taxi to the runway as a result of insufficient brake fluid level in the right brake master cylinder, resulting …The loss of directional control during taxi to the runway as a result of insufficient brake fluid level in the right brake master cylinder, resulting in a taxiway excursion and collision with a drainage culvert. |
| Oct 14, 2015 | Hammond, LA | N33FA | Fatal (2) | destroyed |
The loss of right engine power on takeoff due to maintenance personnel's failure to properly tighten the crankcase through-studs during cylinder repla…The loss of right engine power on takeoff due to maintenance personnel's failure to properly tighten the crankcase through-studs during cylinder replacement, which resulted in crankshaft fracture. Also causal were the pilot's failure to feather the propeller on the right engine and his failure to maintain control of the twin-engine airplane while maneuvering to return to the airport. |
| Sep 21, 2015 | Platteville, WI | N813CA | Minor | substantial | The partial loss of right engine power for undetermined reasons with insufficient runway remaining for the aborted takeoff. |
| Apr 17, 2015 | Diboll, TX | N421PK | Serious (1) | substantial |
The total loss of engine power due to the use of an improper fuel type. Contributing to the accident were the servicing of the airplane with the impro…The total loss of engine power due to the use of an improper fuel type. Contributing to the accident were the servicing of the airplane with the improper fuel, noncompliance with an airworthiness directive, and the fuel nozzle installed on the fueling truck. |
| Aug 28, 2014 | Las Cruces, NM | N51RX | Fatal (4) | destroyed |
The misfueling of the airplane with jet fuel instead of the required aviation fuel, and the resultant detonation and a total loss of engine power duri…The misfueling of the airplane with jet fuel instead of the required aviation fuel, and the resultant detonation and a total loss of engine power during initial climb. Contributing to the accident were the line service technician's inadvertent misfueling of the airplane, the pilot's inadequate supervision of the fuel servicing, and the fixed-base operator's use of a small fuel nozzle on its jet fuel truck. |
| May 24, 2014 | Dallas, TX | N936U | Incident | substantial | The improper rigging of the landing gear by maintenance personnel, which resulted in the landing gear collapse. |
| Apr 22, 2014 | Horseshoe Bay, TX | N866BS | Incident | substantial | The failure of the drive mechanism for the gearbox motor, which resulted in the gear not extending for the landing. |
| Mar 20, 2014 | Charleston, SC | N5929M | Incident | substantial | Inadequate maintenance, which resulted in the collapse of the right main landing gear during landing. |
| Sep 24, 2013 | Colombier-Saugnieu, FR | N556MB | Fatal (4) | destroyed | Investigation pending |
| Aug 27, 2013 | Paris, IL | N229H | Fatal (1) | destroyed |
The pilot's failure to abort the takeoff during the ground roll after detecting the airplane's degraded performance. Contributing to the accident was …The pilot's failure to abort the takeoff during the ground roll after detecting the airplane's degraded performance. Contributing to the accident was the pilot's decision to attempt a flight with a known problem with the left engine and the likely partial loss of left engine power for reasons that could not be determined during the postaccident examination of the engine. |
| May 16, 2013 | Floriston, CA | N421W | Fatal (1) | destroyed | The pilot's failure to maintain airplane control during descent while operating in instrument meteorological conditions. |
| May 01, 2013 | Oakland, CA | N216WA | Incident | substantial | A failure of the left main landing gear pivot bolt in overstress during landing. |
| Mar 27, 2013 | Amarillo, TX | N805DC | Incident | substantial |
Maintenance personnel's failure to detect the misadjustment of the left landing gear actuator's switch after recent maintenance, which prevented the l…Maintenance personnel's failure to detect the misadjustment of the left landing gear actuator's switch after recent maintenance, which prevented the landing gear from locking in the extended position and resulted in the landing gear collapsing during landing. |