Cessna 414 Safety Record

Complete NTSB accident and incident history. 149 events recorded from 1982 to 2026.

149

All Events

59

Incidents

15

Minor

16

Serious

58

Fatal (148 fatalities)

Date Location Reg# Severity Damage Probable Cause
May 02, 2022 Connellsville, PA N46TA Serious (1) substantial
The pilot/mechanic’s failure to properly secure two airplane avionics units, which resulted in the trays supporting the units to sag downward and beco…

The pilot/mechanic’s failure to properly secure two airplane avionics units, which resulted in the trays supporting the units to sag downward and become lodged in the movement area of the elevator bellcrank during the accident takeoff.

Oct 08, 2020 West Palm Beach, FL N8132Q Serious (7) substantial
The pilot’s inadequate preflight inspection during which he failed to detect a flight control abnormality, and his failure to expediently abort the ta…

The pilot’s inadequate preflight inspection during which he failed to detect a flight control abnormality, and his failure to expediently abort the takeoff, which resulted in the co-pilot performing a delayed aborted takeoff and the subsequent runway overrun.

Jun 26, 2014 Maryland Heights, MO N1552T Serious (1) destroyed The loss of left engine power for reasons that could not be determined due to impact and fire damage.
Jan 14, 2003 Palm Springs, CA N127WW Serious (1) substantial
The flight instructor's improper selection of the high boost position for the operating right engine while on base leg to land, which resulted in a lo…

The flight instructor's improper selection of the high boost position for the operating right engine while on base leg to land, which resulted in a loss of engine power of the right engine. Factors associated with the accident are the left engine's loss of power for an undetermined reason, the flight instructor's failure to feather the propellers of the affected engines, and his failure to maintain directional control, which resulted in an off-airport forced landing.

Jan 06, 2002 Sturgis, MI N6560C Serious (1) substantial
the inadequate in-flight emergency planning/decision, the checklist not followed and excessive approach altitude by the pilot. Contributing factors w…

the inadequate in-flight emergency planning/decision, the checklist not followed and excessive approach altitude by the pilot. Contributing factors were the loose oil return line and weather.

Mar 28, 2001 Minneapolis, MN N8247Q Serious (1) substantial
The pilot not maintaining the proper airspeed during the circling approach, the inadvertent stall and the subsequent loss of control. Factors were th…

The pilot not maintaining the proper airspeed during the circling approach, the inadvertent stall and the subsequent loss of control. Factors were the pilot's decision to continue the approach in weather conditions below the approach/landing minimums, the continued flight below the minimum descent altitude, the pilot not following the approach airspeed listed in the owner's manual, the air traffic controllers not issuing weather information to the pilot, and the weather conditions.

Oct 17, 2000 KIEL-HOLTENAU, GE DIDIT Serious (1) Investigation pending
Nov 18, 1998 MONROE, LA N30ML Serious (2) substantial The pilot's spatial disorientation which resulted in a loss of aircraft control. Factors were fog, low ceilings, and dark night conditions.
Nov 28, 1995 CLEVELAND, TN N200DC Serious (1) substantial
THE PILOT'S INACCURATE WEIGHT AND BALANCE CALCULATIONS WHICH RESULTED IN AN OVER MAXIMUM ALLOWABLE GROSS WEIGHT TAKEOFF. CONTRIBUTING TO THE ACCIDENT …

THE PILOT'S INACCURATE WEIGHT AND BALANCE CALCULATIONS WHICH RESULTED IN AN OVER MAXIMUM ALLOWABLE GROSS WEIGHT TAKEOFF. CONTRIBUTING TO THE ACCIDENT WAS THE WET, DOWNSLOPING CONDITION OF THE RUNWAY.

Oct 19, 1989 SAN ANTONIO, TX N5820H Serious (3) substantial
THE FAILURE OF THE RIGHT PROPELLER UNFEATHERING ACCUMULATOR HOSE DUE TO IMPROPER INSTALLATION AND CHAFFING, AND THE PILOT'S OPERATION OF THE AIRPLANE …

THE FAILURE OF THE RIGHT PROPELLER UNFEATHERING ACCUMULATOR HOSE DUE TO IMPROPER INSTALLATION AND CHAFFING, AND THE PILOT'S OPERATION OF THE AIRPLANE BEYOND ITS ENGINE OUT PERFORMANCE CAPABILITY. FACTORS WERE INADEQUATE COMPANY MAINTENANCE, AND THE PILOT'S CONTINUED OPERATION WITH KNOWN MECHANICAL MALFUNCTIONS, AND IMPROPER EMERGENCY PROCEDURES.

Dec 25, 1986 OLATHE, KS N414LL Serious (1) destroyed Investigation pending
Dec 07, 1986 MURTAUGH, ID N37561 Serious (2) destroyed Investigation pending
Oct 23, 1984 CHEYENNE, WY N1569T Serious (1) substantial Investigation pending
Oct 20, 1984 CHEYENNE, WY N1597T Serious (3) destroyed Investigation pending
Apr 01, 1984 DOUGLAS, WY N414EM Serious (2) substantial Investigation pending
Mar 23, 1982 JACKSON, MI N37174 Serious (2) destroyed Investigation pending
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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