Cessna 414 Safety Record
Complete NTSB accident and incident history. 149 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Mar 19, 2004 | Midland, TX | N414FB | Incident | minor | The in-flight wing fire for undetermined reasons. |
| May 26, 2003 | PORT JEFFERSON, NY | N1234 | Incident | destroyed | Loss of power to both engines for undetermined reasons. |
| Jun 01, 2000 | Prescott Valley, AZ | N414PS | Incident | substantial |
The pilot's physical impairment due to the cumulative effects of carbon monoxide from engine exhaust by-products, carbon monoxide from heavy tobacco u…The pilot's physical impairment due to the cumulative effects of carbon monoxide from engine exhaust by-products, carbon monoxide from heavy tobacco use, and the loss of an undetermined amount of cabin pressurization. A factor in the loss of pressurization was a fractured clamp. |
| Jun 13, 1999 | SPRINGDALE, AR | N475JN | Incident | substantial |
The failure of the right main landing gear torque tube support bracket/pivot bearing which resulted in the failure of the landing gear locking mechani…The failure of the right main landing gear torque tube support bracket/pivot bearing which resulted in the failure of the landing gear locking mechanism. |
| Feb 15, 1999 | PHOENIX, AZ | N1557T | Incident | substantial | The overload failure of the left main gear locking mechanism due to improper system rigging by maintenance personnel. |
| Sep 28, 1998 | BURLEY, ID | CGLHP | Incident | substantial | A brake system failure for undetermined reasons. An intentional ground loop was a factor. |
| Jan 27, 1997 | SPRINGFIELD, MO | N414AM | Incident | substantial |
the pilot's continued flight into known icing conditions with an inadequate windscreen deicing system and the diminished visual lookout. Factors were…the pilot's continued flight into known icing conditions with an inadequate windscreen deicing system and the diminished visual lookout. Factors were the icing weather conditions and the windscreen ice. |
| May 27, 1996 | BROOMFIELD, CO | N414AW | Incident | substantial | failure of the pilot to maintain adequate visual lookout by allowing his attention to be diverted. |
| Oct 27, 1995 | GRT BARRINGTON, MA | N2UD | Incident | substantial |
the pilot's inadequate compensation for wind conditions, which resulted in an undershoot of the proper touchdown point for landing. Factors relating …the pilot's inadequate compensation for wind conditions, which resulted in an undershoot of the proper touchdown point for landing. Factors relating to the accident were: the unfavorable wind conditions and the exposed runway lip. |
| Aug 30, 1993 | DICKINSON, ND | N36990 | Incident | minor | the total failure of the airplane's heater system combustion air pressure safety switch. |
| Jul 30, 1993 | LAKE CITY, FL | N4232C | Incident | substantial |
THE FAILURE OF THE PILOT-IN-COMMMAND TO PROPERLY FLARE BEFORE TOUCHDOWN AND THE PILOT'S DECISION TO LAND WITH EXCESSIVE AIRSPEED. A CONTRIBUTING FACTO…THE FAILURE OF THE PILOT-IN-COMMMAND TO PROPERLY FLARE BEFORE TOUCHDOWN AND THE PILOT'S DECISION TO LAND WITH EXCESSIVE AIRSPEED. A CONTRIBUTING FACTOR WAS THE APREHENSION/ANXIETY OF THE PILOT DURING THE PRECAUTIONARY LANDING. |
| Jul 03, 1993 | SEATTLE, WA | N4735A | Incident | substantial |
THE DISENGAGEMENT OF THE GEAR DOWN-LOCK MECHANISM DUE TO CORROSION AND THE PILOT'S INTENTIONAL OPERATION OF THE AIRCRAFT WITH KNOWN DEFICIENCIES IN EQ…THE DISENGAGEMENT OF THE GEAR DOWN-LOCK MECHANISM DUE TO CORROSION AND THE PILOT'S INTENTIONAL OPERATION OF THE AIRCRAFT WITH KNOWN DEFICIENCIES IN EQUIPMENT. |
| Dec 19, 1992 | REXBURG, ID | N911AG | Incident | substantial | THE PILOT DID NOT SELECT THE REMAINING FUEL SUPPLY. FACTORS INCLUDE A DETERIORATED FUEL SELECTOR VALVE. |
| Feb 13, 1992 | LOGANSPORT, IN | N4644G | Incident | substantial |
THE PILOT'S FAILURE TO MAINTAIN AN ADEQUATE APPROACH SPEED WHICH RESULTED IN AN IMPROPER FLARE. FACTORS CONTRIBUTING TO THE ACCIDENT WERE THE INADEQU…THE PILOT'S FAILURE TO MAINTAIN AN ADEQUATE APPROACH SPEED WHICH RESULTED IN AN IMPROPER FLARE. FACTORS CONTRIBUTING TO THE ACCIDENT WERE THE INADEQUATE INFLIGHT DEICING OF THE AIRFRAME SURFACES AND IN ICING CONDITIONS ENCOUNTERED. |
| Jan 19, 1992 | GAYLORD, MI | N6814R | Incident | substantial |
DIRECTIONAL CONTROL WAS NOT MAINTAINED BY THE PILOT. FACTORS RELATED TO THE ACCIDENT WERE: AIRPORT SNOW REMOVAL HAD NOT BEEN PERFORMED BY THE AIRPORT …DIRECTIONAL CONTROL WAS NOT MAINTAINED BY THE PILOT. FACTORS RELATED TO THE ACCIDENT WERE: AIRPORT SNOW REMOVAL HAD NOT BEEN PERFORMED BY THE AIRPORT PERSONNEL, A DARK NIGHT WITH FALLING SNOW AND THE SNOWBANK ON THE RUNWAY. |
| May 07, 1991 | PIQUA, OH | N222SV | Incident | substantial |
THE PILOT'S INCOMPLETE PREFLIGHT OF THE FUEL QUANTITY AND THE INACCURATE FUEL GAGES, WHICH RESULTED IN FUEL STARVATION AND TOTAL LOSS OF ENGINE POWER …THE PILOT'S INCOMPLETE PREFLIGHT OF THE FUEL QUANTITY AND THE INACCURATE FUEL GAGES, WHICH RESULTED IN FUEL STARVATION AND TOTAL LOSS OF ENGINE POWER AND SUBSEQUENT FORCED LANDING ON ROUGH TERRAIN. FACTORS RELATING TO THE ACCIDENT WERE THE PILOT'S IMPROPER INFLIGHT FUEL MANAGEMENT PROCEDURES AND HIS LACK OF EXPERIENCE IN THIS AIRPLANE. |
| Apr 06, 1991 | AVENAL, CA | N242AR | Incident | substantial |
THE FAILURE OF THE PILOT TO MAINTAIN DIRECTIONAL CONTROL AFTER STRIKING A DIRT BERM DURING THE LANDING ROLL. CONTRIBUTING TO THE ACCIDENT WAS THE FAIL…THE FAILURE OF THE PILOT TO MAINTAIN DIRECTIONAL CONTROL AFTER STRIKING A DIRT BERM DURING THE LANDING ROLL. CONTRIBUTING TO THE ACCIDENT WAS THE FAILURE OF THE PILOT TO ENSURE THAT THE AIRPORT WAS ADEQUATE FOR HIS INTENDED OPERATIONS. |
| Oct 17, 1990 | JACKSON, WY | N26853 | Incident | destroyed |
THE PILOT'S INADEQUATE PREFLIGHT PREPARATION OF THE AIRCRAFT, HIS FAILURE TO REMOVE SNOW AND ICE FROM THE AIRCRAFT BEFORE TAKEOFF, AND HIS DELAY IN AT…THE PILOT'S INADEQUATE PREFLIGHT PREPARATION OF THE AIRCRAFT, HIS FAILURE TO REMOVE SNOW AND ICE FROM THE AIRCRAFT BEFORE TAKEOFF, AND HIS DELAY IN ATTEMPTING TO ABORT THE TAKEOFF. |
| Mar 16, 1990 | RAMONA, CA | N711AG | Incident | destroyed |
RIGHT MAIN GEAR SCISSORS ASSEMLBY BECOMING DISCONNECTED DURING LANDING ROLL, ALLOWING THE RIGHT RUN LANDING GEAR TO COLLAPSE; SCISSOR ASSEMBLY WASHERS…RIGHT MAIN GEAR SCISSORS ASSEMLBY BECOMING DISCONNECTED DURING LANDING ROLL, ALLOWING THE RIGHT RUN LANDING GEAR TO COLLAPSE; SCISSOR ASSEMBLY WASHERS NOT BEING REPLACED AS RECOMMENDED IN CESSNA AIRCRAFT SERVICE BULLETIN ME83-37.. |
| Dec 11, 1989 | BULLHEAD CITY, AZ | N8247Q | Incident | substantial | THE PILOT'S FAILURE TO MAINTAIN SUFFICIENT CLEARANCE BETWEEN HIS AIRCRAFT AND GROUND OBJECTS DURING A TAXI TO THE RAMP AREA. |
| Dec 20, 1988 | PONTIAC, MI | N414CM | Incident | substantial | Investigation pending |
| Jan 01, 1988 | FAYETTEVILLE, AR | N30ML | Incident | substantial | Investigation pending |
| Jul 28, 1987 | CUBA, NM | N1648T | Incident | substantial | Investigation pending |
| Jun 11, 1987 | BINGHAMTON, NY | N2691S | Incident | substantial | Investigation pending |
| Dec 13, 1985 | GEORGETOWN, DE | N13FH | Incident | destroyed | Investigation pending |